Cessna 152, VH-RNN, Berowra, New South Wales

Summary

The pilot had been authorised to carry out a night-VFR flight in the Maitland training area on 19 March. That evening VH-RNN was observed to depart Maitland and later in the evening the pilot was seen in his car in the airport carpark. The following morning witnesses observed an unidentified aircraft flying in a northerly direction below low cloud on the eastern side of the F3 freeway, approximately 105 km south of Maitland. The aircraft was subsequently observed to bank steeply to the left and appeared to descend before disappearing from view. The wreckage of VH-RNN was subsequently found on 30 March, near the F3 freeway, about 800 m south of the earlier sighting of the unidentified aircraft.

Toxicological analysis of the pilot revealed the presence of the drug Dextropropoxyphene at levels which may have caused him to experience sleepiness, hallucinations, delusions and confusion during the flight.

The pilot's intentions could not be established. The aircraft was observed manoeuvring in conditions of low cloud and reduced visibility and it is likely that the pilot was attempting to turn back to an area of more favourable conditions. The pilot's ability to remain safely clear of terrain may have been adversely affected by the effects of the drug Dextropropoxyphene.

Significant Factors

  1. The aircraft was operating at a low height in conditions of low cloud and reduced visibility.
  2. The pilot's ability to safely control the aircraft may have been adversely affected by an analgesic drug.

Occurrence summary

Investigation number 199400782
Occurrence date 20/03/1994
Location Berowra
State New South Wales
Report release date 24/01/1996
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category VFR into IMC
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Cessna Aircraft Company
Model 152
Registration VH-RNN
Serial number 15285083
Sector Piston
Operation type Flying Training
Departure point Maitland, NSW
Destination Unknown

Fairchild Metro SA226-AT, VH-SWP, 15 km north-east Tamworth Aerodrome, New South Wales

Summary

SYNOPSIS

The aircraft was engaged on a freight courier service and had departed Bankstown at 0630 EST on 9 March 1994 and proceeded to Tamworth, Armidale, Glen Innes and Inverell. The pilot rested at Inverell for approximately seven hours before departing at about 1640 on the return flight to Bankstown via Glen Innes, Armidale and Tamworth. The flight was planned to be conducted in accordance with the Instrument Flight Rules (IFR) and departed Armidale for Tamworth at 1723. At about 1734 the aircraft impacted a mountain 8.2 NM north-east of Tamworth at 2,685 ft above mean sea level (AMSL), after being cleared to make a visual approach by Tamworth Tower. A short time after the accident, the pilot of a search aircraft observed that the top of the mountain was obscured by cloud.

1. FACTUAL INFORMATION

1.1   History of the flight

VH-SWP was operating on a standard company flight plan for the route Bankstown-Tamworth-Armidale-Glen Innes-Inverell and return, and the flight plan indicated the flight would be conducted in accordance with IFR procedures. The classification of the flight was shown as non-scheduled commercial air transport although the aircraft was operating to a company schedule, and departure and flight times for each route segment were indicated on the flight plan.

The aircraft departed Bankstown at about 0640 and proceeded as planned to Inverell where the pilot rested until his departure that afternoon for the return journey. The schedule required an Armidale departure at 1721. At 1723 the pilot reported to Sydney Flight Service that he was departing Armidale for Tamworth. The planned time for the flight was 17 minutes.

Although the flight-planned altitude for this sector was 6,000 ft, the pilot was unable to climb immediately because a slower aircraft, which had departed Armidale for Tamworth two minutes earlier, was climbing to that altitude. In addition, there was opposite direction traffic at 7,000 ft. The next most suitable altitude was 8,000 ft, but separation from the other two aircraft, which were also IFR, had to be established by the pilot before further climb was possible. The published IFR lowest safe altitude for the route was 5,400 ft.

The pilot subsequently elected to remain at 4,500 ft in visual meteorological conditions (VMC) and at 1727 requested an airways clearance from Tamworth Tower.  A clearance was issued by ATC to the pilot to track direct to Tamworth at 4,500 ft visually. At about 1732 the pilot requested a descent clearance. He was cleared to make a visual approach with a clearance limit of 5 NM by distance measuring equipment (DME) from Tamworth and was requested to report at 8 DME from Tamworth. The pilot acknowledged the instructions and reported leaving 4,500 ft on descent. Transmissions from ATC to the pilot less than two minutes later were not answered. The aircraft was not being monitored on radar by ATC, nor was this a requirement.

At about 1740, reports were received by the police and ATC of an explosion and possible aircraft accident near the mountain range 8 NM north-east of Tamworth Airport. The aircraft wreckage was discovered at about 2115 by searchers on the mountain range.

Soon after the aircraft was reported missing, a search aircraft pilot, who had extensive local flying experience, reported to ATC that the top of the range (where the accident occurred) was obscured by cloud, and that there was very low cloud in the valley nearby.

1.2    Damage and impact information

The aircraft was on the Armidale to Tamworth track 8.2 NM from Tamworth when it impacted trees at approximately 2,685 ft AMSL. It was descending at an angle of approximately 3.5 degrees and was banked about 17.5 degrees to the left at impact. The aircraft maintained a straight path after initial impact but had rolled to a bank angle of 25 degrees left by the time the left wing struck a second tree 35 m further on. It then impacted the ground left wing low and inverted, before bouncing into a rock face 200 m from initial impact. The main fuselage wreckage caught fire, and the cabin area was destroyed.

1.3    The pilot

The pilot was 24 years old and was correctly qualified and endorsed to perform the flight. He had flown on the two days prior to the accident following three days off duty. He had not flown this route before. He completed a flight check on 28 October 1994 and his performance was assessed as satisfactory. The flight check report stated that the requirement to be aware of terrain at all times was reviewed with the pilot.

The pilot was not known to be suffering from any ailment and appeared to be in good spirits on the day of the accident.

1.4    The aircraft

1.4.1    Aircraft history

The Swearingen SA226-AT aircraft was manufactured in 1975. The Australian certificate of airworthiness was issued on 15 May 1986. The last periodic inspection was completed on 11 January 1994.

1.4.2    Weight and balance

The aircraft weight and balance (centre of gravity) were within limits for the flight.

1.4.3   Aircraft serviceability

There were no known unserviceabilities other than the windscreen wipers. When the aircraft arrived at Tamworth in the morning it was raining, and the aircraft was cleared to land on runway 30 right. During the approach the pilot made a comment to the aerodrome controller (ADC) to the effect that it was difficult to see out of the aircraft without the windscreen wipers working. Why the windscreen wipers were not working, or when they became unserviceable, could not be determined. Effective use of the windscreen wipers would not have been possible at the speed at which the aircraft was flying immediately prior to the accident.

1.5    Wreckage examination

1.5.1    Structure

All aircraft extremities and control surfaces were accounted for at the accident site. The damage sustained was consistent with the application of excessive loads during the accident sequence and subsequent fire. There was no evidence found of in-flight fire. As far as could be determined there was no pre-impact abnormality with the structure and all damage was a result of impact forces.

1.5.2    Flight controls

All control systems were examined although only portions of control surfaces were recovered. Where found, the hinges, push-pull rods and cables were correctly assembled and secured. Witness marks indicated that at the time of wing impact with the trees, the aileron was in a neutral position, aileron trim was neutral, and flaps were in the up position.

1.5.3    Landing gear

All major components of the landing gear system had been torn from the aircraft, and it was not possible to determine if the individual legs were up or down. However, the hydraulic actuators which remained attached to the right wing were in a position consistent with the right gear being in the retracted position 

1.5.4    Other systems

Due to the extent of destruction of the aircraft, the functional status of its systems, including the fuel, electrical, and pitot-static systems, could not be determined. 

1.5.5    Crashworthiness

The amount and nature of aircraft destruction indicated that the aircraft approached the accident site at high speed. The cockpit area was destroyed. Examination of the pilot's seat and harness indicated that although the shoulder harness had not been fastened at the time of impact, the impact dynamics were such that the accident was non-survivable.

1.6   Meteorological information

A low-pressure system was situated near Albury NSW with a central pressure of 1,010 hectopascals (hPa). A weak trough extended from the low into Queensland. A high-pressure system with a central pressure of 1,028 hPa was centred in the Tasman Sea. The resulting airstream was a very moist northerly to north-easterly flow with extensive low cloud over the north-eastern regions of New South Wales.

The information being broadcast on the Tamworth Automatic Terminal Information Service (ATIS) at the time of the accident indicated that the weather at Tamworth airport included a light and variable wind, two octas of cloud at 1,000 ft, with visibility reducing to 3,000 m in rain.

The pilot of a search aircraft which was in the area about 20 minutes after contact was lost with VH-SWP said that the general cloud base was about 2,200 ft with lower patches. He said he had climbed above the cloud and found the tops at 2,800 ft, with some higher patches to about 3,100 ft. The higher patches were obscuring the terrain. There was a higher layer of cloud with a base at about 3,800 ft. He could not see towards Armidale as it seemed as though the two layers converged. From the accident area he could see Tamworth easily and visibility in that direction was good. When the same pilot later ascertained where the accident occurred, he confirmed that the area of the accident site had been covered by wispy cloud when he flew over it shortly after the accident.

1.7   Additional information

1.7.1   Recorded radar data

The aircraft was under radar coverage from Armidale to a point approximately 2.5 NM from the accident location. The recorded radar data showed that the aircraft departed Armidale (runway 05) and turned left to intercept the Armidale-Tamworth track. The aircraft climbed initially to 5,000 ft but then descended to 4,500 ft and maintained this altitude until about 1731 when it climbed to 4,900 ft. (Its position at that time coincided with Mt Gulligal which is 4,070 ft AMSL.) The radar data showed the aircraft leaving 4,500 ft at 1732:40, which was the time the pilot received descent clearance. The last recorded altitude was 3,900 ft when radar contact was lost at about 10 NM from Tamworth. The computed aircraft ground speed at that position was 260 kts.

1.7.2   Air-ground communications

Automatic voice recordings of air-ground and air-air communications indicated that satisfactory two-way communications existed in the period leading up to the accident.

2. ANALYSIS

Other traffic on the Armidale-Tamworth route delayed the pilot of VH-SWP from climbing to his planned altitude of 6,000 ft. As a result, he apparently elected to remain at 4,500 ft and conduct the flight in VMC. When the pilot called Tamworth Tower, he reported being visual at 4,500 ft, and was given a clearance to track direct to Tamworth in visual conditions at 4,500 ft before being cleared for a visual approach. The accident site was observed to be covered by cloud shortly after the accident. It is possible, therefore, that the pilot inadvertently entered cloud and failed to remain in visual contact with the ground.

3. CONCLUSIONS

3.1    Findings

  1. The pilot was correctly endorsed and qualified to undertake the flight, and the flight was operating in accordance with the scheduled departure time from Armidale.
  2. The flight was planned to be conducted under the instrument flight rules but because of other traffic it was not expedient to climb to an appropriate altitude.
  3. The flight was conducted at 4,500 ft, apparently under the visual flight rules.
  4. The pilot reported that he could remain visual and was cleared by ATC to make a visual approach.
  5. The aircraft was not being monitored on radar by ATC, nor was this a requirement.
  6. The last recorded radar data showed the aircraft descending through 3,900 ft, 2.5 NM from the accident site.
  7. There was low cloud and rain in the area at the time of the accident.
  8. The pilot allowed the aircraft to descend into terrain for reasons which could not be determined.
  9. No evidence was found of any physiological impairment of the pilot or of aircraft defects which may have contributed to the accident.

3.2   Significant factors

  1. The pilot was making a visual approach in weather conditions unsuitable for such an approach.
  2. The pilot had not flown this route before.
  3. The aircraft was flown below the lowest safe altitude in conditions of poor visibility.

Occurrence summary

Investigation number 199400612
Occurrence date 09/03/1994
Location 15 km north-east Tamworth Aerodrome
State New South Wales
Report release date 12/10/1995
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category VFR into IMC
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Fairchild Industries Inc
Model SA226
Registration VH-SWP
Serial number AT-033
Sector Turboprop
Operation type Charter
Departure point Armidale NSW
Destination Tamworth NSW

Cessna 182Q, VH-WIS, 28 km north-west of Cowarie Station, South Australia

Summary

The pilot, accompanied by a young employee, departed Cowarie Station airstrip at about 0730 CSuT to carry out an aerial inspection of the property.

The pilot's wife was in the habit of maintaining contact with the aircraft at regular intervals using a CB radio.  When the pilot failed to respond to a scheduled call at 1000 CSuT she became worried and contacted relatives and friends for advice.  She continued making calls at 15 minute intervals, but without response. The police were notified and an aerial search initiated.  The aircraft wreckage was found at 1820.  The pilot had received fatal injuries, and the employee seriously injured.  The time of the accident cannot be determined, but probably prior to 1000 CSuT.

The aircraft, while flying on a heading of about 100 degrees, had struck a tree approximately 30 feet above ground level with the right wing, which separated causing the aircraft to roll inverted and impacted the ground in a nose low attitude about 100 metres from the tree.

An inspection of the aircraft by the police officer at the accident site revealed that all seats except that of the pilot were missing.  They were later found in the property hangar.  He also found a green garbage bag in the aircraft containing numerous small pieces of meat resembling dog baits, with other similar size pieces of meat lying nearby.

A certain amount of confusion existed as to whether the aircraft had been involved in a dog baiting operation. When interviewed the employee was extremely vague and stated that he was unable to remember anything from breakfast time that morning until after the accident.  He could not remember the reason for the flight, at what height the aircraft had been flying prior to the accident, or if he had been correctly seated. Later when interviewed by the police he stated that there had been no dog baiting gear in the aircraft, and that in the 11 months working at the property he had never seen dog baiting carried out.

When the pilot's wife advised the police of her concern at not being able to contact the aircraft, she told the constable that her husband and the employee had gone flying to check water conditions and conduct some dog baiting.  Later in a statement given to the police she said that the dog baits were kept in the hangar.

The aircraft wreckage was retrieved for further inspection.  Indications were that the aircraft had impacted the tree, then the ground at a relatively fast forward speed.  The cabin roof was crushed and the tail unit to cabin area failed between the luggage door opening and the right (passenger) door.  The luggage door, still attached to the cabin area, was undamaged indicating that it was probably open at the time of impact. If closed it would have offered a certain amount of structural integrity to that area of the fuselage and also sustain some degree of damage.

The aircraft appeared to be in good condition and regularly maintained.  A bulk strip and inspection of the engine showed that it was capable of normal operations, and the propeller damage indicated that the engine was under power at the time of impact.

The amount of fuel on board is unknown, but if the aircraft had suffered fuel exhaustion, or any other similar problem, the terrain was such that a survivable forced landing could have been made.

The Bureau of Meteorology advised that the general weather in the Maree to Birdsville area early that morning was fine with one octa of cloud at 5000 feet and light winds, but storms and heavy rain became evident during the day.

The emergency locator beacon (ELB) installed in the aircraft failed to activate at impact.  A new battery had been fitted recently, and the unit tested in the normal manner by turning on and listening for a signal.   Dismantling of the ELB revealed the impact switch to be faulty and was probably in this condition prior to the accident.

A postmortem carried out on the pilot revealed a 9% carbon monoxide level.  The pathologist believed this to be significant, and although not enough to cause the pilot to pass out, would have caused him some confusion.

Removal of the co-pilot and rear bench seat from the aircraft would have allowed the necessary space to carry a bag of dog baits and given the employee easy access to the luggage compartment door while seated on the floor.  It is therefore feasible that the luggage door was open as the means for the employee to drop these baits.  The location of the open door would have allowed exhaust gases to swirl back into the cabin, with the associated carbon monoxide effecting both pilot and passenger.

Inspection of the cabin heat and exhaust systems indicated that they had been serviceable prior to the accident and would not have contributed to carbon monoxide ingress to the cabin.  All door and window seals were intact and there was no evidence of any exhaust gas leakage past them.

Although it cannot be shown that the pilot was actually low flying and dog baiting, the evidence suggests that this type of operation had been carried out. The pilot did not have any formal low flying training, qualifications or approvals. There were no approved Flight Manual supplements, or other instructions issued allowing this aircraft to operate with doors opened or removed.

Safety Action

As a result of this occurrence, the following Safety Advisory Notice has been issued.

Safety Advisory Notice

The Bureau of Air Safety Investigation suggests that the Civil Aviation Authority:

  1. Publish an article on the dangers of carbon monoxide ingestion from medical and operational perspectives, highlighting the dangers of flying with doors removed or open, particularly if such an operation is not approved in the aircraft flight manual; and
  2. publish an article stressing the need for appropriate training and approvals to be obtained before undertaking low-flying operations.

    In light of this occurrence, it is suggested that the article could incorporate both topics.

Occurrence summary

Investigation number 199400478
Occurrence date 22/02/1994
Location 28 km north-west of Cowarie Station
State South Australia
Report release date 21/04/1995
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Flight crew incapacitation
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Cessna Aircraft Company
Model 182
Registration VH-WIS
Serial number 18267124
Sector Piston
Operation type Aerial Work
Departure point Cowarie Station
Destination Cowarie Station
Damage Destroyed

Grob Astir CS 77, VH-IKJ, 2.5 km south-south-west of Waikerie, South Australia

Summary

Factual information

The glider was launched by aerotow for a local flight and at about 2,000 ft it was observed by the tug pilot to release and to fly straight and level.

Sometime later, the pilot a of glider flying in the Waikerie circuit area reported that there was a damaged glider in a field about 3 km south of the airfield. The tug pilot immediately commenced an aerial search and on locating the severely damaged glider, alerted emergency services. The pilot had not survived the impact.

On-site examination of the wreckage indicated that the glider had impacted the flat, grass covered terrain at high speed in a vertical, or near vertical dive. There was no evidence that the aircraft had been rotating immediately at impact and all aircraft components were located at the site except for the radio battery. Impact forces had destroyed the cockpit area, partially detached both wings, and broken the fuselage near the wing trailing edge.

The wreckage was recovered to a hangar at the airfield and inspected by engineers. Despite the extreme disruption of the airframe, all primary control system components were identified and examined. Many components had fractured during impact, however, it was determined that the control systems were all correctly connected prior to impact. The damage to componentry precluded a conclusive examination for jamming or obstruction of the control systems. The radio battery location was in an area of the aircraft well away from the control systems. The battery to electrical system connector wiring was found torn apart, consistent with separation of the battery from the aircraft at impact.

The glider had a valid maintenance release, and no maintenance deficiencies were identified. No evidence was found to suggest that a pre-existing failure of an aircraft component contributed to the accident.

The pilot was one of a group of foreign glider pilots visiting Waikerie for a period of intensive flying. He was correctly licensed and endorsed on the type. Prior to being approved to conduct solo flights at Waikerie, he was given flight instruction which included stall and spin recovery techniques.

A witness reported that on the day before the accident, a similar glider flown by the same pilot had pitched steeply nose-down and lost height immediately after release from the aero-tow.  The pilot was severely shaken, and he was subsequently debriefed by instructional staff before undertaking further flying.

The tow had appeared normal to the tug pilot who also briefly observed the glider in straight and level flight following the release. The descent was apparently not observed; however, in the light of the witness report of the previous day's incident, the possibility that the pilot lost control of the glider cannot be discounted.

The reason for the dive and the inability of the pilot to regain control of the glider could not be determined.

Occurrence summary

Investigation number 199400622
Occurrence date 12/03/1994
Location 2.5 km south-south-west of Waikerie
State South Australia
Report release date 24/01/1996
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Loss of control
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Grob - Burkhart Flugzeugbau
Model G102
Registration VH-IKJ
Serial number 1675
Sector Other
Operation type Gliding
Departure point Waikerie, SA
Destination Waikerie,SA
Damage Destroyed

Collision with terrain involving Rutan LONG-EZ, VH-MJL, Oakey, Queensland

Summary

The pilot was having a dam constructed on his property which is adjacent to the Oakey airfield. Witnesses working on the dam site reported that the pilot had indicated that he would conduct a low fly-past over the dam after taking off from Oakey.

The aircraft was observed to fly at low level across the dam and commence a climb before striking powerlines located on the property. After the mainwheels contacted the wires, the aircraft impacted the ground inverted. The pilot received fatal injuries.

Occurrence summary

Investigation number 199400362
Occurrence date 12/02/1994
Location Oakey
State Queensland
Report release date 28/06/1994
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Collision with terrain, Wirestrike
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Rutan Aircraft Factory
Model LONG-EZ
Registration VH-MJL
Sector Piston
Operation type Private
Departure point Oakey QLD
Destination Oakey QLD
Damage Destroyed

Loss of control involving Beech Aircraft Corp A36, VH-AKX, Lithgow, New South Wales

Summary

After an uneventful flight from Merimbula, the pilot overflew the airstrip to check the windsock. He noted that the windsock was swinging erratically around a mean direction of about 30 degrees left of the strip direction (approximately 140 degrees magnetic). The pilot then positioned the aircraft on the downwind leg to land towards the south-east.

Neither the pilot nor the surviving passengers reported any significant turbulence during the circuit. The pilot indicated that he was aiming to touch down about 100m in from the end of the strip. At what he thought was about 100 feet above the level of the strip, at an indicated airspeed of 85-90 kt, and with full flap selected, the aircraft rapidly lost altitude and landed very heavily a short distance in from the end of the strip. It then bounced, becoming airborne again.

The pilot reported that he was startled by the heavy landing. When the aircraft became airborne again, he momentarily applied power to go around but saw that the aircraft was headed towards trees, so he closed the throttle. His memory from this point was not complete but he did recall applying full right rudder, with no apparent effect, as the aircraft headed towards the trees. He also recalled the stall warning operating twice - once during the sink which led to the heavy landing, and again when the aircraft bounced.

Examination of the scene of the accident revealed that after the aircraft bounced, it contacted the ground again, left wing tip first, about 150m beyond the initial impact point and heading towards the left side of the strip. By this stage, the aircraft had developed a marked right skid. It continued in this manner across a dirt mound at the left edge of the strip and struck trees. The principal impact occurred when the aircraft fuselage just forward of the right-wing root struck a large tree, causing severe deformation to the right-side cockpit area.

The aircraft was equipped with an autopilot and a yaw damper. The pilot had conducted the cruise section of the flight with both these aids engaged. On arriving overhead, the strip he had disengaged the autopilot via the control wheel disengage switch. In normal operations, this switch also disengages the yaw damper. On this occasion, the pilot had checked that the autopilot had disengaged but did not confirm the yaw damper had disengaged. The pilot expressed the view that the difficulty he experienced in attempting to regain directional control when the aircraft was heading towards the left side of the strip could have been due to a problem with the yaw damper. However, a check of the yaw damper system after the accident did not reveal any faults.

The surface wind at the time of the accident was estimated by the Bureau of Meteorology to have been 110/15 knots.

The sequence of events described by the pilot indicates that the aircraft probably encountered windshear or a downdraft on late final approach. Given the prevailing wind conditions and the local topography, either of these phenomena could have been present. The pilot's recollection that he heard the stall warning sound during the bounce, plus the fact that the aircraft then contacted the ground left wing tip first indicate that the aircraft probably stalled during the bounce (possibly as a result of the pilot closing the throttle), causing the left wing to drop. The effect of the left wing tip dragging on the strip surface would have been to yaw the aircraft further (i.e. exacerbate the right skid). The decreasing speed of the aircraft as it headed towards the edge of the strip, along with the large skid angle, would have reduced rudder authority. This would then have prevented the pilot regaining directional control of the aircraft.

The factors considered relevant to the development of the accident were:

1. Windshear or downdraft conditions caused the pilot to lose control of the aircraft on late final approach.

2. The aircraft probably stalled during the bounce after a heavy landing, causing the left wing to contact the runway and the aircraft to yaw further left.

3. A severe right skid and decreasing speed reduced rudder effectiveness and prevented the pilot from regaining directional control.

Occurrence summary

Investigation number 199400266
Occurrence date 02/02/1994
Location Lithgow
State New South Wales
Report release date 23/09/1994
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Loss of control
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Beech Aircraft Corp
Model 36
Registration VH-AKX
Serial number E-1557
Sector Piston
Operation type Private
Departure point Merimbula, NSW
Destination Lithgow, NSW
Damage Substantial

Weatherly 620B, VH-WEK, Mount Murray, Victoria

Summary

The aircraft arrived at Snowy Range airstrip from Moorabbin at 1245 ESuT to participate in fire-bombing operations. Three fire-bombing flights to Mt Murray were completed. The aircraft was then reloaded and refuelled prior to the next flight which departed Snowy Range at 1455. At 1515, the pilot of a spotter aircraft, participating in the firefighting operation at Mt Murray, reported that VH-WEK had crashed while completing a fire-bombing run.

There were numerous firefighters who witnessed VH-WEK make its bombing run, some also witnessing the accident. A media helicopter crew recorded on video the aircraft making its bombing run and the accident sequence. From these sources, it was established that the aircraft made its bombing run flying up a steep slope on Mt Murray. The retardant was dropped and, about four to five seconds later, the aircraft appeared to commence a left turn. It was apparent from the video that airspeed was rapidly decreasing at this time. The aircraft appeared to stall, after which it struck trees and crashed.

Immediately after the accident, the helicopter pilot flew his aircraft to about 100 feet above the trees in the vicinity of the accident site but reported that due to downdrafts he was unable to sustain slow speed flight. He then repositioned his aircraft to about 500 to 600 feet above the accident site where he was able to sustain slow speed flight.

Witnesses reported that the engine of VH-WEK was at high power until the time the aircraft hit the trees. The previous bombing run was also made up-slope and the aircraft recovered via a wingover manoeuvre. Witnesses estimated that the aircraft was higher above the trees on the first run than it was on the accident run.

The investigation did not disclose any aircraft defect that could have contributed to the accident. The pilot probably elected to fly up-slope for greater bombing accuracy. However, up-slope runs create a difficult situation for exiting the valley at the completion of the run. An up-slope run also limits the options available in the event of an encounter with a downdraft, an adverse wind shift or a mechanical malfunction that prevents the load being dropped. The reason for the apparent loss of airspeed as the aircraft completed the firebombing run may be attributable to the reported downdrafts. However, this could not be positively determined.

Factors

The following factors were considered relevant to the development of the accident:

  1. The pilot flew the fire-bombing run up a steep slope.
  2. After the load was dropped, there was a loss of airspeed to the extent that a recovery after completion of the bombing run was not possible.
  3. Downdrafts were evident at the time of the accident.

Occurrence summary

Investigation number 199400232
Occurrence date 31/01/1994
Location Mount Murray
State Victoria
Report release date 09/03/1995
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Model Weatherly Aviation Company Ltd 620B
Registration VH-WEK
Sector Piston
Operation type Aerial Work
Departure point Snowy Range
Destination Snowy Range
Damage Substantial

Fatality aboard the off-shore supply vessel Shelf Supporter

Final report

Summary

Early on the morning of 29 December 1993, the Australian offshore supply vessel Shelf Supporter was discharging a deck cargo of empty skips and a container to North Rankin A platform, 70 miles north-west of Dampier. The weather was fine with the wind from the south-west at 20 knots.

The Master was manoeuvring the vessel, maintaining position, from the after end of the bridge, looking out over the cargo deck.

Seas were breaking over the stern, but conditions were not such as to cause the cancellation of cargo operations.

While a skip was being hoisted to the platform the two-man deck watch aboard Shelf Supporter decided to re-spool a wire used to secure the cargo, onto the winch. While this wire was being released from a block, a sea broke over the stern. Despite a warning from the Master, one of the two men on deck was crushed between the vessel's own rubbish skip and an empty skip when it was moved by the seawater.

Conclusions

It is considered that:

  1. The sea conditions at the time of the incident were not such as to warrant the cancellation of cargo operations.
  2. There was no apparent reason why the AB should not have heard the warning made by the Master.
  3. The AB was apparently caught unawares by the forward movement of the skip.
  4. The decision to re-spool the port tugger wire, to prevent it from being damaged, was in accordance with good seamanship but, coupled with an apparent belief that the position immediately forward of the athwartships skip was a safe one, resulted in the AB being in such a position so as to be crushed between the two skips.
  5. The act of leaving the port tugger wire lying flaked along the deck, and not re-spooling it on the winch as soon as the first lift was clear, was not in accordance with good seamanship and the delay in re-spooling the wire resulted in the athwartships skip becoming exposed before action was taken.
  6. Athwartships stowage, particularly of empty skips and other forms of bin, is undesirable, due to their greater vulnerability to movement by seas breaking on board.
  7. All cargo operations should be fully discussed between the platform/rig manager and the supply vessel master, and the order of operations agreed, before the vessel goes alongside.
  8. Although time may be at a premium, crane hooks should not be lowered to the supply vessel until such time as the crew on deck have signalled their readiness.

Occurrence summary

Investigation number 62
Occurrence date 29/12/1993
Location N. W. AUSTRALIA
Report release date 22/09/1994
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Marine
Marine occurrence category Fatality
Occurrence class Serious Incident
Highest injury level Fatal

Ship details

Name Shelf Supporter
IMO number 8405440
Ship type Supply vessel/dive support
Flag Australia
Departure point Dampier
Destination North Rankin A platform 70 miles NNW

Aero Commander 690A, VH-BSS, Sydney, on 14 January 1994

Summary

On 14 January 1994 at 0114, Aero Commander 690 aircraft VH-BSS struck the sea while being radar vectored to intercept the Instrument Landing System approach to runway 34 at Sydney (Kingsford-Smith) Airport, NSW. The last recorded position of the aircraft was about 10 miles to the south-east of the airport. At the time of the accident the aircraft was being operated as a cargo charter flight from Canberra to Sydney in accordance with the Instrument Flight Rules. The body of the pilot who was the sole occupant of the aircraft was never recovered. Although wreckage identified as part of the aircraft was located on the seabed shortly after the accident, salvage action was not initially undertaken. This decision was taken after consideration of the known circumstances of the occurrence and of the costs of salvage versus the potential safety benefit that might be gained from examination of the wreckage.

About 18 months after the accident, the wing and tail sections of the aircraft were recovered from the sea by fishermen. As a result, a detailed examination of that wreckage was carried out to assess the validity of the Bureau's original analysis that the airworthiness of the aircraft was unlikely to have been a factor in this accident. No evidence was found of any defect which may have affected the normal operation of the aircraft.

The aircraft descended below the altitude it had been cleared to by air traffic control. From the evidence available it was determined that the circumstances of this accident were consistent with controlled flight into the sea.

No safety recommendations resulted from this investigation.

Occurrence summary

Investigation number 199400096
Occurrence date 14/01/1994
Location 18 km SSE Sydney
State New South Wales
Report release date 27/04/1996
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Collision with terrain
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Aero Commander
Model 690
Registration VH-BSS
Serial number 11044
Sector Turboprop
Operation type Charter
Departure point Canberra, ACT
Destination Sydney, ACT
Damage Destroyed

Fire on board the Union Rotorua

Final report

Summary

The New Zealand registered roll on/roll off, gas turbine/electric ship Union Rotorua was about 27 miles south of Sydney Heads, en route for Melbourne, when a fire broke out in the gas turbine house.

It was established that the seat of the fire was in one of the cubicles of the 6.6 kilovolt switchboard, which distributed power from the gas turbine generator to the propulsion motors and auxiliary electrical systems.

Initial attempts to fight the fire with extinguishers proved to be ineffective and a decision was made to utilise the fixed firefighting medium and flood the space with CO2.

This was effective in extinguishing the fire. With the high voltage switchboard out of commission, the vessel was towed to Sydney, where it remained for three months undergoing repairs.

Conclusions

  1. It was not possible to establish the exact cause of the fire, although evidence indicates that it probably started in the yellow phase of the main generator circuit breaker at the lower "tulip", connecting the generator input to the circuit breaker.
  2. Initiation of the fire at the "tulip" connector may have been due to high electrical resistance caused by one or more of the following:
    • Loss of spring pressure (due to age or other causes) behind the connecting "fingers" of the "tulip".
    • Oxidation of the contact surfaces due to loss of silver plating on the contacts.
    • Mechanical fracture, due to vibration, of the end of the circuit breaker's connecting post at the point of change of cross-sectional area.
    • Loosening or fracture (due to vibration) of the socket-head cap screw securing the aluminium alloy collar mounting the connecting "fingers", to the end of the copper post.
  3. Although the Electrician's workbook noted, in June 1991, that the contacts on the "Main HT breaker" needed re-silvering, there was no indication that this was ever carried out.
  4. The fire spread to the adjoining cubicle containing the circuit breaker for the no.1 ship's service transformer. This may have been due to ionisation of the atmosphere by products of combustion from the fire in the main generator circuit breaker cubicle.
  5. The Inspector considers that the delay in shutting down the gas turbine generator, after the fire was discovered, was excessive, but that the actions of the ship's officers and crew in tackling the fire were prompt and correct in all other respects.
  6. The emergency response was effective and demonstrated planning and procedures of a high standard.

Occurrence summary

Investigation number 61
Occurrence date 29/12/1993
Location Off Port Kembla
State New South Wales
Report release date 11/01/1995
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Marine
Marine occurrence category Fire
Occurrence class Serious Incident
Highest injury level None

Ship details

Name Union Rotorua
Ship type General cargo
Flag New Zealand
Departure point Sydney, NSW
Destination Melbourne, Vic.