Investigation number
199602557
Occurrence date
Location
Brisbane
State
Queensland
Report release date
Report status
Final
Investigation type
Occurrence Investigation
Investigation status
Completed
Occurrence class
Incident

During climb, passing 5,300 ft, a loud bang was heard. The pilot initially thought the noise to be a birdstrike, however it was noticed that the inner cowl on the left engine had fallen from the aircraft. The pilot elected to return to Brisbane. Post flight inspection revealed that the cowl had torn off along the hinge line and had struck the fuselage forward of the entry door causing denting and scoring of the fuselage skin.

The aircraft had undergone maintenance on the previous day, but no work had been done on the left engine, and there was no known reason for the left engine cowl to be unfastened. The copilot, who performed the daily inspection in the early hours of the morning (it was still dark) had not noticed the cowl was not properly fastened. The cause of the cowl being unfastened could not be determined.

Aircraft Details
Manufacturer
Beech Aircraft Corp
Model
B300
Registration
VH-OXF
Operation type
Charter
Sector
Turboprop
Departure point
Brisbane QLD
Destination
Blackwater QLD
Damage
Minor