Investigation number
199301894
Occurrence date
State
New South Wales
Report release date
Report status
Final
Investigation type
Occurrence Investigation
Investigation status
Completed
Aviation occurrence category
Abnormal engine indications
Occurrence class
Incident

The pilot reported that during cruise, the engine had a tendency to overspeed when the power lever was retarded but was operating normally at high power. He elected to proceed to the destination with high power set. When power reduction was required for landing a precautionary engine shut down was carried out and a single engine landing was made. Investigation revealed that the concentric control shafts at the fuel control unit were binding and causing mutual interference. The shafts were lubricated and the overspeed defect disappeared. The aircraft had been washed recently. Failure to reapply lubrication after the wash probably contributed to the defect. Significant factors: The FCU concentric control shafts were not lubricated after the aircraft was washed.

Aircraft Details
Manufacturer
Mitsubishi Aircraft Int
Model
MU-2B-30
Registration
VH-WMW
Sector
Turboprop
Departure point
Bankstown NSW
Destination
Wagga Wagga NSW
Damage
Nil