While conducting a 20° right turn at about 1,750 ft above ground level, there was a sudden loss of engine power. The propeller continued to windmill. The pilot established a glide attitude, confirmed the power loss, and attempted to restart the engine. The pilot reported that the fuel selector was changed from the right tank to ‘BOTH’, the throttle was opened a one-quarter inch, and the fuel-air mixture set to ‘rich’, but the engine did not restart. They could not recall if the electric auxiliary fuel boost pump was applied, which was required by the aircraft manufacturer’s emergency ‘airstart’ procedure. The pilot also stated that the environmental conditions during the flight were ‘very bumpy due to thermal activity.’
At about 750 ft, the pilot abandoned attempts to start the engine and committed to executing a forced landing. The landing gear and flaps were selected down, and a large field was chosen for the landing. A MAYDAY call was made and the aircraft’s location broadcast on the common traffic advisory frequency. The aircraft landed without incident.
A visual inspection of the aircraft was completed by the pilot and no damage was found. The pilot checked the fuel tanks and measured about 100 L in the left tank, and nil indication of fuel in the right tank. The pilot had checked the right tank during the pre-flight inspection and noted 65 L at that time. It was reasoned that the nil indication of the right tank was due to the angle of the aircraft at the time of the check. The pilot concluded that the engine failure was due to ‘fuel starvation due to the prolonged turn and angle of bank/choppy winds.’
The engine was restarted with the fuel tank selector on the left tank and the auxiliary fuel boost pump on. Checks were conducted and the engine performed as expected. With the belief that the power loss was due to a low fuel level, and after an assessment of the field and a discussion with the passenger, it was decided to fly back to the Swan Hill. The pilot also noted that they were close to the airport and there were other small fields available if another power loss occurred en route.
After landing at Swan Hill, further assessment of the issue was conducted. The right fuel tank was checked with the aircraft level and 47 L of fuel was indicated. However, the engine would not start or run without the auxiliary boost pump on, regardless of the fuel tank selector position. After consulting maintenance personnel, the engine-driven mechanical fuel pump was suspected to have failed. This pump had been installed new during a recent engine rebuild.
Fuel pumps
The aircraft was fitted with an engine-driven mechanical fuel pump, which provided a continuous flow of fuel to the engine. The pump design allowed pressurised fuel from the auxiliary fuel pump to flow through it in the event of a failure. The electric auxiliary fuel pump was controlled by a 2-position switch in the cockpit and was used as a boost for starting, or in the event the engine-driven pump failed.
Emergency engine airstart procedure
The pilot’s operating handbook emergency procedures checklist specified the following conditions for a windmilling engine airstart:
maintain a minimum airspeed of 82 kt for a windmilling propeller
fuel selector is on the fuller tank; the procedure specifically noted not to use the BOTH position
mixture is rich
throttle position is at least half open
ignition switch is selected to ‘BOTH’
auxiliary fuel pump is on.
Safety message
This incident highlights the importance of sound pilot judgement and aeronautical decision‑making. The United States Federal Aviation Administration (Pilot’s Handbook of Aeronautical Knowledge) recommends pilots use the perceive, process, and perform model to aid decision-making by utilising a number of checklists. When discussing the various steps within the checklists, it was specifically noted that:
It is important to recognize the reality of an aircraft’s mechanical condition. If you find a maintenance discrepancy and then find yourself saying that it is “probably” okay to fly with it anyway, you need to revisit the consequences…
While no further issues occurred on the subsequent flight to Swan Hill, system failures can occur in many ways, often without an obvious reason and can sometimes be transient in nature. Whenever there is any doubt as to the serviceability of an aircraft, specialist assistance should be sought, and a thorough inspection completed prior to flight resuming.
It is further emphasised that pilots should also know and understand an aircraft’s emergency procedures and be able to perform them from memory.
About this report
Decisions regarding whether to conduct an investigation, and the scope of an investigation, are based on many factors, including the level of safety benefit likely to be obtained from an investigation. For this occurrence, no investigation has been conducted and the ATSB did not verify the accuracy of the information. A brief description has been written using information supplied in the notification and any follow-up information in order to produce a short summary report, and allow for greater industry awareness of potential safety issues and possible safety actions.
During the take-off roll, there were no abnormal performance indications. After take-off, the aircraft did not perform as expected and the pilot observed a decreasing airspeed. The pilot considered the urban terrain ahead and rejected the take-off, landing on the remaining runway. The aircraft subsequently overran the runway and stopped in the overrun area.
Operator comments
The operator investigation revealed the maximum take-off weight (MTOW) may have been exceeded with the centre of gravity (COG) positioned at or forward of the forward limit.
The aircraft flight manual weight and balance documents were found to be misleading. The documents displayed a permitted MTOW for aircraft of a certain serial number range of which the incident aircraft did not apply. Additionally, the weight and balance documentation stated the data was valid for occupant weights within a certain range. The pilot was unaware of this restriction.
The pilot calculated the COG at take-off to be on the forward limit and elected to carry ballast in the cargo bay. This ballast was not secured and may have moved during the take-off.
Safety action
As a result of this incident, the operator has implemented the following safety actions:
The operator has amended company operations to permit a blanket MTOW below the permitted MTOW for all PA-28-161 aeroplanes to account for any variances.
All pilots will be weighed on a regular basis if there is a likelihood of a maximum take-off weight (MTOW) or performance limit exceedance.
The operator has implemented a structured ballast system including marked water containers, tie down straps and accompanying standard operating procedures.
Safety message
This incident highlights the importance of ensuring accurate weights are used when completing weight and balance documentation as part of pre-flight preparations. Accurate passenger weights should be obtained if the pilot in command believes a weight or balance limitation may be exceeded.
Pilots should also have a thorough understanding of the aircraft flight manual weight and balance documentation, including any restrictions and limitations for all aircraft operated by the operator.
About this report
Decisions regarding whether to conduct an investigation, and the scope of an investigation, are based on many factors, including the level of safety benefit likely to be obtained from an investigation. For this occurrence, no investigation has been conducted and the ATSB did not verify the accuracy of the information. A brief description has been written using information supplied in the notification and any follow-up information in order to produce a short summary report, and allow for greater industry awareness of potential safety issues and possible safety actions.
Occurrence summary
Mode of transport
Aviation
Occurrence ID
AB-2022-016
Occurrence date
28/09/2022
Location
Bankstown
State
New South Wales
Occurrence class
Incident
Aviation occurrence category
Aircraft preparation
Highest injury level
None
Brief release date
08/02/2023
Aircraft details
Manufacturer
Piper Aircraft Corp
Sector
Piston
Operation type
Part 141 Recreational, private and commercial pilot flight training
On the morning of 18 July 2022, a Kavanagh E-260 hot air balloon, registered VH-FSR (FSR) and a Kavanagh B-400 hot air balloon, registered VH-OOP (OOP) were being operated on a balloon transport flight about 6 km south‑east of Alice Springs Airport. Both balloons were operated by Red Centre Ballooning.
At 0700, FSR was flying at about 900 ft above ground level (AGL) within a faster north-easterly wind, while about 1,150 m ahead, OOP was at about 100 ft AGL within a slower westerly wind.
At that time, the pilot of FSR decided to descend to the lower-level wind (below 200 ft AGL) to slow the balloon. Before descending, the pilot of FSR incorrectly judged OOP to also be flying in the higher, faster wind and assessed that FSR would descend behind OOP while maintaining sufficient separation.
During the descent, the pilot of FSR realised that OOP was flying lower and more slowly than initially assessed and recognised that a collision was possible. The pilot of FSR was aware that a basket to envelope collision carried the risk of tearing the envelope of the lower balloon and controlled the descent so that any collision would be between the balloon envelopes.
At 0702, the two balloons collided close to the widest point of each envelope. The balloons were not damaged and there were no injuries. After the collision, the balloons separated, and the flights continued without further incident.
What the ATSB found
The ATSB found that while attempting to descend to a position behind OOP, the pilot of FSR misjudged the speed and direction of OOP and descended FSR toward OOP. After recognising that a collision was likely, the pilot of FSR then managed the balloon's descent so that a basket did not collide with an envelope, reducing the risk of damage.
What has been done as a result
The operator has educated all company pilots on radio and passenger communications and close proximity balloon operations.
Safety message
While in this case, the pilots were able to avoid damage during the collision, this incident highlights the importance of evaluating all available options to support good decision making. The Civil Aviation Safety Authority Resource booklet Decision Making provides the following tips to improve the quality of decision making:
You cannot improvise a good decision, you must prepare for it. You will make a better and timelier final decision if you have considered all options in advance.
Always have reserve capacity for reacting to unexpected events.
Where possible, advise others of your plans before you act. This increases the chances of successful follow through on your decision and ensures people are not caught unaware.
When time is not so critical, involve others in the decision making. That way everybody is more invested in the decision and therefore are likely to be more motivated to support it.
This incident also highlights the risks of misinterpreting what is seen. The Civil Aviation Safety Authority Advisory Circular AC 91-14 Pilots' responsibility for collision avoidance provides guidance for collision avoidance including:
Not only is seeing important, but accurately interpreting what is seen is equally vital.
The investigation
Decisions regarding the scope of an investigation are based on many factors, including the level of safety benefit likely to be obtained from an investigation and the associated resources required. For this occurrence, a limited-scope investigation was conducted in order to produce a short investigation report, and allow for greater industry awareness of findings that affect safety and potential learning opportunities.
Before departing, the pilots released a pilot balloon[2] to determine wind conditions. The pilots observed that up to about 200 ft above ground level (AGL) a 3‑5 kt westerly wind prevailed. Above this was a 100 ft thick layer of calm air. Extending above the calm layer was a north‑easterly wind of about 10‑15 kt (Figure 1). The pilots also noted that cloud and visibility conditions were clear.
Figure 1: Departure site and prevailing winds
Source: Google Earth, annotated by ATSB
Both balloons departed at about 0645 local time. On board FSR was a pilot and 10 passengers, while OOP had a pilot and 23 passengers on board.
At about 0700, FSR was flying at about 900 ft above ground level (AGL) within the faster north‑easterly wind, while 1,150 m ahead, OOP was at about 100 ft AGL within the slower westerly wind. At about this time, the pilot of FSR decided to descend to the lower-level wind (below 200 ft AGL) to slow the balloon.
Before descending, the pilot of FSR incorrectly judged OOP to also be flying in the faster wind. Consequently, the pilot of FSR assessed that FSR would descend behind OOP with sufficient separation and made a radio broadcast using an ultra-high frequency (UHF) radio advising of the descent. The pilot of FSR did not confirm that the pilot of OOP had received and understood the broadcast.
During the descent, the pilot of FSR realised that OOP was flying lower and more slowly than initially assessed. When the distance between the two balloons reduced to about 250 m, the pilot of FSR recognised that a collision was possible.
About 40 seconds before the eventual collision, the pilot of OOP observed FSR closing and recognised the potential for contact (Figure 2), so called the pilot of FSR 4 times using a UHF radio. During that time, the pilot of FSR was focussed on managing the descent and misinterpreted these broadcasts as communications between other balloons that were operating in the area and therefore did not reply.
Figure 2: Overview of flights
Note: The balloon flightpaths were not recorded, the tracks depicted are representative only of the overall flights.
Source: Google Earth and operator, annotated by ATSB
The pilot of FSR was aware that a basket to envelope collision carried the risk of tearing the envelope of the lower balloon and so attempted to control the descent such that any collision would be between the balloon envelopes. FSR continued to decelerate slowly, but the balloon’s momentum continued to carry it toward OOP. To minimise the risk of envelope to basket contact, the pilot of OOP attempted to maintain a steady altitude. As FSR closed on OOP, the pilot of OOP alerted the passengers to the likely collision.
At 0702, the two balloons collided close to the widest point of each of their envelopes (Video 1). The balloons were not damaged and there were no injuries. After the collision, the balloons separated, and the flights continued without further incident.
Video 1: The collision
Source: Passenger aboard FSR
Context
Pilot information
The pilot of FSR held a Commercial Pilot Licence (Balloon) valid for Class 1 and Class 2 balloons.[3] At the time of the occurrence the pilot had accrued a total flying time of 1,010 hours, with 258 hours on the E-260 hot air balloon (Class 2). The pilot also held a current CASA Class 2 aviation medical certificate.
The pilot of OOP was the operator’s Head of Operations and also held a Commercial Pilot Licence (Balloon) valid for Class 1 and Class 2 balloons. At the time of the occurrence the pilot had accrued a total flying time of about 4,415 hours, with about 600 hours on the B-400 hot air balloon (Class 2). The pilot held a current CASA Class 2 aviation medical certificate.
A review of both pilots’ activities over the 72 hours prior to the occurrence identified that it was unlikely that either pilot was experiencing a level of fatigue known to affect performance.
Aircraft information
VH-FSR was a Kavanagh Balloons E-260 hot air balloon manufactured in 2009. The E‑260 balloon had an envelope capacity of 260,000 cubic feet (7,362 cubic meters) and a maximum take-off weight of 2,184 kg.
VH-OOP was a larger Kavanagh Balloons B-400 hot air balloon. The B‑400 balloon had an envelope capacity of 400,000 cubic feet (11,327 cubic meters) and a maximum take-off weight of 3,100 kg.
Airspace
The incident occurred within Alice Springs airspace. At the time of the incident, the control tower was not active, and the airspace was operating as class G airspace, utilising a common traffic advisory frequency.
Communications and collision avoidance
The balloons were equipped with both very-high frequency and ultra-high frequency (UHF) communications radios.
The Civil Aviation Safety Regulation (CASR) Part 91 Manual of Standards, Chapter 21 stated that when in the vicinity of a non-controlled aerodrome, a pilot must make a broadcast when the pilot ‘considers it reasonably necessary to broadcast to avoid the risk of a collision with another aircraft’.
The operator’s operations manual stated:
When in close proximity to other Company balloons establish contact on UHF Radio... The upper balloon will be responsible for avoiding basket to envelope contact between balloons. The lower balloon will acknowledge calls.
The operations manual also included a Civil Aviation Safety Authority (CASA) instrument, which stated:
Whilst in flight give way to any balloon at a lower level by climbing to avoid the risk of the balloon basket contacting the envelope of the lower balloon, and
except during inflation and launching, avoid envelope to envelope contact with other balloons.
At the time of the occurrence, CAR 163 had been superseded by the following CASRs:
91.055 - Aircraft not to be operated in a manner that creates a hazard
91.325 - A flight crew member must, during a flight, maintain vigilance, so far as weather conditions permit, to see and avoid other aircraft.
On 13 August 1988, two hot air balloons, VH-NMS and VH-WMS, were operating tourist charter flights from the same launch site to the south‑east of Alice Springs Airport. VH-WMS departed about 2 minutes ahead of VH-NMS and climbed to about 4,000 ft AMSL (2,000 ft AGL) and drifted in a westerly direction. After reaching 4,000 ft, VH-WMS then commenced descending as VH-NMS climbed towards it.
VH-NMS continued climbing until its envelope collided with the basket of VH-WMS, tearing a large hole in the fabric. The degree of disruption to the envelope of VH-NMS was such that the balloon could not remain inflated. The balloon then descended uncontrolled until it collided with terrain. The pilot and 12 passengers were fatally injured. VH-WMS landed without further incident.
Safety analysis
While flying at about 900 ft above ground level (AGL) in 10‑15 kt winds, the pilot of hot air balloon VH-FSR (FSR) decided to descend to slow the balloon’s progress. The pilot of FSR observed VH-OOP (OOP), which was flying at about 100 ft AGL and about 1,150 m ahead within a layer of slow wind. However, the pilot of FSR misjudged the height of OOP and believed it to be flying higher in the same faster moving air stream that FSR was operating in. Based on that assessment, the pilot of FSR believed that sufficient separation would be maintained as FSR descended to a position behind OOP at a similar altitude. However, this misjudgement resulted in FSR converging toward OOP as it descended.
During the descent the pilots of both balloons identified the risk of collision. In response to the conflict, the pilot of OOP made 4 radio broadcasts to communicate with the pilot of FSR. However, the pilot of FSR was concentrating on managing the descent and misinterpreted these calls as communications between other balloons and not relevant so did not respond. However, by this time, it was unlikely that action could be taken to avoid the collision.
The pilot of FSR assessed that a collision could not be avoided and knowing the risks of basket to envelope contact, attempted to manage the descent so that the envelopes collided. To assist in avoiding basket to envelope contact, the pilot of OOP attempted to maintain a steady altitude. Although the envelope collision still carried safety risk, these actions resulted in the balloons avoiding basket to envelope contact and neither balloon was damaged in the collision.
Findings
ATSB investigation report findings focus on safety factors (that is, events and conditions that increase risk). Safety factors include ‘contributing factors’ and ‘other factors that increased risk’ (that is, factors that did not meet the definition of a contributing factor for this occurrence but were still considered important to include in the report for the purpose of increasing awareness and enhancing safety). In addition, ‘other findings’ may be included to provide important information about topics other than safety factors.
These findings should not be read as apportioning blame or liability to any particular organisation or individual.
From the evidence available, the following findings are made with respect to the mid-air collision between Kavanagh E-260, VH-FSR and Kavanagh B-400, VH-OOP on 18 July 2022.
Contributing factors
While attempting to descend to a position behind VH-OOP, the pilot of VH-FSR misjudged the speed and direction of VH-OOP and descended VH-FSR toward VH-OOP.
After recognising that a collision was likely, the pilot of VH-FSR managed the balloon's descent so that a basket and envelope did not collide, reducing the risk of damage.
Safety actions
Whether or not the ATSB identifies safety issues in the course of an investigation, relevant organisations may proactively initiate safety action in order to reduce their safety risk. The ATSB has been advised of the following proactive safety action in response to this occurrence.
Proactive safety action by Red Centre Ballooning
In response to the occurrence, the operator provided education to all company pilots emphasising:
the need to make radio communications advising of intentions when operating in close proximity if anything out of the ordinary. If required, use alternative means of communication such as mobile phone.
the importance of passenger communication to the passengers throughout a flight. This could include but is not limited to layover landings and flying around other aircraft.
that higher balloons should overfly lower balloons before descending as higher balloons are generally travelling faster than lower balloons and may still be carrying some forward momentum after completion of a descent.
the requirements of the company operations manual, including operating in accordance with the Civil Aviation Safety Authority instrument.
Sources and submissions
Sources of information
The sources of information during the investigation included the:
balloon operator
pilots of the VH-FSR and VH-OOP
Civil Aviation Safety Authority
Airservices Australia
balloon passengers
Bureau of Meteorology
References
Civil Aviation Safety Authority 2021, Advisory Circular AC 91-14 v1.0 Pilots’ responsibility for collision avoidance, October 2021
Submissions
Under section 26 of the Transport Safety Investigation Act 2003, the ATSB may provide a draft report, on a confidential basis, to any person whom the ATSB considers appropriate. That section allows a person receiving a draft report to make submissions to the ATSB about the draft report.
A draft of this report was provided to the following directly involved parties:
the balloon operator and the involved pilots
the Civil Aviation Safety Authority
Submissions were received from:
the balloon operator and the involved pilots
the Civil Aviation Safety Authority
The submissions were reviewed and, where considered appropriate, the text of the report was amended accordingly.
Purpose of safety investigations
The objective of a safety investigation is to enhance transport safety. This is done through:
identifying safety issues and facilitating safety action to address those issues
providing information about occurrences and their associated safety factors to facilitate learning within the transport industry.
It is not a function of the ATSB to apportion blame or provide a means for determining liability. At the same time, an investigation report must include factual material of sufficient weight to support the analysis and findings. At all times the ATSB endeavours to balance the use of material that could imply adverse comment with the need to properly explain what happened, and why, in a fair and unbiased manner. The ATSB does not investigate for the purpose of taking administrative, regulatory or criminal action.
Terminology
An explanation of terminology used in ATSB investigation reports is available here. This includes terms such as occurrence, contributing factor, other factor that increased risk, and safety issue.
Publishing information
Released in accordance with section 25 of the Transport Safety Investigation Act 2003
Ownership of intellectual property rights in this publication
Unless otherwise noted, copyright (and any other intellectual property rights, if any) in this report publication is owned by the Commonwealth of Australia.
Creative Commons licence
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Creative Commons Attribution 3.0 Australia Licence is a standard form licence agreement that allows you to copy, distribute, transmit and adapt this publication provided that you attribute the work.
The ATSB’s preference is that you attribute this publication (and any material sourced from it) using the following wording: Source: Australian Transport Safety Bureau
Copyright in material obtained from other agencies, private individuals or organisations, belongs to those agencies, individuals or organisations. Where you wish to use their material, you will need to contact them directly.
[1] The flight was operated under Civil Aviation Safety Regulations Part 131 (Balloons and hot air airships).
[2] A method of determining winds aloft by tracking the ascent of a small free-lift balloon.
[3] The Civil Aviation Safety Authority (CASA) classifies balloons into three classes. Class 1 – Hot air balloons that have a volume of not more than 260 000 cubic feet. Class 2 – Hot air balloons that have a volume of more than 260 000 cubic feet. Class 3 – Gas balloons.
Dash 8 cabin could not pressurise due to removal of the recirculation fan previously during maintenance;
The unserviceability was not detected by the operator or the flight crew prior to take-off;
Operator Maroomba Airlines has taken action to prevent a re-occurrence.
A charter airline has taken a series of safety actions after one of its Dash 8 aircraft took off in an unserviceable state from Perth in 2021, resulting in the cabin failing to pressurise, an Australian Transport Safety Bureau investigation report notes.
On the morning of 20 November 2021, a Maroomba Airlines Dash 8 turboprop left Perth as a charter flight to Port Hedland, Western Australia.
Approaching 10,000 ft after take-off, flight crew observed the cabin had not pressurised. At this altitude oxygen masks were not needed, but attempts to rectify the problem in flight were unsuccessful and the flight crew opted for an immediate return to Perth.
“It was found the aircraft failed to pressurise because its recirculation fan had been removed during maintenance the day prior, and this meant that the cabin was not fully sealed,” ATSB Director Transport Safety Dr Michael Walker said.
The ATSB investigation found Maroomba’s operations personnel incorrectly interpreted a message from the engineering department regarding the aircraft’s maintenance status, and it remained assigned to the charter flight.
“This allocation also remained on the flight crew’s roster and the flight manifest, which contributed to the flight crew’s confidence that the aircraft was serviceable,” Dr Walker said.
“As there were no defects recorded in the aircraft’s defect summary, the captain did not check the maintenance log, which was where the fan’s removal was recorded.
“Also, the captain reset a circuit breaker that had been opened to facilitate the fan removal without fully reviewing the maintenance documentation as per the operator’s flight crew operating manual.”
Since the incident, the operator has taken a range of steps to avoid a recurrence.
These include refining the terminology used by the engineering department to communicate aircraft serviceability, reviewing internal communication methods, and reiterating existing paperwork and circuit breaker resetting requirements.
“All tasks, including those that may seem innocuous, should be performed as though they are the last defence to ensure safe operation,” Dr Walker said.
“The aircraft documents are the primary record of airworthiness, and this occurrence shows that thoroughly checking them remains an important control to determine if the aircraft can be operated.”
On the afternoon of 18 January 2023, a Boeing 737-838 aircraft, registered VH-XZB and operated by Qantas, departed Auckland, New Zealand on a scheduled passenger service to Sydney, Australia. While in the cruise, about 1 hour and 24 minutes after departure, there was an uncommanded shutdown of the left engine. Due to their location at the time, the flight crew declared a MAYDAY, to prioritise communications with air traffic control and to ensure they were cleared for an immediate descent to flight level 240 (24,000 ft). The engine could not be restarted in-flight, and the flight crew conducted an uneventful single-engine landing at Sydney Airport about 1 hour later.
What the ATSB found
The engine examination identified separation of the radial driveshaft (located in the inlet gearbox), which resulted in a mechanical discontinuity between the engine core and accessory gearbox. Loss of drive to the accessory gearbox resulted in a loss of fuel pump pressure and uncommanded shutdown of the engine. There was also secondary damage to some components as the engine shut down. In addition, the failed driveshaft prevented the engine restarting in-flight.
Further, the ATSB found that the cockpit voice recorder was inadvertently overwritten during maintenance activities conducted after the aircraft arrived at Sydney Airport.
What has been done as a result
As a result of this incident, Qantas has enhanced their procedures to prevent inadvertent overwrite of cockpit voice recorders and flight data recorders.
Safety message
It has been well established that the importance of training, following standard procedures, and effective communications are crucial to aviation safety. This incident highlighted the positive benefits of effective decision-making and management of an unexpected situation. Such actions are best demonstrated by:
maintaining a high level of situation awareness, utilising all sources of information, via procedural checklists and communications, including with cabin crew and air traffic control
consideration of all options and evaluation to decide the best course of action to ensure additional operational difficulties are not inadvertently introduced
a frequent review to ensure appropriate actions are being maintained throughout changing circumstances.
In addition, operators need to ensure correct procedures are in place to protect information recorded during the flight that enhances the accuracy and effectiveness of a safety investigation.
On the afternoon of 18 January 2023, a Boeing 737-838 aircraft, registered VH-XZB and operated by Qantas Airways, was being prepared for a scheduled passenger service from Auckland, New Zealand to Sydney, Australia. On board were 2 flight crew, 5 cabin crew and 143 passengers. The captain was designated as the pilot flying and the first officer was the pilot monitoring.[1]
The captain reported that the pre-flight briefing package identified good weather conditions for Auckland, en route, and Sydney. The weather forecast for additional airports was also included, in case of the requirement for a diversion. The flight was dispatched as an extended diversion time operations (EDTO)[2] flight authorised to operate up to 180 minutes or 1,200 NM (2,222 km) from an alternate aerodrome. The required EDTO maintenance had been completed in Auckland. This inspection included engine and auxiliary power unit (APU)[3] oil quantity checks, and a review of recent oil consumption records. The aircraft departed Auckland at 1430 local time and reached a cruise altitude of flight level (FL)[4] 360 about 20 minutes later.
The flight crew reported that they carried out an EDTO brief before entering the EDTO segment. The EDTO briefing included that, in the event of an engine failure, Auckland and Sydney were the primary airports.
After about 1 hour in the cruise, the flight crew transferred high frequency (HF) radio communications from Auckland to the en route controller at Brisbane Centre (en route controller).[5] Once the en route controller accepted monitoring of the aircraft, the flight crew requested to climb to FL 380. About 3 minutes later, and before the climb was authorised, the flight crew reported hearing a ‘pop’ sound, followed by the autopilot and auto throttle disengaging, with associated warning lights and horn. They then identified left (#1) engine was not operating. The flight crew broadcast MAYDAY,[6] citing an engine failure and requested an immediate descent to FL 240. The en route controller enquired if it was a single or double engine failure, to which the flight crew confirmed a single-engine failure (Figure 1). About 1 minute later, the en route controller authorised a descent to FL 240 when ready.
Figure 1: Map showing VH-XZB flight path and location of the engine failure
Source: APS Flight Analysis System (FAS) using Cesium, annotated by the ATSB
At the same time, following the completion of cabin service, the cabin safety manager (CSM) heard a noise and felt the aircraft yawing in a manner they described as ‘not normal’. After confirming that the cabin crew member next to them had also experienced the event, the CSM advised that they called the flight deck. The captain answered and advised the CSM that they could not talk at that moment as an engine had just failed. The CSM then called the cabin crew team leader at the rear of the cabin to inform them of the situation.
About 5 minutes later, the captain called the CSM to the flight deck and explained the situation, in that the left engine had shut down uncommanded and they were unsure why. The captain further advised that the aircraft was operating safely on one engine, and they were working through the engine failure, and associated checklists. The captain requested that the CSM relay this information to the cabin crew, monitor the passengers and to advise the flight deck if anything changed in the cabin.
Soon after, the CSM advised the flight crew that the cabin was getting quite warm[7] and power was not available to various galley equipment and the rear bathrooms.[8] The APU had been selected to ‘on’ as part of the engine failure checklist, however, cabin airflow had been affected. The flight crew reported they then selected the temperature controller to minimum and conditions improved.
The flight crew continued working through the non-normal checklists, while on a slow descent. Following authorised descent to FL 200, and with all checklists completed, the flight crew decided to attempt the in-flight engine restart checklist. While the first few steps were accomplished, the engine start attempt had to be aborted when a designated parameter could not be achieved. The flight crew then consolidated their plan and prepared for a single-engine landing at Sydney.
Throughout the descent into Sydney, en route and Brisbane Centre air traffic controllers[9] maintained contact with the flight crew, with scheduled check-in times to ascertain location details, operational status, and updates to any requirements in Sydney.
Just prior to top of descent, the flight crew advised Brisbane Centre they were downgrading from a MAYDAY to PAN PAN[10] but would still like aviation rescue fire-fighting services to attend and inspect the left engine before they proceeded to the terminal. Shortly after, air traffic control (ATC) communications were transferred to Sydney.
At about this time the captain made an announcement to the passengers, stating:
they were to commence the descent into Sydney in a few minutes time
acknowledging there were some issues with one engine that was affecting the air-conditioning and some electrical systems
once on the ground, emergency services would attend the aircraft to inspect the engine, as a precaution, before they proceeded to the terminal
reassuring them that everything was okay, and they would make another announcement once on the ground.
Following an uneventful landing at Sydney at 1526 local time, emergency services met the aircraft on the taxiway. Once cleared, the aircraft was taxied to the terminal, where engineering personnel conducted an additional inspection before the airbridge was positioned. At this point, the captain made a further announcement advising that they had experienced an engine failure about 1 hour out of Sydney. The captain thanked the passengers for their patience and understanding. In addition, the flight crew exited the flight deck and personally addressed each passenger as they disembarked.
The captain held an Air Transport Pilot (Aeroplane) Licence, a current Class 1 Aviation Medical Certificate, and had accumulated 12,335 hours of aeronautical experience. Of this, about 1,620 hours were on the Boeing 737 type, and the captain had logged 230 hours in the preceding 90 days.
The first officer also held an Air Transport Pilot (Aeroplane) Licence, a current Class 1 Aviation Medical Certificate, and had accumulated 10,540 hours of aeronautical experience. Of this, about 794 hours were on the Boeing 737 type, and they had logged 165 hours in the preceding 90 days.
The training records showed the most recent full flight simulator session for the captain was completed in September 2022 and for the first officer in October 2022. In addition, the captain had practiced one engine inoperative situations (including during the cruise, missed approach and landing phases of flight) in November 2020, with the first officer completing this training in February 2022.
The flight crew reported being well rested and alert at the commencement of duty for the flight and there was no evidence to indicate that fatigue affected their performance during the flight.
Aircraft and engine information
General information
VH-XZB was a Boeing Company 737-838 aircraft, powered by 2 CFM56-7B26E[11] high bypass turbofan engines. The engine is a dual-rotor, axial-flow turbofan. The N1 refers to the rotational speed of the low-speed spool, which consists of a fan, a low‑pressure compressor and a low‑pressure turbine. N1 is the primary indication of engine thrust. The N2 refers to the rotational speed of the high-speed spool, which consists of a high-pressure compressor (HPC) and a high‑pressure turbine. The N1 and N2 rotors are mechanically independent. The N2 rotor drives the engine gearboxes.
When the engine is running, the accessory drive system extracts part of the core engine power, from the HPC (or N2) and transmits it through a series of shafts and gearboxes, to drive the engine and aircraft accessories, including the:
fuel pump and hydromechanical unit
hydraulic pump
integrated drive generator.
The starter, also located on the accessory gearbox, used the same gearboxes and shafts to drive the HPC for engine start, either on the ground or in-flight.
Engine examination
An engine teardown inspection was conducted by the engine manufacturer at their technical facility in Malaysia and was observed by Qantas and the Air Accident Investigation Bureau Malaysia (on behalf of the ATSB). The examination identified that the inner radial driveshaft separated at 2 locations, at the mid-length bearing and near the upper spline (Figure 2). Subsequently, the mechanical discontinuity between the HPC shaft and accessory gearbox resulted in loss of fuel pump pressure and uncommanded shutdown of the engine. The mid-length bearing oil feed nozzle appeared clear (nil blockage). There was secondary damage to some components as the engine spooled down.
The failed driveshaft also prevented the starter from driving the HPC, which prevented the in‑flight engine restart.[12]
Figure 2: CFM56-7B engine, showing the accessory gearbox location, associated driveshafts and failure locations (red line)
Source: Operator, annotated by the ATSB
The manufacturer advised that the level of deterioration of the failed driveshaft and mid-length bearing prevented identification of the separation initiator. Further, the inner driveshaft oil supply features were destroyed by the bearing failure and therefore its condition at the time of the event could not be determined. Nevertheless, the engine manufacturer reported that the rupture of the inner driveshaft was considered the primary failure.
It was noted that the CFM56-7B world engine fleet had reported 7 similar radial driveshaft bearing events since 2012. However, there was no consistent component time accumulation prior to the failure. At the time of this incident, the approximate totals for the worldwide fleet were 15,200 engines, with 500 million hours in-service and 258 million cycles in-service.
Engine maintenance requirements
The engine oil system included scavenge screens and magnetic chip detectors that could collect any debris suspended in the oil. Metal contamination of the oil could be indicative of abnormal wear or impending failure of a component. Any metal contamination was to be examined to identify its origin and ascertain the quantity of the material. The engine manufacturer’s procedures then detailed steps to monitor or replace the affected component. In addition, an increase in oil consumption would require further inspection as per maintenance procedures.
The left engine was the original engine for the aircraft and had not been subject to any major repairs or overhaul. On 11 December 2022, a 500-hourly inspection was completed on the left engine oil system. This included a detailed inspection of the forward sump, aft sump, accessory and transfer gearboxes magnetic chip detectors and scavenge screens for debris and/or metal contamination. Further, the EDTO inspection completed in Auckland on 18 January 2023 included a review of the engine oil consumption over the previous 10 flights, to ensure it was within prescribed limits. Maintenance records indicated no metal contamination was identified and the oil consumption was within prescribed limits.
Recorded information
The cockpit voice recorder was downloaded at the ATSB’s technical facilities in Canberra. However, as the aircraft had been powered for maintenance activity following arrival at Sydney Airport, without the cockpit voice recorder being isolated, the audio data recorded during the incident flight was overwritten and not available for this investigation.
Data from the flight data recorder and quick access recorder was provided to the ATSB by the operator. The data showed that, 1 hour and 24 minutes after take-off from Auckland, the left engine abruptly shut down uncommanded. Further analysis of the data did not identify any appreciable changes to engine parameters, such as vibrations or temperature increase, prior to the failure. The flight crew also reported that there were no adverse indications prior to the sudden engine shutdown.
Operational procedures
Declaration of MAYDAY and PAN PAN
The operator’s procedures defined a MAYDAY and PAN PAN call consistent with the international standards as:
MAYDAY: A condition of being threatened by serious and/or imminent danger and requiring immediate assistance.
PAN PAN: A condition concerning the safety of an aircraft or other vehicle, or some person on board or within sight, but which does not require immediate assistance.
The flight crew considered the following regarding their decision to declare a MAYDAY:
their location mid-way between Auckland and Sydney, and considerable distance to any other suitable airport
desire to establish priority communication with Brisbane Centre via HF, which the flight crew reported could be busy and unreliable at times[13] (there was no satellite communication on the aircraft, therefore, HF radio was the only means of communication with ATC at that time)[14]
requirement to ensure the airspace was clear for an immediate descent to an optimal altitude for single-engine operation and aircraft controllability
uncertainty of the reason for the uncommanded shutdown and whether the remaining engine may also be affected.
Further, the flight crew advised that their decision to downgrade to a PAN PAN was based on the following:
their reducing distance to their destination, and effective very high frequency communications with Sydney ATC
all checklists were completed
continued stable operation on one engine
single-engine landing at Sydney had been planned and briefed by the flight crew.
Decision to continue to Sydney
The final step in the engine failure or shutdown checklist stated ‘plan to land at the nearest available airport’. The operator’s procedures stated that, ‘in a non-normal situation, the pilot-in-command, having the authority and responsibility for operation and safety of flight, must make the decision to continue the flight as planned or divert’. The procedures also stated considerations should include suitability of nearby airports in terms of facilities and weather, in decision-making where ‘the safest course of action is divert to a more distant airport than the nearest airport’.
At the time of the engine failure, the aircraft was located about (distance from) (Figure 3):
Auckland 611 NM (1,132 km) and a 180° turn
Sydney 560 NM (1,037 km) continuing on the current track
Williamtown/Newcastle 550 NM (1,019 km) with a slight diversion to right of track
Norfolk Island 484 NM (896 km) and a 115° right turn.
Figure 3: Engine failure location with respect to the 400 NM (741 km) EDTO radius from nearby alternate airports
Source: Google Earth, annotated by the ATSB
The Qantas Route Manual Supplement section for Norfolk Island noted several difficulties associated with the airport including:
‘actual weather can change rapidly and vary from forecast’ and a diversion to Australia may be required
high terrain near the airport and rising terrain at the end of runway 11 could result in the illusion of being too high on approach
strong winds in February and March could produce severe turbulence
no mobile services
the supplement-authorised runway at Norfolk Island was identified as 1,950 m long.
The flight crew reported that Sydney was on their direct route, the forecast weather conditions were more favourable, and the airport offered extensive emergency response (if required). In addition, their planned runway for landing was on a straight-in approach and 3,962 m long. The flight crew therefore elected to continue to Sydney.
Flight and cabin crew training
The captain and CSM had flown together previously, however, it was the first time either of them had flown with the first officer. The flight crew and CSM reported that the operator’s crew resource management training, which was conducted with flight and cabin crew combined, fostered an understanding of each area of operation, enabling openness and free-flowing sharing of information between the flight deck and cabin. In addition, role-specific training and use of standard procedures allowed them to each focus on their required tasks during an unanticipated situation.
While Norfolk Island was closer at the time of the engine failure, a diversion required a deviation from their current track. In addition, Norfolk Island presented changeable weather and operational conditions. In contrast, Sydney Airport was on their direct route, had favourable weather conditions forecast, had an extensive emergency response, and a straight‑in approach on a very long runway. The flight crew’s decision to continue to Sydney ensured no additional risk was added to an already high workload situation.
The ATSB publication Black box flight recorders highlights the benefits of aircraft flight recorders such as the cockpit voice recorder, by creating a record of the total audio environment in the cockpit area. This includes crew conversations, radio transmissions, aural alarms, and ambient cockpit sounds, check list management, and decision making. As highlighted in the ATSB’s publication, around 80% of aircraft accidents involve human factors, which means that crew performance may have contributed to some events. As a result, the cockpit voice recorder often provides accident investigators with invaluable insights into why an accident occurred. In this case, the recorded audio of this incident was inadvertently overwritten during maintenance operations. However, flight data was available and was found to be consistent with the flight crew’s recollections and ATC audio recordings.
Findings
ATSB investigation report findings focus on safety factors (that is, events and conditions that increase risk). Safety factors include ‘contributing factors’ and ‘other factors that increased risk’ (that is, factors that did not meet the definition of a contributing factor for this occurrence but were still considered important to include in the report for the purpose of increasing awareness and enhancing safety). In addition ‘other findings’ may be included to provide important information about topics other than safety factors.
These findings should not be read as apportioning blame or liability to any particular organisation or individual.
From the evidence available, the following findings are made with respect to the engine failure involving Boeing Company 737-838, VH-XZB, en route between Auckland, New Zealand and Sydney, Australia, on 18 January 2023.
Contributing factors
During cruise, separation of the radial driveshaft led to a mechanical discontinuity between the engine core and accessory gearbox. This resulted in loss of the accessory gearbox-driven main fuel pump pressure and uncommanded shutdown of the left engine. In addition, the failed driveshaft prevented the engine from being restarted in-flight.
Based on the more favourable forecast weather conditions and operational requirements, the flight crew decided to continue to Sydney rather than divert to Norfolk Island, which ensured that no additional risk was added to an already high workload situation.
The cockpit voice recorder was inadvertently overwritten during maintenance activity following the incident flight. Although not critical to this investigation, this information could have provided direct evidence regarding the flight crew's coordination, check list management, and decision making throughout the flight.
immediately notify the duty technical manager to raise a task in the maintenance software to have the requested item quarantined (or at a minimum, power to the recorders is to be removed)
follow up with a telephone call to the respective port and ensure the ground engineer is advised of the limited timeframe to secure the data
continually follow up with the applicable ports until positive confirmation of the requested action has been confirmed.
Under section 26 of the Transport Safety Investigation Act 2003, the ATSB may provide a draft report, on a confidential basis, to any person whom the ATSB considers appropriate. That section allows a person receiving a draft report to make submissions to the ATSB about the draft report.
A draft of this report was provided to the following directly involved parties:
Qantas Airways Limited
the flight crew and cabin service manager on VH-XZB
engine manufacturer
United States National Transportation Safety Board
New Zealand Transport Accident Investigation Commission.
The submissions were reviewed and, where considered appropriate, the text of the report was amended accordingly.
Purpose of safety investigations
The objective of a safety investigation is to enhance transport safety. This is done through:
identifying safety issues and facilitating safety action to address those issues
providing information about occurrences and their associated safety factors to facilitate learning within the transport industry.
It is not a function of the ATSB to apportion blame or provide a means for determining liability. At the same time, an investigation report must include factual material of sufficient weight to support the analysis and findings. At all times the ATSB endeavours to balance the use of material that could imply adverse comment with the need to properly explain what happened, and why, in a fair and unbiased manner. The ATSB does not investigate for the purpose of taking administrative, regulatory or criminal action.
Terminology
An explanation of terminology used in ATSB investigation reports is available here. This includes terms such as occurrence, contributing factor, other factor that increased risk, and safety issue.
Publishing information
Released in accordance with section 25 of the Transport Safety Investigation Act 2003
Ownership of intellectual property rights in this publication
Unless otherwise noted, copyright (and any other intellectual property rights, if any) in this report publication is owned by the Commonwealth of Australia.
Creative Commons licence
With the exception of the Coat of Arms, ATSB logo, and photos and graphics in which a third party holds copyright, this publication is licensed under a Creative Commons Attribution 3.0 Australia licence.
Creative Commons Attribution 3.0 Australia Licence is a standard form licence agreement that allows you to copy, distribute, transmit and adapt this publication provided that you attribute the work.
The ATSB’s preference is that you attribute this publication (and any material sourced from it) using the following wording: Source: Australian Transport Safety Bureau
Copyright in material obtained from other agencies, private individuals or organisations, belongs to those agencies, individuals or organisations. Where you wish to use their material, you will need to contact them directly.
[1] Pilot flying (PF) and pilot monitoring (PM): procedurally assigned roles with specifically assigned duties at specific stages of a flight. The PF does most of the flying, except in defined circumstances; such as planning for descent, approach and landing. The PM carries out support duties and monitors the PF’s actions and the aircraft’s flight path.
[2] Extended diversion time operations (EDTO): Any operation by an aeroplane with 2 or more turbine engines where the diversion time to an en route alternate aerodrome is greater than the threshold time established by the State of the Operator. For VH-XZB, the threshold time was 60 minutes, or 400 NM (741 km).
[3] The auxiliary power unit (APU) is a self-contained gas turbine engine, located in the tail of the airplane. The APU supplies bleed air for engine starting or air conditioning. An alternating current (AC) electrical generator on the APU provides an auxiliary AC power source.
[4] Flight level: at altitudes above 10,000 ft in Australia, an aircraft’s height above mean sea level is referred to as a flight level (FL). FL 360 equates to 36,000 ft.
[5] Brisbane Centre’s flight information region includes the Oceanic airspace off the east coast of Australia. Aircraft flying between Auckland and Sydney travel through Brisbane airspace for a significant portion of their journey.
[6] MAYDAY: an internationally recognised radio call announcing a distress condition where an aircraft or its occupants are being threatened by serious and/or imminent danger and the flight crew require immediate assistance.
[7] Two air-conditioning systems were powered independently by each engine, therefore operating on a single engine reduced airflow to the cabin.
[8] Primary AC power was supplied by 2 engine-driven generators. During flight, if one power source was lost, certain systems would be shed (automatically removed) in a sequence (from least critical to flight safety), to reduce electrical load. Engaging the APU could reduce/reverse shedding, depending on total aircraft electrical load.
[9] Brisbane en route handed over to Brisbane Centre when the aircraft entered VHF radio range, shortly after reaching FL 240.
[10] PAN PAN: an internationally recognised radio call announcing an urgency condition which concerns the safety of an aircraft or its occupants but where the flight crew does not require immediate assistance.
[11] CFM International is 50-50 joint venture between GE Aviation (United States) and Safran Aircraft Engines (France).
[12] The engine in-flight restart checklist required 11% N2 (HPC rotation) to be achieved before fuel was introduced. In this incident, this parameter was not achieved and the attempted re-start was aborted by the flight crew.
[13] The aircraft was not equipped with SATCOM and the reliability of HF can vary considerably, depending on the time of the day, frequency used and range over water, among other things.
[14] VHF relay via nearby aircraft was also possible, in the event that HF become unavailable and nearby aircraft were monitoring that frequency.
Occurrence summary
Investigation number
AO-2023-007
Occurrence date
18/01/2023
Report release date
03/08/2023
Report status
Final
Investigation level
Short
Investigation type
Occurrence Investigation
Investigation status
Completed
Mode of transport
Aviation
Aviation occurrence category
Engine failure or malfunction
Occurrence class
Incident
Highest injury level
None
Aircraft details
Manufacturer
The Boeing Company
Model
737-838
Registration
VH-XZB
Serial number
39360
Aircraft operator
Qantas Airways Litd
Sector
Jet
Operation type
Part 121 Air transport operations - larger aeroplanes
Statement can be attributed to ATSB Chief Commissioner Angus Mitchell
Last night the Australian Transport Safety Bureau commenced a transport safety investigation into the in-flight engine failure incident involving a Qantas 737 aircraft during a flight from Auckland to Sydney.
The ATSB has assigned a team of three experienced transport safety investigators, with experience in aircraft maintenance, aircraft operations, and data recovery, to commence the evidence collection phase of this investigation.
At the ATSB’s request the operator has quarantined the aircraft’s cockpit voice and flight data recorders. Once downloaded, information from those recorders will be analysed at the ATSB’s technical facilities in Canberra.
Other likely investigation activities will include interviewing the flight crew, reviewing operator procedures, analysing weather information, examining any relevant engine components, and potentially attending any tear-down inspection of the engine.
Our investigators will now work methodically to progressively establish the incident’s sequence of events and contextual information, with a view to determining contributing factors and any underlying safety issues, which will be detailed in the investigation’s final report.
The scope of the investigation and its timeframe will be determined as the ATSB build its understanding of the nature of the event.
Passenger-carrying operations are the ATSB’s highest investigation priority, and, as with all ATSB investigations, if at any time during the course of this investigation we uncover any critical safety issues, we will immediately share those with relevant stakeholders so timely safety action can be taken.
On 8 January 2023, the pilot of a Robinson R44 helicopter, registered VH-ZUJ, noticed a persistent clutch warning light on approach to Hamilton Island Airport, Queensland, and carried out the clutch warning light emergency procedure. The aircraft landed at Hamilton Island Airport, where ground crew found that the clutch actuator electric drive motor had separated from the gearmotor assembly and fallen between the drive belts and the right-hand fan shroud.
What the ATSB found
The ATSB established that during assembly of the gearmotor the required thread adhesive was not applied, or applied in a manner that did not prevent the loosening of the electric motor retaining nut. Consequently, over time, normal aircraft vibrations loosened the retaining nut, resulting in the clutch actuator electric motor separating from the gearmotor assembly in flight.
What has been done as a result
Robinson Helicopter Company advised that they are actively working with the component manufacturer to rectify identified quality issues with the gearmotor assembly and are considering updating the procedures for the inspection of the clutch actuator assembly.
Safety message
Personnel involved in maintenance and operation of R44 helicopters should be aware of the risks posed by the failure of this component, specifically the risk of a loose component interfering with the v-belts and impacting rotor drive. The ATSB encourages pilots and maintenance engineers to physically check the security of the R44 clutch gearmotor assembly on a regular basis.
Hand checking the motor for security, with electrical power off or visual inspection for motor rotation during operation are 2 methods that may detect a loosening motor prior to complete separation.
If a defect is identified, the gearmotor assembly should be replaced and the defect reported to the Civil Aviation Safety Authority and the manufacturer.
At about 1130 local time the aircraft departed Qualia helipad, with no passengers aboard, for a positioning flight to Hamilton Island Airport. On approach to runway 14, at about 300 meters from the threshold, the pilot noted the illumination of the clutch caution light.
The pilot waited for 10 seconds, then, as the light did not extinguish, they pulled the clutch motor circuit breaker in accordance with the clutch warning light emergency procedure in the pilot’s operating handbook. The landing was completed at Hamilton Island Airport and the aircraft was shut down without further incident.
Ground crew visually inspected the drive belt tensioner assembly and found that the clutch actuator electrical drive motor had separated from the gear assembly and was found between the drive belts and fan shroud. The motor was still attached electrically to the aircraft, and the gear assembly was securely attached to the drive belt tensioner assembly. (Figure 1)
The Robinson R44 helicopter's rotor drive system incorporates a belt driven common shaft for main and tail rotor drive. Power is transmitted from the engine to the main and tail rotors through vertically mounted sheaves (also commonly called drive pulleys) and a v-belt arrangement (Figure 2). The drive assembly carries 4 double‑banded v-belts. Each drive belt consists of 2 single v-belts that are bonded by a common rubber backing (tie-band). The lower drive sheave is bolted to the output flange of the engine crankshaft, while the upper sheave is located immediately above on the common main and tail rotor driveshaft.
Before the engine is started, the clutch actuator is placed in the disengaged position, which leaves the v-belts slack and allows the engine to start and run freely without the load of the main and tail rotors. A pilot-operated, electrically‑driven actuator progressively tensions the drive belts and enables power transfer from the engine to the rotor system.
Figure 2: R44 clutch assembly
Source: Robinson Helicopter Company. Modified for clarity and annotated by the ATSB
Drive belt clutch system
The clutch actuator is vertically positioned between the upper and lower sheaves. When the actuator is engaged, the upper sheave and clutch shaft are moved upward, applying tension to the drive belts. A column spring arrangement within the clutch actuator senses the compressive load caused by increasing belt tension and stops the actuator gearmotor when the tension reaches a pre-set value. The actuator also incorporates up limit switches to prevent over extension due to belt stretching, and a down limit switch to set the clutch disengaged positions. The clutch gearmotor assembly uses an electric motor to drive the actuator, via a worm-drive[1] arrangement, which ensures that belt tension forces are not fed back into the actuator motor; this allows the motor to be de-energised and belt tension to be maintained. The gearmotor assembly is attached to the belt tensioner by 4 corrosion resistant screws. (Figure 2)
A clutch caution light is illuminated in the cockpit whenever the gearmotor is running, either engaging or disengaging the clutch. It is normal for the clutch caution light to illuminate briefly during flight as the actuator re-tensions the drive belts to maintain the correct drive belt tension.
Gearmotor assembly
The clutch actuator electrical motor and gear assembly, collectively known as the gearmotor assembly, are factory assembled. The assembly is not field serviceable or repairable, requiring return to the manufacturer if unserviceable. The motor is attached to the drive gear by a threaded, free‑rotating, captive retaining nut. The retaining nut is secured with a commercially available thread locking adhesive and torqued with a c-spanner using castellations built into the nut, The electric motor case is then partially slid over the retaining nut, covering the castellations. (Figure 3) The design does not include a mechanical locking device, and no visual indication of loosening creep is embodied.
The incident gearmotor assembly was retained and inspected by the ATSB. The inspection noted the following (Figure 4):
No unusual damage to the threads of the electric motor or gear assembly was evident.
A black residue was found in the root of the gear assembly threads. This residue was not chemically identified due to an insufficient amount available for analysis.
The thread locking compound specified was designed to fluoresce in ultraviolet light to enable inspection of the fastener. The ATSB assembled a test piece with the locking compound and when disassembled the compound was evident when examined under ultraviolet light.
No evidence of thread adhesive was found on the engaging threads of either part of the incident gearmotor assembly under ultraviolet, or visible light conditions.
Fluorescent residue was found on a threaded section of the gear assembly, outside of the engaging threads section.
Loosening of threaded fasteners subject to vibration or rotation is an established and understood phenomenon of aircraft operation.[2] Secondary locking devices and assembly torque are carefully designed to minimise the risk of the threaded fastener loosening in service. Thread adhesive can be used as a secondary locking mechanism to mitigate vibration‑induced loosening of threaded fasteners.
The thread adhesive specified for the gearmotor is a medium strength adhesive designed for permanent locking and sealing. Once cured, it has a wide operating temperature and requires parts to be heated to 232°C to reduce the adhesive strength for disassembly. The tightening torque applied to a threaded fastener is calculated, in part, by taking into account the opposing friction created between the threads during the torquing process.
Thread locking adhesive can have a secondary effect of lubrication of the threaded fastener during assembly and tightening. This lubrication allows a greater proportion of the torquing force to be converted into clamping force between 2 parts. The increased clamping force contributes to a reduction in vibration induced loosening.[3]
Gearmotor scheduled inspections
Scheduled inspection of the clutch actuator assembly is limited to a visual inspection and functional checking of the assembly during 100-hour/1-year inspections, up to its 2,200-hour overhaul life. The inspection procedure specifies inspections of the upper and lower bearings and testing of the limit switches, among other visual inspections. It does not specify a check for security of the gearmotor assembly, or of the electrical motor.
At the time of the incident the aircraft had a total of 133 flight hours, with the 100-hour inspection certified on 23 December 2022. All the required inspections were carried out on the clutch actuator assembly at this time, and no defects were noted by the certifying licenced aircraft maintenance engineer.
Pilot action
If the clutch caution light illuminates in flight, and does not go out within 10 seconds, the pilot’s operating handbook, clutch caution light emergency procedure, instructed pilots to:
…pull CLUTCH circuit breaker and land as soon as practical. Reduce power and land immediately if there are other indications of drive system failure (be prepared to enter autorotation). Have drive system inspected for possible malfunction.[4]
It is likely that the electric motor separated from the gear assembly sometime between the pilot engaging the clutch after start, and the continuous illumination of the clutch caution light immediately prior to landing. The clutch system attempted to re-tension the belts and as the motor had separated from the gear assembly, the motor ran continuously, illuminating the clutch caution light.
On noticing the clutch caution light and waiting the requisite 10 seconds, the pilot carried out the clutch caution light emergency procedure and was able to land immediately. Had the landing been delayed in this incident it is possible that the position of the electric motor, between the drive belts and right fan shroud, could have caused damage to the drive belts and created a hazard to the safety of flight.
Safety analysis
The gearmotor assembly process incorporated the application of a thread adhesive designed to act as a secondary locking device to prevent the inadvertent loosening of the electric motor due to normal helicopter vibrations in flight. ATSB inspection of the threaded sections of the incident gearmotor under ultraviolet light showed that the thread adhesive was not visible in an area that would reliably ensure the security of the motor. This resulted in loosening of the motor due to normal operating vibrations. The reason for the absence of thread locking adhesive on the mating surfaces of the threads could not be determined.
The absence of thread adhesive during assembly, and its associated lubricating effect, probably reduced the intended design clamping force between the gear assembly and electric motor. It is important to note that the residue found in the gear assembly threads was not chemically identified so the impact it had on adhesion or lubrication, could not be assessed. The extent to which these factors influenced the failure of the gearmotor assembly was not determined, but it is possible that a reduced assembly clamping load contributed to the failure.
The integrity and effectiveness of thread adhesives are difficult to determine by visual inspection alone, and generally require specialised tooling or procedures to accurately assess. It is therefore likely that the inspecting licenced aircraft maintenance engineers would have been unable to have detected the gearmotor defect by visual inspection, had it existed at the time of the last scheduled inspection.
Findings
ATSB investigation report findings focus on safety factors (that is, events and conditions that increase risk). Safety factors include ‘contributing factors’ and ‘other factors that increased risk’ (that is, factors that did not meet the definition of a contributing factor for this occurrence but were still considered important to include in the report for the purpose of increasing awareness and enhancing safety). In addition, ‘other findings’ may be included to provide important information about topics other than safety factors.
These findings should not be read as apportioning blame or liability to any particular organisation or individual.
From the evidence available, the following findings are made with respect to the drive belt tensioning motor failure involving Robinson Helicopter R44, VH-ZUJ, at Hamilton Island Airport, Queensland on 8 January 2023.
Robinson Helicopter Company advised that they are actively working with the component manufacturer to rectify identified quality issues with the gearmotor assembly and are considering updating the procedures for the inspection of the clutch actuator assembly.
Under section 26 of the Transport Safety Investigation Act 2003, the ATSB may provide a draft report, on a confidential basis, to any person whom the ATSB considers appropriate. That section allows a person receiving a draft report to make submissions to the ATSB about the draft report.
A draft of this report was provided to the following directly involved parties:
United States National Transportation Safety Board
Whitsunday air services (Operator)
Helibiz
Robinson Helicopter Company
Globe Motors
the pilot of the incident flight.
Submissions were received from:
Robinson Helicopter Company
Globe Motors
The submissions were reviewed and, where considered appropriate, the text of the report was amended accordingly.
Purpose of safety investigations
The objective of a safety investigation is to enhance transport safety. This is done through:
identifying safety issues and facilitating safety action to address those issues
providing information about occurrences and their associated safety factors to facilitate learning within the transport industry.
It is not a function of the ATSB to apportion blame or provide a means for determining liability. At the same time, an investigation report must include factual material of sufficient weight to support the analysis and findings. At all times the ATSB endeavours to balance the use of material that could imply adverse comment with the need to properly explain what happened, and why, in a fair and unbiased manner. The ATSB does not investigate for the purpose of taking administrative, regulatory or criminal action.
Terminology
An explanation of terminology used in ATSB investigation reports is available here. This includes terms such as occurrence, contributing factor, other factor that increased risk, and safety issue.
Publishing information
Released in accordance with section 25 of the Transport Safety Investigation Act 2003
Ownership of intellectual property rights in this publication
Unless otherwise noted, copyright (and any other intellectual property rights, if any) in this report publication is owned by the Commonwealth of Australia.
Creative Commons licence
With the exception of the Coat of Arms, ATSB logo, and photos and graphics in which a third party holds copyright, this publication is licensed under a Creative Commons Attribution 3.0 Australia licence.
Creative Commons Attribution 3.0 Australia Licence is a standard form licence agreement that allows you to copy, distribute, transmit and adapt this publication provided that you attribute the work.
The ATSB’s preference is that you attribute this publication (and any material sourced from it) using the following wording: Source: Australian Transport Safety Bureau
Copyright in material obtained from other agencies, private individuals or organisations, belongs to those agencies, individuals or organisations. Where you wish to use their material, you will need to contact them directly.
[1] Worm-drive: Consisting of a worm gear driving a worm wheel oriented with their rotation axes at 90° to each other.
[2] Australian Journal of Mechanical Engineering, Vol 2, No.2. Mechanisms and prevention of vibration loosening in bolted joints. Fernando (2005)
[3] NRP-1228, NASA Reference Publication: Fastener design manual (1990).
[4] Robinson Model R44 pilot operating handbook: Section 3, Emergency procedures. Page 3-9. FAA Approved 21 October 2016.
Amendments to the Transport Safety Investigations Regulations (TSI Regulations), which detail the requirements for reporting transport accidents and incidents to the ATSB, took effect on 1 January 2023.
“The TSI Regulations set out the ATSB’s safety occurrence reporting scheme and prescribes what occurrences must be reported to the ATSB, the ‘responsible persons’ who are required to make a report, and the particulars to be included in a report,” said ATSB Chief Commissioner Angus Mitchell.
The changes predominantly relate to the aviation industry.
“For aviation there are two key changes in the amended regulations – the creation of four categories of aircraft operations, each with different reporting requirements, and new requirements for sport aviation bodies to report accidents and incidents to the ATSB,” Mr Mitchell explained.
The four categories comprise Category A (passenger transport), Category B (commercial non-passenger, including medium to large RPA), Category C (non-commercial) aircraft operation, and Category D (small non-excluded RPA and certain uncrewed balloons) aircraft operation.
“Higher categories, in particular passenger-carrying and commercial operations, will have a greater reporting focus due to the greater public safety benefit that could be derived,” said Mr Mitchell.
“Non-commercial aircraft operations and uncrewed RPA and balloons will have lower reporting requirements.”
The Regulations define occurrences that must be reported to the ATSB as “immediately reportable”, which must be reported by telephone as soon as reasonably practical, and “routine reportable” matters, which can be notified to the ATSB by a written report within 72 hours.
“Changes to the regulations ensure immediately reportable matters are those more likely to be considered for investigation by the ATSB, while reducing the reporting requirements on industry for those matters the ATSB is less likely to consider for investigation,” Mr Mitchell explained.
Other changes to the Regulations include aligning aircraft operation categories and definitions with CASA flight operations rules introduced in December 2021, and aligning definitions of aircraft accident, serious aircraft incident, aircraft incident, fatal injury and serious injury with International Civil Aviation Organization definitions
“Changes to the regulations also simplify reporting requirements for industry by removing prescriptive lists of individual kinds of occurrences and defining these concepts more broadly.”
Reporting is now based on more general concepts including accidents, serious incidents, incidents, loss of separation and declaration of emergency. Guidance on the ATSB website and to be provided in the Aeronautical Information Publication details comprehensive examples of type of occurrences that fit into each.
The ATSB consulted extensively with industry on the proposed changes over a five-week timeframe between January and March 2022. Feedback received during that process was largely positive, and helped shape the final Regulations package.
The amended Regulations and new reporting requirements subsequently took effect on 1 January 2023.
“Reporting to the ATSB is a simple and quick process,” Mr Mitchell said.
The ATSB has also updated the reporting forms on the ATSB website to make reporting even easier.
“Nonetheless we do recognise the aviation industry has been through a period of considerable change and disruption in recent years and do stress that our approach to implementing these amended regulations is focusing on education and encouraging better reporting practices over an extended period, with less emphasis placed on compliance particularly for industry participants who may not be fully across the new requirements.”
Aside from being the basis for starting safety investigations, all occurrences reported to the ATSB are maintained in Australia’s official aviation occurrence database and used for safety research and analysis.
“Ultimately all of aviation benefits from an open and trusted aviation occurrence reporting framework.”
On the morning of 5 January 2023, a British Aerospace BAE 146-200, registered VH-SFV and operated by Pionair Australia, operated a freight transport flight in darkness from Brisbane to Rockhampton, Queensland. After discontinuing a required navigation performance approach to runway 33 at Rockhampton because of low cloud, the crew conducted a missed approach and commenced a second approach at 0358 local time.
When commencing the second approach, the captain began descending the aircraft from 3,500 feet above mean sea level at the initial approach fix waypoint SARUS. Prior to crossing the intermediate fix at the waypoint BRKSI, the aircraft descended below the 3,000 ft segment minimum safe altitude (SMSA). The aircraft then continued descending on about a 3° profile and crossed BRKSI at 1,705 ft (1,295 ft below the SMSA) before then also descending below the next SMSA of 1,500 ft a few seconds later.
As the aircraft continued descending toward the minimum descent altitude, the flight crew recognised that the aircraft had descended below the SMSA and immediately commenced a missed approach. At about the same time, the ground proximity warning system activated.
What the ATSB found
The ATSB found that the captain commenced the second approach descent early based upon the incorrect application of their preferred regular descent technique but from a lower altitude. Additionally, the first officer did not identify the early descent due to an incorrect mental model of the aircraft's position in relation to the required flightpath. This led to the aircraft twice descending below segment minimum safe altitudes.
The ATSB also found that due to the time of the approaches and inadequate sleep, both flight crewmembers were likely experiencing a level of fatigue known to adversely affect performance. This, in combination with a period of high workload associated with the missed approach and second approach, led to the early descent and monitoring errors.
Finally, while the operator's flight crew rosters were compliant with applicable regulations and adequate sleep opportunities were available, the rosters were irregular and disruptive to the flight crew's sleep patterns which adversely impacted their ability to obtain adequate sleep prior to the incident flight.
What has been done as a result
Following the occurrence, the operator implemented several organisational, operational, and training changes including:
the establishment of a fatigue safety action group
a temporary reduction in total operational workload to reduce roster pressures and increase roster stability while training of additional flight crew was completed
revisions to standard operating procedures to clarify actions and reduce workload during approaches
revision of the training programs for flight management computer use during approaches.
Safety message
This incident illustrates the human factors implications associated with the combination of increased workload and the effects of fatigue.
The ATSB SafetyWatch highlights the broad safety concerns that come out of our investigation findings and from the occurrence data reported by industry. One of the priorities is improving the management of fatigue, which is the physical and psychological state typically caused by prolonged wakefulness and/or inadequate sleep.
Managing fatigue is a shared responsibility. This incident emphasises the importance of operators providing predictable and stable rosters to support pilots in achieving adequate sleep. Also highlighted, is the importance of pilots monitoring their own health and wellbeing to ensure that they are well-rested, especially when conducting overnight operations.
The investigation
Decisions regarding the scope of an investigation are based on many factors, including the level of safety benefit likely to be obtained from an investigation and the associated resources required. For this occurrence, a limited-scope investigation was conducted in order to produce a short investigation report, and allow for greater industry awareness of findings that affect safety and potential learning opportunities.
The occurrence
At 0238 local time on 5 January 2023, a British Aerospace BAE 146-200, registered VH-SFV and operated by Pionair Australia, departed Brisbane, Queensland (QLD) for a freight transport flight to Rockhampton, QLD with 2 crewmembers on board.[1] The captain was acting as pilot flying, and the first officer was acting as pilot monitoring.[2]
At 0300, as the aircraft climbed through flight level 220,[3] air traffic control cleared the flight to track to the waypoint SARUS. This waypoint was the initial approach fix for the required navigation performance (RNP) approach for runway 33 at Rockhampton and the tracking allowed the crew to proceed directly from the cruise and descent to a straight-in RNP approach (Figure 1).
Source: Operator and Google Earth, annotated by the ATSB
At 0330, the aircraft crossed SARUS to commence the RNP approach for runway 33. As was the captain’s normal practice (see the section titled Crew approach techniques), the aircraft crossed SARUS at 4,980 ft above mean sea level while descending. The aircraft continued descending along the approach until reaching the 710 ft minimum descent altitude (MDA) for the approach. Upon reaching the MDA, the crew could not see the runway lights due to cloud and commenced a missed approach.
The crew carried out the missed approach, climbed to 4,500 ft and returned to the waypoint SARUS to prepare for a second approach (Figure 2). At SARUS, the crew conducted a holding pattern and descended to the minimum holding altitude of 3,500 ft. While conducting the holding pattern, the crew obtained updated weather information from ATC, reactivated the pilot-activated runway lights, completed an approach briefing and readied the aircraft for the second approach.
Figure 2: Flight path of first missed approach, holding and second approach
Source: Operator and Google Earth, annotated by ATSB
At 0358, the aircraft crossed SARUS at 3,500 ft to begin the second approach and, the captain applied their usual descent technique and commenced descending. At the same time, the first officer made a radio broadcast on the Rockhampton common traffic advisory frequency (CTAF). As the first officer was busy with the broadcast, the captain took on the pilot monitoring task of calling out the aircraft’s altitude and distance to run to the next waypoint (BRKSI).
After completing the radio calls, the first officer took over the pilot monitoring tasks and started to call out the altitude and distance to run, continuing from the captain’s previous callout but incorrectly believing that the aircraft had already passed BRKSI.
At 0358:55, prior to crossing BRKSI, the aircraft descended below the 3,000 ft segment minimum safe altitude (SMSA) (Figure 3). The aircraft continued descending on about a 3° approach profile and crossed BRKSI at 1,705 ft (1,295 ft below the SMSA) before then descending below the next SMSA of 1,500 ft, 24 seconds later at 04:00:56.
As the aircraft continued descending toward the MDA, along a descent profile consistent with it being one approach segment further along than it actually was, the flight crew recognised that the ground lighting appeared different to the first approach and that distance measuring equipment indications were not as expected. In response, the first officer looked at the flight management computer and identified that the next waypoint was BRKSF, not the expected missed approach point, and immediately called for the captain to conduct a missed approach.
At about the same time, 0401:54, the ground proximity warning system generated a ‘terrain’ alert (see the section titled Ground proximity warning system). The crew then conducted a second missed approach. The minimum height recorded during the approach was 602 ft above ground level.
Following the missed approach, the crew diverted to Mackay, QLD and landed without further incident. The crew then completed a return trip to Rockhampton and Brisbane before completing their duty.
Context
Crew details
The captain held an air transport pilot licence (aeroplane) and class 1 aviation medical certificate. The captain had over 16,400 hours of flying experience, of which about 2,000 were on the BAE 146.
The first officer held an air transport pilot licence (aeroplane) and class 1 aviation medical certificate. The first officer had over 2,400 hours of flying experience, of which about 280 were on the BAE 146.
The first missed approach at Rockhampton was the first officer’s first missed approach in a BAE 146 aircraft (other than in a simulator).
The crewmembers regularly operated from Brisbane to Rockhampton. When conditions favoured a runway 33 approach at Rockhampton, both crewmembers preferred to conduct an RNP approach by tracking straight in from the inbound track via SARUS.
When operating as pilot flying, the captain preferred to conduct a constant descent from the cruise segment to cross SARUS at about 5,000 ft above mean sea level while continuing the descent into the approach.
The first officer usually descended and levelled at 3,500 ft prior to crossing SARUS as this allowed additional time to configure the aircraft for the approach before continuing the approach descent from the waypoint BRKSI.
Both descent methods were consistent with the operator’s procedures.
Flight crew fatigue and workload
Crewmember sleep details
On the morning of 4 January, the captain and first officer completed a 9-hour duty together at 0445. Following this, the captain had about 2 hours of sleep and the first officer about 3 hours. In the evening, the captain had a further period of about 3 hours of sleep, waking at 2100 and the first officer about 2.5 hours before waking at 2130. On the previous day (3 January), the captain had about 4 hours of sleep while the first officer had about 7 hours. Therefore, at the commencement of duty at 0140 on 5 January, the captain had achieved about 9 hours of sleep in the preceding 48 hours, while the first officer had achieved about 12.5 hours.
Prior to 3 January, the captain had 2 days free of duties and the first officer had 11 days free.
Causes and effects
Civil Aviation Safety Authority (CASA) advisory publication CAAP 48-01 v3.2 Fatigue management for flight crew membersprovides a substantial amount of information on flight crew fatigue, sleep, workload, and the effects of sleep loss on performance.
The publication stated that the average adult needs between 7 to 9 hours of quality sleep per day to sustain normal performance and that obtaining sufficient, quality sleep during the optimum window for rest was essential. In the absence of sufficient sleep, the brain does not operate effectively and both concentration and decision making are negatively impacted. In addition, the effects of restricting sleep accumulate with pilots becoming progressively less alert and functional with each further day of sleep restriction. This is described as accumulating a ‘sleep debt’.
Insufficient sleep can lead to a deterioration in an individual’s processing speed and ability to maintain attention. More complex mental tasks, such as anticipating events, planning, and reacting to novel situations are also negatively impacted. These capabilities are critical to aviation safety, particularly during critical and high workload phases such as an instrument approach. Furthermore, once people are sufficiently fatigued, they are no longer able to reliably assess their own levels of fatigue, and consequently relying solely on self-assessment of fatigue can be flawed.
Additionally, the time of day can also have an impact on sleep and performance. Humans exhibit various predictable physiological and behavioural rhythms within a period of about a day known as circadian rhythms. These rhythms include periods of reduced alertness corresponding with the body temperature decreasing to its lowest level from 0300 to 0600 and, to a lesser extent, from 1600 to 1800. These circadian rhythms are synchronised to the solar day by external factors, the most important of which is the external light-dark cycle. Therefore, night work is particularly challenging, as it requires an individual to override the circadian rhythm to maintain adequate alertness.
The CASA advisory publication also emphasised the following with regard to flight crew duty rosters:
Publishing of rosters
Studies have demonstrated that shift workers are able to partially adapt to working at sub-optimal times by adapting their daily routine to match required work patterns. This can be more difficult in aviation due to changes in rostered duty times on consecutive days as a result of schedule constraints.
Publishing duty rosters allows flight crew members to plan adequate rest before their next assigned duty. Operators should be aware that their flight crew members will require some degree of certainty in organising their work/life balance and organising their sleep routine. For scheduled operations, operators should publish a planned roster at least seven (7) days prior to commencement of the roster period.
While late changes to rosters are sometimes unavoidable, operators should make all reasonable efforts to ensure that these changes are kept to a minimum. Procedures need to be in place so that any fatigue risk resulting from the effects of late roster changes is identified and managed.
Operator guidance
Pionair’s operations manual included a Fatigue Management Policy which provided crewmembers with fatigue guidance and, in part, aimed to:
ensure that crewmembers were aware of the accrual, and identification of (and need to address) fatigue that can arise from work and personal factors
embrace a fair and just reporting culture to facilitate improvement of fatigue management understanding and procedures
facilitate fatigue management rostering and practices that avoid disruptive roster patterns and minimise the risks associated with fatigued crewmembers, with the goal of having no flight operations on which crewmembers are fatigue impaired to the extent that safety is impacted.
This policy also stated the following with regard to determining personal fatigue level:
Whilst it is easy to understand that adequate sleep is a prerequisite for an alert flight crewmember, the notion of adequate sleep is subject to individual variability. This is further complicated by the tendency to overestimate the amount, and quality, of sleep we actually get. As a general guide an individual who was previously well rested requires at least 6 hours sleep in 24 hours, and 13 hours in 48 hours to remain adequately alert.
The policy also required a crewmember to notify the operator should the crewmember believe that because of fatigue they were not fit for duty. Fatigue management is also emphasised in CAAP 48‑01 as a shared responsibility between the operator and crewmembers.
Roster stability
Both crew members reported that inconsistent and varying rosters reduced their ability to achieve sufficient and good quality sleep. Prior to departure, the captain and first officer discussed the difficulty in obtaining sleep the previous day. The captain recalled feeling moderately tired, although neither crewmember reported feeling unfit for duty or felt the need to make a fatigue report prior to commencing duty.
The ATSB undertook an analysis of the operator’s rostering practices. This analysis included examinations of the rosters of the operating crew and a further 4 flight crew (2 captains and 2 first officers) and found the following:
regarding maximum flight and duty hours, number of consecutive duties during window of circadian low, and minimum hours off-duty; all rosters assessed were compliant with Civil Aviation Order 48.1 as applicable at the time of the occurrence
there was no pattern to the rosters and there was variability in terms of duty start times which was also evident during consecutive days of duty
some duty start times were in forward rotation and some in backwards rotation[4]
crew were not completing more duties than originally rostered, nor completing duties during standby periods
almost all the recorded duty times varied from the published roster but in most cases did not affect maximum duty period or minimum off-duty periods.
Aircraft details
General
The BAE 146 is a 4-engine, high-wing, regional jet aircraft. VH-SFV was manufactured in 1987 and was configured for air freight operations (Figure 4).
The BAE-146 entered service in 1983 and was fitted with an analogue cockpit based upon technologies and ergonomic considerations of the time (Figure 5). When manufactured, VH‑SFV was not equipped with an integrated flight management computer (FMC) although one was later fitted to allow for operational practices introduced since the aircraft’s manufacture. The FMC fitted to VH-SFV included a lateral navigation function but did not include a vertical navigation function or vertical path protection. Management of the vertical profile of the approach using the autopilot was achieved using the vertical speed mode. In this mode, the PF used the control column to descend the aircraft and, once the desired descent rate was achieved, pressed a ‘sync’ button to enter the targeted vertical speed into the autopilot.
The control display units (CDU) of the FMC were positioned on the centre pedestal of the cockpit and allowed for the entry of navigation data. During an RNP approach, the FMC provided a waypoint distance to run indication on the horizontal situation indicator, but did not identify the waypoint name (Figure 6). Waypoint information, including the waypoint where the aircraft was tracking from and to, and the subsequent approach waypoint was displayed on the CDU screen (Figure 7).
The aircraft was equipped with an enhanced ground proximity warning system (EGPWS). This system used aircraft inputs, including geographic position, attitude, altitude, and speed combined with internal terrain, obstacles, and airport runway databases to predict potential conflicts between the aircraft flight path and terrain or an obstacle. When a terrain or obstacle conflict was detected, the system provided a visual and audio warning alert.
Meteorology
Both approaches at Rockhampton were conducted in dark night conditions.
At 0336, the time of the commencement of the first missed approach, the Bureau of Meteorology (BoM) automatic weather station at Rockhampton Airport recorded the wind as 3 kt from 273° magnetic. Cloud cover was recorded: few[5] at 526 ft above mean sea level (AMSL) and scattered at 5,746 ft. Visibility was recorded as 23 km.
About 22 minutes later, at 0358, as the crew commenced the second approach, the station recorded the wind as 5 kt from 225° magnetic. Cloud cover was recorded as: few at 922 ft and scattered at 1,936 ft AMSL. Light rain had been recorded at the station in the preceding minute and visibility was recorded as 6,700 m.
Aerodrome weather information service
Rockhampton Airport was equipped with an aerodrome weather information service (AWIS), providing observations of meteorological conditions observed at the airport. These observations were available via telephone or air traffic control briefing. The Rockhampton AWIS was not available on a discrete radio frequency.
Rockhampton RNP runway 33 approach
Minimum descent altitude and missed approach requirements
For a 2-dimensional approach, to allow for the transition from descent to a level segment or missed approach without descending below the minimum descent altitude (MDA), the operator’s procedures required the addition of 50 ft to the 660 ft MDA. This provided a 710 ft MDA for the RNP approach in Rockhampton.
When the aircraft reached the missed approach point, if visual reference with the runway was not established (as occurred during the first approach), a missed approach was required.
Approach procedure chart
Airservices Australia and Jeppesen (an approved data service provider) published charts for the RNP runway 33 procedure. The charts produced by both organisations were designed and published in accordance with International Civil Aviation Organisation (ICAO) guidance.[6] The crew of VH-SFV used an electronic approach chart provided by Jeppesen, which was presented in dark mode for the night approach.
The Airservices Australia chart vertical profile presentation included the full approach, including the waypoint SARUS. This chart also included the minimum altitude of 3,500 ft at SARUS, the distance to the missed approach point of 15.3 nm (Figure 8) and the segment minimum safe altitude (SMSA) of 3,000 ft between SARUS and BRKSI. The Jeppesen chart (Figure 9) vertical profile commenced at waypoint BRKSI and did not include the waypoint SARUS, nor the SMSA between SARUS and BRKSI.
Figure 8: Airservices Australia RNP runway 33 approach chart
To provide a standardised presentation of aeronautical data for Jeppesen charts worldwide, Jeppesen chart design specifications directed that the vertical profile commence at the intermediate fix (IF) when an approach has multiple transitions. Jeppesen noted that this was the most common worldwide depiction of profile information. As the Rockhampton RNP approach had multiple transitions leading to the BRKSI IF, the vertical profile commenced at that waypoint.
Recorded data
Analysis of flight data from VH-SFV’s flight data recorder showed the descent profiles of the 2 approaches (Figure 10). The profiles show a similar descent angle, but with the second approach displaced by about 5 nm (1 approach segment).
Figure 10: RNP approach procedure showing the descent profiles of the 2 approaches
Source: Airservices and ATSB
Safety analysis
Early descent and error identification
After completing the first approach and missed approach, the crew completed a holding pattern to prepare for a second approach. The holding pattern provided a straight track to the initial approach fix SARUS, similar to the normal sequence for the crew when conducting a Brisbane to Rockhampton flight. The captain’s normal practice for this straight-in approach was to have the aircraft descending to cross SARUS at about 5,000 ft above mean sea level and to continue descending towards the next waypoint, BRKSI, while remaining above the 3,000 ft segment minimum safe altitude (SMSA).
On this occasion, following the missed approach and holding pattern, the aircraft crossed SARUS, and the captain immediately commenced descending as per their normal practice, but from the minimum holding altitude of 3,500 ft rather than their accustomed crossing altitude of 5,000 ft during a straight-in approach. This resulted in the aircraft incorrectly descending along a profile consistent with being one approach segment further along than its actual position.
As the aircraft descended along a normal descent angle, but one segment early, it twice descended below SMSAs. In dark night and cloudy conditions, this removed terrain and obstacle separation protections.
As the aircraft approached the minimum descent altitude, the different external sight picture and distance measuring equipment indications led the first officer to check the control display unit indications and identify that the aircraft was one approach segment behind their mental model of the approach and immediately call for a missed approach. At about the same time, the aircraft penetrated the ground proximity warning system warning envelope and a ‘terrain’ alert sounded.
The first officer’s normal practice when acting as pilot flying was to commence the approach from 3,500 ft at the waypoint after SARUS ‑ BRKSI. At the time of the descent of the second approach, the first officer’s focus was on completing radio broadcasts. While the first officer completed these broadcasts, the captain took over the callout and monitoring of descent distance and altitudes, temporarily removing the first officer from the approach monitoring task. When the first officer took over the task, they commenced monitoring the approach in the belief that the aircraft had already passed their preferred approach descent commencement point, BRKSI. Additionally, the next waypoint information was not immediately visible on the horizontal situation indicator and further contributed to the early descent error not being immediately recognised.
In addition, the Jeppesen approach chart used by both crews, while designed and published in accordance with ICAO guidance, did not include the waypoint SARUS or the SMSA for the SARUS-BRKSI segment on the vertical profile depiction. Although not considered contributory, this potentially limited the usefulness of the chart as an aid in enabling the crew to identify the early descent error.
The approaches took place during the crew’s window of circadian low, a time of increased fatigue risk. Additionally, the crew were likely subject to an accumulated sleep debt resulting from the inability to get adequate sleep on the day prior to the incident as well as on the previous day. Both crew had also achieved less sleep than was considered adequate in Pionair’s fatigue management policy, particularly the captain. This sleep debt resulted in both flight crewmembers likely experiencing a level of fatigue known to adversely affect performance at the time of the approaches.
In addition, the second approach commenced during a period of high workload. The crew had completed one approach and a missed approach, the first in a BAE 146 aircraft (other than in a simulator) for the first officer. The crew then positioned the aircraft in the holding pattern and prepared for the second approach in dark and turbulent conditions. During the holding pattern, with Rockhampton Airport meteorological information not available via radio, the first officer obtained this information through air traffic control while also making the standard broadcasts to both air traffic control and on the common traffic advisory frequency. The aircraft’s analogue instrumentation and rudimentary autopilot systems also required significant input from the crew, further increasing the workload. The high workload, combined with the likely effects of fatigue, contributed to the early descent error made by the captain (as pilot flying) and to the first officer not immediately identifying the error (as pilot monitoring).
Stable rostering
The crews were operating night duties, which required sleeping during normal wakeful periods. This required the crew to adapt their sleeping patterns to match the available sleep opportunities. On the day prior to the occurrence duty, despite an adequate opportunity being available, both crewmembers were unable to obtain adequate sleep. The ATSB’s analysis of the operator’s rosters found that the rosters were irregular, unpredictable and that the duty hours operated were often inconsistent and varied from those rostered. This was disruptive to the crew’s sleep patterns and reduced their ability to effectively adapt to the available sleep opportunities, which in turn adversely impacted their ability to obtain adequate sleep prior to the incident flight.
Managing fatigue is a shared responsibility of the operator and crew. Part of this responsibility is the requirement of crew to self-report if they believe that they are unfit for duty due to fatigue. However, a known effect of fatigue is a reduction in an individual’s ability to accurately self-assess their fatigue level. This can reduce the effectiveness of crew self-reporting as a means of preventing crew from operating when fatigued, further reinforcing the need for stable and predictable rosters.
While the rostering practices increased the risk of the crew being unable to obtain adequate sleep, they were not considered contributory to the incident. Both the rosters and duties operated by the crews were found to be compliant with regulatory requirements. Furthermore, the time of the incident was generally associated with a reduction in human alertness and high fatigue risk, while also coinciding with a period of high workload following a missed approach and preparation for a second approach. Finally, the existence of other protections such as the ground proximity warning system alert were assessed as being effective in alerting the crew to the situation in sufficient time to take action.
Findings
ATSB investigation report findings focus on safety factors (that is, events and conditions that increase risk). Safety factors include ‘contributing factors’ and ‘other factors that increased risk’ (that is, factors that did not meet the definition of a contributing factor for this occurrence but were still considered important to include in the report for the purpose of increasing awareness and enhancing safety). In addition ‘other findings’ may be included to provide important information about topics other than safety factors.
These findings should not be read as apportioning blame or liability to any particular organisation or individual.
From the evidence available, the following findings are made with respect to the descent below minimum altitude involving British Aerospace BAE 146, VH-SFV, 15 km south of Rockhampton Airport on 5 January 2023.
Contributing factors
Following a missed approach, a second approach descent was commenced early when the captain applied their regular descent technique, but from a lower altitude, while the first officer did not identify the early descent due to an incorrect mental model of the aircraft's position along the approach. This resulted in the aircraft twice descending below segment minimum safe altitudes.
Due to the time of the approaches and inadequate sleep, both flight crewmembers were likely experiencing a level of fatigue known to adversely affect performance. This, in combination with a period of high workload associated with the second approach, led to the early descent and monitoring errors.
Other factors that increased risk
While the operator's flight crew rosters were compliant with applicable regulations and adequate sleep opportunities were available, the rosters were irregular and disruptive to the flight crew's sleep patterns. This adversely impacted their ability to obtain adequate sleep prior to the incident flight.
Other finding
As the aircraft descended toward the approach minimum descent altitude one approach segment early (prior to the final approach fix), the flight crew identified the error and commenced a missed approach. At about the same time, the ground proximity alert activated.
Safety actions
Whether or not the ATSB identifies safety issues in the course of an investigation, relevant organisations may proactively initiate safety action in order to reduce their safety risk. The ATSB has been advised of the following proactive safety action in response to this occurrence.
Safety action not associated with an identified safety issue
Proactive safety action by Pionair Australia
Action number:
AO-2023-004-PSA-01
Action organisation:
Pionair Australia
Following the occurrence, the operator implemented the following organisational, operational, and training changes:
a fatigue safety action group was established
From 8 May to 17 July 2023, the operator temporarily reduced total operational workload to reduce roster pressures, increase roster stability and complete training of additional flight crew
to reduce workload during required navigation performance (RNP) approaches, standard operating procedures were revised to require crew to configure the aircraft for landing, including completion of the landing checklist, prior to crossing the initial approach fix
the BAE146 standard operating procedures manual section 'Decision at the Minima' was amended to include instructions for crew to state the following (as applicable): ‘When approaching the initial approach fix, cleared for the approach, and compliance with any altitude restriction is assured, set the altitude selector to the minimum descent altitude or decision altitude.’
the operations manual instructions limiting multiple approaches to 2 was revised to include all operations (passenger and freight) and the guidance wording changed from ‘should’ to ‘shall’
the operations manual was revised to clarify the guidance for temporary removal of flight crew from duty following an incident
the simulator training program was revised to include use of the flight management computer during RNP approaches
the flight training department revised the BAE 146 RNP approach ground theory training guidance for flying RNP approaches using the Universal UNS-1 Lw flight management system (as fitted to VH-SFV)
guidance was distributed to all flight crew highlighting the absent initial approach fixes and total distance to the missed approach point information of Jeppesen RNP charts
The operator also advised that details of the incident will be disseminated to all flight crew and incorporated into training courses.
Sources and submissions
Sources of information
The sources of information during the investigation included:
Under section 26 of the Transport Safety Investigation Act 2003, the ATSB may provide a draft report, on a confidential basis, to any person whom the ATSB considers appropriate. That section allows a person receiving a draft report to make submissions to the ATSB about the draft report.
A draft of this report was provided to the following directly involved parties:
Pionair Australia
the flight crew
Civil Aviation Safety Authority.
Submissions were received from:
Pionair Australia
Civil Aviation Safety Authority.
The submissions were reviewed and, where considered appropriate, the text of the report was amended accordingly.
Purpose of safety investigations
The objective of a safety investigation is to enhance transport safety. This is done through:
identifying safety issues and facilitating safety action to address those issues
providing information about occurrences and their associated safety factors to facilitate learning within the transport industry.
It is not a function of the ATSB to apportion blame or provide a means for determining liability. At the same time, an investigation report must include factual material of sufficient weight to support the analysis and findings. At all times the ATSB endeavours to balance the use of material that could imply adverse comment with the need to properly explain what happened, and why, in a fair and unbiased manner. The ATSB does not investigate for the purpose of taking administrative, regulatory or criminal action.
Terminology
An explanation of terminology used in ATSB investigation reports is available here. This includes terms such as occurrence, contributing factor, other factor that increased risk, and safety issue.
Publishing information
Released in accordance with section 25 of the Transport Safety Investigation Act 2003
Ownership of intellectual property rights in this publication
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[1] The flight was operated under Civil Aviation Safety Regulations Part 121 (Air transport operations - larger aeroplanes).
[2] Pilot Flying (PF) and Pilot Monitoring (PM): procedurally assigned roles with specifically assigned duties at specific stages of a flight. The PF does most of the flying, except in defined circumstances; such as planning for descent, approach and landing. The PM carries out support duties and monitors the PF’s actions and the aircraft’s flight path.
[3] Flight level: at altitudes above 10,000 ft in Australia, an aircraft’s height above mean sea level is referred to as a flight level (FL). FL 220 equates to 22,000 ft.
[4] A forward rotating roster is one in which shifts commence later on successive days. A backwards rotating roster is one in which shifts commence earlier.
[5] Cloud cover: in aviation, cloud cover is reported using words that denote the extent of the cover – ‘few’ indicates that up to a quarter of the sky is covered, ‘scattered’ indicates that cloud is covering between a quarter and a half of the sky.
[6] International Civil Aviation Organization 2016, Aeronautical Chart Manual third edition, document 8697.
Occurrence summary
Investigation number
AO-2023-004
Occurrence date
05/01/2023
Location
15km south of Rockhampton Airport
State
Queensland
Report release date
13/12/2023
Report status
Final
Investigation level
Short
Investigation type
Occurrence Investigation
Investigation status
Completed
Mode of transport
Aviation
Aviation occurrence category
E/GPWS warning
Occurrence class
Serious Incident
Highest injury level
None
Aircraft details
Manufacturer
British Aerospace
Model
BAE 146 SERIES 200-11
Registration
VH-SFV
Serial number
E2086
Aircraft operator
Pionair Australia Pty Ltd
Sector
Jet
Operation type
Part 121 Air transport operations - larger aeroplanes