United Treasure’s permit to work aloft system had not been effectively implemented on board the ship. In addition, the standard form for the permit did not ensure that the officer in charge of the work and its authoriser were not the same person and that a risk assessment was formally undertaken by at least two responsible officers.
The tower was not assembled as designed. The outriggers and intermediate planks, both key components, were missing and the work platform guard rails were not used. The manufacturer’s instructions were also missing but no attempt was made to obtain them, a parts list or the missing parts.
While enclosed space entry checklists were being filled out by the crew members on board Bow De Jin, the checklist system was not being used as a proactive means to ensure that the necessary safety requirements were being met prior to tank entries.
Following the separation of the IP turbine disc from the drive arm, the engine behaved in a manner that differed from the engine manufacturer’s modelling and experience with other engines in the Trent family, with the result that the IP turbine disc accelerated to a rotational speed in excess of its design capacity whereupon it burst in a hazardous manner.
Interruption of electrical power to the multi purpose flight recorder due to water ingress removed of an important source of information used to identify safety issues.
The lack of formalised procedures in place requiring the Air Crew Officer (ACO) to monitor key instrument indications probably contributed to the undetected altitude loss.
The absence of an altitude deviation alert within the Australian Defence Air Traffic System increases the risk of undetected altitude variation and contributed to the significant loss of altitude.
The design and relative positioning of the external air vent and avionics modules permitted the ingress of moisture and particulates that led to corrosion and contamination of electronic avionics components and consequently the generation of multiple erroneous crew alerting system (CAS) messages due to electrical shorting.
The procedures for connecting and disconnecting the import hose and disconnecting from the CALM buoy in place on board Karratha Spirit were signed off as being satisfactory and reflecting shipboard practice, but they had not been effectively reviewed on board the ship. Consequently, the ambiguities in the procedures and the discrepancies between the procedures and the ship’s practices were not identified during any shipboard review or audit and were not made known to the ship’s managers through any review process.
In this instance, the consensus of the regulatory authorities is that Karratha Spirit was not in a navigable form at the time of the accident and was therefore under NOPSA’s jurisdiction according to the OPGGSA. However, the point at which Karratha Spirit became ‘navigable’ is not clearly defined in the OPGGSA and is open to interpretation.
The ship’s procedures for connecting and disconnecting from the CALM buoy did not provide explicit, succinct and unambiguous guidance and there were differences between the procedures and the actual shipboard practices that increased the level of risk associated with those operations
The Job Hazard Analysis (JHA) for disconnecting from the CALM buoy did not provide an accurate assessment of the all of the hazards and associated risks in performing the task. In addition, the crew did not use it to assess the risks associated with undertaking an unfamiliar operation and it was reviewed without any involvement from the crew. Consequently, the JHA was not an effective means for assessing and controlling the risks associated with the operation of disconnecting from the CALM buoy.
NOPSA does not undertake the audits necessary for maritime compliance and AMSA is only able to do so, while the facility is on station, with NOPSA’s cooperation. NOPSA had carried out annual occupational health and safety inspections on board the ship and AMSA had carried out the necessary third party audits of the system to meet its certification requirements. However, none of these audits or inspections had identified the discrepancy between the mooring hawser procedures and actual shipboard practices or that the ship’s internal review processes had not identified the discrepancy.
The servo valve within the left green aileron servo was incorrectly adjusted during manufacture.
The aircraft operator did not comply with the reporting requirements of the Transport Safety Investigation Act 2003.
Fatigue cracking originated within the aircraft nose landing gear (NLG) right axle as the result of surface damage associated with grinding during manufacture, and was probably assisted in its initiation by hydrogen evolved during plating processes.