On 18 April 2017, at about 0934 Western Standard Time, a Bombardier DHC-8-315 aircraft, registered VH-XKI, departed from Meekatharra Airport, Western Australia (WA), for a charter flight to Leinster, WA. There were two flight crew, two cabin crew and 49 passengers on board.
The captain reported that the aircraft performed as normal during the take-off run. However, at some point between retracting the flap and 1,000 ft above ground level, the flight crew experienced a vibration through the airframe and noticed a change in the pitch of the aircraft noise (deep pitch sound). The flight crew noticed the right propeller was at about 500 RPM (normal governed flight range is 900–1200 RPM) and the engine torque was excessively high. The low propeller RPM and high engine torque led them to conclude the malfunction was an ‘unscheduled feather’ incident.
The flight crew shutdown the right engine, in accordance with their emergency operating procedures. Noting that the aircraft was above the maximum landing weight, the flight crew reviewed the performance charts, and concluded that the runway at Meekatharra was suitable for an emergency landing and elected to return. The aircraft landed without incident. No persons were injured and the aircraft was not damaged.
The aircraft captain reported that they felt the incident was handled well by the flight crew and cabin crew. They found that the use of automation was effective in reducing their workload while responding to the malfunction. The captain reported that the incident was completely unexpected, which highlighted to them the need for, and benefit of, regular simulator training.
Aviation Short Investigations Bulletin Issue 61
What happened
On 18 April 2017, at about 0934 Western Standard Time (WST), a Bombardier DHC-8-315 aircraft, registered VH-XKI, departed from Meekatharra Airport, Western Australia (WA), for a charter flight to Leinster, WA. There were two flight crew, two cabin crew and 49 passengers on board.
The aircraft had departed from Perth Airport, WA, at about 0540 that morning, on a charter flight to Leinster, with Meekatharra as the alternate airport. While the aircraft was en route to Leinster, the flight crew received an updated weather report, which indicated there was fog present at Leinster. The flight crew conducted one approach at Leinster and as they did not get visual with the runway, they diverted to Meekatharra. While on the ground at Meekatharra, the captain received a report from their[1] operations department in Perth that the weather at Leinster had improved. The captain elected to depart Meekatharra with sufficient fuel for the flight to Leinster while maintaining Meekatharra as the alternate airport.
The captain reported that the aircraft performed as normal during the take-off run. After take-off, the landing gear was retracted, followed by the flap.[2] At some point between retracting the flap and 1,000 ft above ground level, the flight crew experienced a vibration through the airframe and noticed a change in the pitch of the aircraft noise (deep pitch sound). The flight crew noticed the right propeller was at about 500 RPM (normal governed flight range is 900–1200 RPM) and the engine torque was excessively high.[3] The low propeller RPM and high engine torque led them to conclude the malfunction was an ‘unscheduled feather’[4] incident.[5]
While the aircraft climbed to the lowest safe altitude, the flight crew shutdown the right engine, in accordance with their emergency operating procedures. Once at their lowest safe altitude, the flight crew engaged the autopilot, completed the checklist actions and made a PAN[6] radio broadcast to air traffic control. Noting that the aircraft was above the maximum landing weight, the flight crew reviewed the performance charts, and concluded that the runway at Meekatharra was suitable for an emergency landing and elected to return. The flight crew briefed the cabin crew that they were going to land overweight with one engine shutdown and therefore to prepare the cabin for an emergency landing. The aircraft landed without incident. No persons were injured and the aircraft was not damaged.
Unscheduled autofeather
The autofeather system meets the regulatory requirements for an automatic take-off thrust control system, and in the event of an engine failure, the system:
- trims the opposite engine power by a pre-determined amount to permit continued safe take-off without pilot intervention
- feathers the propeller of the failing engine to minimise the drag after a three second time delay.
In the event of an engine failure on take-off (less than 29 per cent torque sensed), the failed engine torque signal conditioning unit (TSCU) initiates autofeathering by switching its logic from ‘arm’ to ‘arm and fail.’ A relay signals the engine control unit (ECU) of the other engine to increase power (uptrim) to compensate for the failed engine (Figure 1). After 3 seconds, the TSCU logic transitions from ‘arm and fail’ to ‘fail and feather’. This isolates the second engine’s TSCU to disable its autofeather system to ensure both propellers cannot be feathered at the same time, and energises the failed engine feathering solenoid to feather the propeller of the failed engine.
Figure 1: Autofeather overview for no.2 (right) engine failure

Source: ATSB (information from aircraft manufacturer)
Aircraft inspections
The operator’s maintenance organisation downloaded the flight data recorder for analysis by the engine manufacturer. It was determined that an uptrim signal was sent to the left engine by the right engine TSCU and the right engine experienced an over-torque event of 146% for 25 seconds.[7] Both engine control units provided several fault codes, which were investigated with no defects found. The right engine TSCU and propeller hub and blades were replaced in accordance with the directions from the respective manufacturers. The right engine reduction gearbox[8] and oil system were inspected with no defects found. In addition, the right engine electronic controller was replaced for troubleshooting purposes.
In 2002 the aircraft manufacturer published an in-service engineering and technical support letter titled ‘Autofeather arming and uncommanded autofeather events’. The purpose of the letter was to identify uncommanded autofeather events and suggest solutions. The maintenance organisation referred to this letter for troubleshooting and completed the procedures for ‘autofeather during power applications’ and ‘autofeather during take-off or climb with the system armed (uncommanded).’ No defects were found. It was determined from the flight data analysis that a heavy landing inspection was not required. After several engine ground runs were conducted at take-off power with the autofeather system armed, without any faults, the aircraft was flown to Perth. The flight to Perth was reported as uneventful and the aircraft was returned to service.
Safety action
Whether or not the ATSB identifies safety issues in the course of an investigation, relevant organisations may proactively initiate safety action in order to reduce their safety risk. The ATSB has been advised of the following proactive safety action in response to this occurrence.
Operator
As a result of this occurrence, the aircraft operator has advised the ATSB that they are taking the following safety actions:
Maintenance inspections
The operator’s continuing airworthiness management organisation has scheduled recurrent inspections of the reduction gearbox oil system and are following up with the engine manufacturer for their findings concerning the removed engine electronic controller and torque signal conditioning unit.
Safety message
The aircraft captain reported that they felt the incident was handled well by the flight crew and cabin crew. They found that the use of automation was effective in reducing their workload while responding to the malfunction. Despite the fact that both cabin crew were relatively new to the company, the captain could clearly hear them making their emergency landing calls to the passengers in accordance with their emergency operating procedures. The captain reported that the incident was completely unexpected, which highlighted to them the need for, and benefit of, regular simulator training.
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