Cessna 210M, VH-XAJ

Safety Action

Safety Action Statement

As a result of this occurrence, the Australian Transport Safety Bureau issues the following safety advisory notice to the Civil Aviation Safety Authority.

SAN20010046

The Civil Aviation Safety Authority should note the safety deficiency identified during this investigation and consider introducing methods to identify and record time in service of piston engine cylinder heads particularly for those cylinder heads utilised in passenger carrying operations.

Analysis

The flight had progressed normally until the pilot reported the rough-running engine and associated high-indicated cylinder head temperature. The pilot could not determine the problem with the engine and decided to conduct a forced landing. As the pilot was seriously injured, the carriage of a portable ELT was ineffective in that the able-bodied passengers could not locate it in the aircraft.

The engine, while still within the overhaul period, had required several previous cylinder changes due to cylinder head cracking. The engine failure leading to the accident had also resulted from cylinder head fatigue cracking due to overheating.

Overheating of the cylinder head could be attributed to several factors.

  • The operation of the engine at a higher than normal operating temperature. This is possible due to varying pilot engine operating techniques over a number of flights. Only limited, and possibly inaccurate, engine temperature information was available to any pilot because of recorded defects with the cylinder head temperature indicating system.
  • The ring-type cylinder head temperature sensor was fitted to the number one cylinder head with the normal spark plug washer, effectively reducing the spark plug length. This may have contributed to a change in the normal combustion process, producing localised overheating near the plug and altering the thermal transfer within the cylinder. However, as this sensor was not fitted to other cylinders, this would not have occurred on the previous number four and number six cylinder failures.
  • The engine cooling baffles, being in poor condition, would have been less efficient in providing cooling airflow to the cylinders. The number one cylinder, being at the rear of the engine, would have been more susceptible to overheating. The engine manufacturer advises that poor baffling will have a significant effect on cylinder lives.
  • The prior cracking and replacement of the number four and number six cylinders indicates that the engine may have been subjected to higher than normal operating temperatures or that the cylinders had a reduced thermal cycle tolerance due to their age and time in service. At the time of the accident, the failed number one cylinder was seventeen years old.

CONCLUSIONS

The occurrence and subsequent occupant injuries were a result of the failure of the number one cylinder through fatigue cracking and the subsequent forced landing. Inaccurate cylinder head temperature indications may have contributed to the failure of the cylinder.

There are ongoing reported structural failures of piston engine cylinders as documented in the CASA MDR and ATSB occurrence data. Some of these failures have led to forced landings, which increases the risk of injury to aircraft occupants.

Aircraft piston engines must be maintained in accordance with CASA requirements and have their time in service history recorded in the engine logbook. However, this is not the case for piston engine cylinders, which are not required to have serial numbers for maintenance history documentation.

This report also highlights the limitations of carrying a portable ELT should the pilot become incapacitated and the need for comprehensive passenger briefings on the location and use of emergency equipment.

SAFETY DEFICIENCY

At present, there are no recommended or mandatory life requirements for piston engine cylinders in Australia for aircraft operated in any category of operation by either the piston engine manufacturers or the Civil Aviation Safety Authority. There is also no requirement for piston engine cylinders to be identified with serial numbers to document their history and time in service.

Summary

The flight, using a Cessna 210 aircraft, had been arranged as a charter after the scheduled regular public transport (RPT) service aircraft had become unserviceable. Waiting passengers were advised of the cancellation of the scheduled service and that limited seating would be available on a charter flight. Five passengers elected to take the charter flight using their previously purchased tickets and the company agent briefed them on the changed status of the flight.

Subsequently, while cruising at an altitude of 4,500 ft, the pilot reported to Adelaide flight service that the engine was running rough, that the engine cylinder head temperature (CHT) indication had become very high and that she was attempting to locate a clear area for a forced landing. The pilot landed the aircraft in a cleared gravel pit. During the landing roll however, the aircraft struck large mounds of gravel and was substantially damaged. The pilot and several passengers sustained serious injuries.

The aircraft came to rest upright, resting on the lower fuselage and right wingtip, with the tricycle landing gear folded back under the aircraft. The left wing was damaged with fuel escaping from the wing fuel tank. The engine had separated from the airframe and came to rest inverted in front of the wreckage.

The passengers evacuated the aircraft and assisted the unconscious pilot from the cabin. Adelaide flight service arranged for overflying aircraft to locate the accident aircraft and coordinated a rescue team to be dispatched from Darwin. A search-and-rescue (SAR) helicopter attended the scene and took the occupants to Darwin for medical attention.

The aircraft carried a manually operated GME Electrophone MT310 portable emergency locator transmitter (ELT), however the passengers were not aware of its location. Although the injured pilot attempted to direct the passengers to the ELT in the aircraft, the passengers were unable to locate it and as a result the ELT was not activated.

Aircraft engine

The aircraft was fitted with a Teledyne-Continental IO-520-L engine, serial number 567962, that had completed 734.5 hours since being overhauled. The engine was removed to a suitable engine maintenance facility for examination which revealed that the number one cylinder head had cracked, resulting in the observed high cylinder head temperature and rough running reported by the pilot. The cylinder head, part number TM642320F, had 10/81 stamped on the rocker boss, indicating that the cylinder head had been manufactured in October 1981. The history of the cylinder head, including the total time in service, could not be determined.

A detailed metallurgical examination of the cracked cylinder head determined that the cylinder head had failed as a result of fatigue cracking due to overheating (See Technical Analysis Report).

The engine was fitted with a six-point cylinder head temperature sensing system with a temperature sensor probe in the head of each cylinder. However, this system was inoperative at the time of the occurrence. A single, ring-type temperature sensor was fitted to the number one cylinder lower spark plug, in addition to a standard spark plug washer. Normally, a ring-type temperature sensor replaces the spark plug washer. This sensor provided cylinder head temperature information to the aircraft cylinder head temperature gauge. A maintenance release entry, dated 27 September 1998, stated "CHT gauge drops to zero periodically".

The engine baffles, used to direct cooling airflow over the engine cylinders, were in a generally poor condition with several cracks, broken mounting rings and worn areas. In one place, a baffle had been worn through by contact with an engine hose.

The engine had been overhauled on 18 August 1997 and fitted with six overhauled cylinders. On 11 August 1998, the number four cylinder head had failed because of cracking and was replaced. On 28 August 1998, the number six cylinder head had similarly failed because of cracking and was replaced. On 14 October 1998, 16.4 flying hours before the accident, the engine had passed a cylinder pressure leak check during routine maintenance.

Piston engine maintenance requirements

The Australian Civil Aviation Safety Authority (CASA) airworthiness directive, AD/ENG/4 (Amdt 7), details continuing airworthiness requirements for piston engines. That directive requires piston engines, operated in charter operations, to be overhauled in accordance with the engine manufacturer's requirements or in accordance with an approved system of maintenance. The directive also requires that the engine service history be recorded in the engine logbook. The engine manufacturer, Teledyne Continental Motors (TCM), does not specify retirement lives for engine cylinders but advises that "at some point in operating hours, generally very high, the aluminium cylinder head will fatigue due to the cylinder pressure loads and temperatures." TCM also advise that for cylinders in excess of two overhaul cycles "past that, duty cycle and the nature of field repairs make it difficult to project future life."

TCM also report that cylinder head life can be affected by any detonation/preignition event during the cylinder life, and that hot cylinder operation due to poor baffles or fuel mismanagement has a significant effect. CASA's information brochure titled "Piston Engine Cylinders" also recognises that those components have a limited life and suggests that cylinders be replaced every second or third engine overhaul. However, piston engine cylinders are not required to have serial numbers and recorded life history in the same manner as their parent engine.

Data review

A review of ATSB data covering the 10-year period January 1990 to December 1999 revealed that there had been over 60 reported occurrences, including a number of forced landings, involving piston engine cylinder head structural failures. Only one other reported cylinder head failure during this period resulted in occupant injuries. A review of the CASA major defect reporting (MDR) system for the same period revealed that there had been about 250 reported piston engine cylinder head structural failures, an average of approximately one failure every 2 weeks. The data only records the proportion of cylinder failures that have been reported through formal reporting procedures. Other cylinder head failures, such as those detected during routine maintenance, are possibly not represented.

Occurrence summary

Investigation number 199804715
Occurrence date 30/10/1998
Location 4 km S Gumadeer
State Northern Territory
Report release date 05/04/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Occurrence class Accident
Highest injury level Serious

Aircraft details

Manufacturer Cessna Aircraft Company
Model 210
Registration VH-XAJ
Serial number 21062846
Sector Piston
Operation type Charter
Departure point Maningrida, NT
Destination Darwin, NT
Damage Substantial

Boeing 737-377, VH-CZN

Safety Action

Local safety action

The Airservices Australia investigation report included a number of recommendations for consideration by Melbourne Centre management. A precis of those recommendations and responses follows:

  1. Recommendation - A controller who has just completed familiarisation should not oversight the familiarisation of another officer.

    This recommendation was not implemented. It remains the responsibility of individual controllers to assess whether they are capable of monitoring another officer.

  2. Recommendation - Amend the flight progress strip presentation for waypoints Oodnadatta and AGAGO.

    That recommendation was implemented.

  3. Recommendation - Review flight progress board presentation and sector workload.

    A workload review was conducted and the sector will be split horizontally. This is scheduled for implementation in November 1999.

  4. Recommendation - The coordinator position to be staffed with sufficient lead-time.

    A notice reminding controllers to employ the coordinator in sufficient time to enable adequate briefing and traffic assessment to be conducted has been included in console operational documents.

  5. Recommendation - Familiarisation should not take place when traffic density dictates that a coordinator is required.

    The recommendation was implemented.

  6. Recommendation - Review alternate methods for annotating potential conflict situations.

    No change was made.

Summary

A Boeing 737 (B737), VH-TJT, was en route from Darwin to Adelaide via air route J187 at flight level (FL) 370. Another B737, VH-CZN, was en route from Ayers Rock to Sydney via air route G222, also at FL370, which was a standard level for the direction being flown by both aircraft. The air routes converged, and eventually crossed at Oodnadatta. Both aircraft were under procedural (non-radar) control by Melbourne Sector 1. The sector console was staffed by a controller who was undergoing re-familiarisation prior to being checked for return to controlling. He was being supervised by a controller who had recently returned after a six month break from full-time operational controlling.

The controller had calculated estimates for Oodnadatta of 1518 and 1520 respectively for CZN and TJT. At 1515, when the crew of TJT reported at SARAH, 40 NM north-north-west of Oodnadatta, the controller became aware that there was no separation standard being applied between the two aircraft, so he instructed the crew of TJT to descend immediately to FL350. The crew reported on descent and indicated that their traffic alerting and collision avoidance system (TCAS) showed an aircraft 33 NM ahead, over Oodnadatta. The crew of TJT subsequently reported maintaining FL350 at 1520. As a result, there was a breakdown of the required vertical separation standard of 2,000 ft.

Both controllers had earlier noted the possibility for conflict between the two aircraft and annotated their respective flight progress strips with an Oodnadatta position, and the calculated estimates for that position. The estimates were annotated at different locations on the strips. There was no local instruction for the standardisation of the annotation of the Oodnadatta position or similar positions that marked the intersections of the various route crossings in the area. During the following 90 minutes, the traffic level steadily increased and the two controllers had discussed the need for a coordinator. The sector was normally operated as a solo operator position; however, there were periods when there were significant or complex traffic levels and there were procedures to enable the controller to be assisted by a coordinator in such cases.

Approximately 10 minutes prior to the occurrence, the controllers requested the assistance of a coordinator and as a consequence, a third controller joined them at the console. At this stage, the traffic situation was very busy, with approximately 70 flight progress strips being monitored and with additional strips being discarded or added to the board as flights progressed through the sector. The coordinator controller had little opportunity to obtain an adequate handover/takeover brief from the two controllers already at the position. The third controller assumed the coordinator position and endeavoured to action any items that he considered required attention as he attempted to gain some idea of the traffic disposition. He was unable to monitor the Sector 1 controller's air-ground-air program on a continuous basis due to the conduct of coordination actions. The work at the console was difficult, with three controllers working in an area normally used by only two controllers.

As a result of a combination a factors, the potential confliction between CZN and TJT, although recognised earlier by both controllers, was subsequently overlooked as the sector workload increased. It was only when the crew of TJT reported at SARAH that action was undertaken resolve the situation.

Airservices Australia carried out an investigation of this occurrence under the overall supervision of a Bureau officer. The significant factors that contributed to this occurrence were found to be;

  1. The two controllers manning the Sector 1 position were not operating at their optimum level of performance due to a lack of recency.
  2. Following an increase in Sector 1 traffic density, the controllers' recognition that they required coordination assistance to manage the increased workload was too late to provide any effective relief.
  3. The amount and disposition of traffic in the sector led the controllers to be distracted to a point where they were unable to adequately monitor all sector traffic.
  4. The controllers' annotation of flight progress strips did not alert them to the possibility for a conflict between CZN and TJT.

Occurrence summary

Investigation number 199804690
Occurrence date 29/10/1998
Location Oodnadatta, (NDB)
State South Australia
Report release date 26/07/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Loss of separation
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer The Boeing Company
Model 737
Registration VH-CZN
Serial number 24303
Sector Jet
Operation type Air Transport High Capacity
Departure point Ayers Rock, NT
Destination Sydney, NSW
Damage Nil

Aircraft details

Manufacturer The Boeing Company
Model 737
Registration VH-TJT
Serial number 24445
Sector Jet
Operation type Air Transport High Capacity
Destination Adelaide, SA
Damage Nil

Beech Aircraft Corp 1900D, UE-200

Safety Action

The Australian Transport Safety Bureau (formerly BASI) is conducting a technical analysis of the blade failure. Any safety deficiencies identified will be published in the Bureau's Quarterly Safety Deficiency Report.

Summary

Whilst taxiing for a night departure, the right propeller was struck by a large bird, resulting in the separation of one propeller blade. The ensuing vibration caused substantial damage to the engine mountings and firewall, before the engine could be shut down.

A technical analysis determined that the blade had failed in overload about 15cms from the blade root whilst the propeller was in fine pitch. There was no evidence of any pre-existing cracking or defects in the area which may have contributed to the failure.

The blade had completed 10,228 hours of operation since new and 3,805 hours since last overhaul. The aircraft records indicated that there were no outstanding maintenance requirements on the propeller. The blade complied with all propeller certification requirements.

Witnesses described the bird carcass as that of a Brolga. This species grows to a height of 0.7 to 1.3 metres with a mass of 10 to 15 kilograms.

Occurrence summary

Investigation number 199804451
Occurrence date 20/10/1998
Location Coffs Harbour, Aero.
State New South Wales
Report release date 12/01/2000
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Birdstrike
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Beech Aircraft Corp
Model 1900
Registration VH-AFR
Serial number VH-AFR
Sector Turboprop
Operation type Air Transport Low Capacity
Departure point Coffs Harbour, NSW
Destination Unknown
Damage Minor

Abnormal engine indications Pilatus PC-12, VH-FMC, 19 km south-south-east of Port Augusta, 20 October 1998

Safety Action

Local safety action

The operating company repaired the faulty wiring loom and checked the other aircraft in the fleet for similar problems.

Safety action by the engine manufacturer

The engine manufacturer has initiated an oil and oil filter analysis program across the worldwide fleet, in an ongoing product improvement program to remedy the discolouration and particulate problems.

Bureau of Air Safety Investigation safety action

The Bureau is monitoring the analysis program.

Summary

While climbing through 7,000 ft the engine indicating system, low oil pressure caution light, illuminated. With the oil pressure indication fluctuating around 90 pounds per square inch, and the caution light flickering, the pilot in command reduced power and elected to return to Port Augusta. During descent the warning light continued to flicker, changes in power setting having no effect. As the aircraft turned on to base leg, the warning light became steady and the oil pressure dropped to less than 60 pounds per square inch. The aircraft made an uneventful landing. Shortly after touchdown, the oil pressure returned to 100 pounds per square inch and the caution/warning lights extinguished.

Investigation by maintenance personnel resulted in an oil filter change due to suspected carbon contamination. The aircraft was then returned to service. The operator raised the recurring oil pressure fluctuation problems with the engine manufacturer.

The Pratt & Whitney PT6 engine model installed in the PC12 has experienced episodes of oil discolouration, and carbon particles in the oil. The discolouration was traced to the coatings in the magnesium gearbox, and the carbon was traced to the No. 2 bearing area.

Further investigation of the fluctuating oil pressure indications revealed a fault in the main engine wiring loom.

Occurrence summary

Investigation number 199804687
Occurrence date 20/10/1998
Location 19 km SSE Port Augusta, (NDB)
State South Australia
Report release date 15/07/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Abnormal engine indications
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Pilatus Aircraft Ltd
Model PC-12
Registration VH-FMC
Serial number 109
Sector Turboprop
Operation type Aerial Work
Departure point Port Augusta, SA
Destination Adelaide, SA
Damage Nil

Aero Commander 500-S, VH-YJT

Safety Action

As a result of the investigation into the circumstances leading to the accident of a Cessna 185E floatplane at Calabash Bay, NSW (Occurrence 199802830), the Bureau issued Recommendation R19980277 on 6 January 1999. During the course of that investigation a number of organisational and management deficiencies were identified concerning the conduct of charter flight operations. One of those deficiencies concerned the adequacy of assessing chief pilot applicants in their ability to manage the conduct of safe flight operations. A similar safety deficiency was identified during the course of this investigation (Occurrence 199804432).

Part (ii) of safety recommendation R19980277 stated:

"The Bureau of Air Safety Investigation recommends that the Civil Aviation Safety Authority:

(ii) develop a process to assess the ability of a chief pilot applicant to administer and manage regulatory and safety compliance."

The response from CASA indicated that it intended to amend the Air Operator Certification Manual to more adequately address system safety management issues. The Bureau will continue to monitor the progress of that amendment.

Significant Factors

  1. The pilot had little experience flying in operationally limiting situations and did not appear to recognise the critical need to carefully monitor fuel quantity during those situations.
  2. There was no reliable system available to the pilot to assess the fuel quantity in the aircraft during the accident flight.

Analysis

Evidence indicated that the engines had stopped because of fuel exhaustion.

In order to maximise payloads the aircraft was normally operated with the minimum fuel sufficient for safe flight. Consequently, the fuel tanks would have rarely been filled to capacity. As filling the fuel tanks to capacity provided one of the only opportunities to accurately determine a datum for the assessment of fuel quantity, any subsequent inaccuracies in the system of assessing fuel quantity would have compounded over extended periods. As most of the pilot's previous flying experience had not involved working in situations where it was necessary to carefully balance the requirements of payload against fuel, it is possible that he did not recognise the critical need to carefully monitor such aspects of the operation.

There were two systems available to a pilot to monitor fuel quantity - a fuel quantity indicator and a fuel log. The fuel quantities as determined by each system should have been in agreement. During the accident flight, however, the pilot had covered the fuel gauge due to intermittent and unreliable fuel indications, which made one system unusable. In addition, the fuel-log system was not being applied with rigour and did not provide an accurate indication of the actual fuel quantity. This had masked any opportunity to reveal differences in estimated and actual consumption rates, when compared with the fuel gauge. As a result, at the time of the occurrence the aircraft had substantially less fuel on board than the pilot believed to be the case.

CASA had recently assessed the pilot as competent to act as chief pilot. Although he met all the regulatory requirements to fulfil that role, he had little experience in managing flight operations to ensure regulatory compliance. The process of approval for the position of chief pilot did not appear to adequately assess his capabilities to control and maintain a consistent, safe system of flight operations. The process adequately addressed the candidate's knowledge of the regulatory requirements, but was insufficient to adequately assess managerial ability. Although the organisation was approved to conduct fare-paying passenger flights, the management structure and expertise of the chief pilot did not provide for effective oversight of the operational aspects of those activities. The rear left seat passenger was thrown forward into the front right seat by impact forces because the seat-belt restraint was probably not secure at the time of impact, due to the unusual amount of force required to secure it correctly. This may have given the impression that the harness was locked when in fact it was not securely fastened.

FINDINGS

  1. The pilot was correctly licensed and qualified to operate the flight as a VFR charter operation.
  2. The aircraft was dispatched with an unusable fuel quantity indicator.
  3. The right engine fuel control unit was worn and allowed additional fuel through the system, increasing fuel consumption by approximately 6 L/hr.
  4. Inappropriate fuel consumption rates were used for flight planning.
  5. The aircraft fuel log contained inaccuracies that resulted in a substantial underestimation of the total fuel used.
  6. At the time of the occurrence, there was no useable fuel in the aircraft fuel system.
  7. Although the pilot met the Civil Aviation Safety Authority criteria to fulfil his role as chief pilot, he did not have the expertise to effectively ensure the safety of company flight operations.

Summary

History of the flight

A Shrike Commander departed Horn Island on a charter flight to Saibai and Boigu Islands in accordance with the visual flight rules (VFR). The flight to Saibai took 32 minutes, and a further 13 minutes to Boigu Island. The aircraft then departed Boigu to return to Horn Island with an expected flight time of 35 minutes.

The pilot reported that he had maintained 5,500 ft until commencing descent at 35 NM from Horn Island. He tracked to join final approach to runway 14 by 5 NM, reducing power at 1,500 ft. At 5 NM from the runway, the pilot extended the landing gear and approach flap and commenced a long final approach.

When the aircraft was approximately 3 NM from the runway both engines commenced to surge, with the aircraft initially yawing to the right. The pilot commenced engine failure procedures and retracted the flaps. He tried a number of times to determine which engine was losing power by retarding the throttle for each engine, before deciding that the right engine was failing. The pilot shut down that engine and feathered the propeller. A short time later, when the aircraft was approximately 200 ft above the water, the left engine also lost power. The pilot established the aircraft in a glide, advised the passengers to prepare for a ditching, and transmitted a MAYDAY report on the flight service frequency before the aircraft contacted the sea. The aircraft quickly filled with water and settled on the seabed. All five occupants were able to escape and make their way ashore.

Wreckage and impact information

The aircraft ditched approximately 400 m short of the threshold of runway 14, and settled in 2.5 m of water. It was subsequently recovered for examination. Although the aircraft had been damaged during the ditching, it remained essentially intact. The fuselage was distorted in front of and behind the cabin area as a result of impact forces. The underside of the fuselage had also been pushed upwards, and both windscreens were broken. The fuel tanks were intact, and the fuel tank vents were not obstructed.

Personnel information

The pilot in command had gained a commercial pilot licence in 1994, and worked as a flight instructor until April 1998. He had been based at Horn Island since April and was subsequently appointed as the company chief pilot on 11 September 1998. Two days prior to his appointment he had been endorsed on the Aero Commander. At the time of the occurrence, the pilot had accumulated a total flying experience of 2,045 hours, including 566 hours on multi-engine aircraft, and 79 hours on Shrike Commander aircraft.

Aircraft information

The aircraft had undergone scheduled maintenance in Cairns on 28 August 1998, and had since flown 100.8 hours. The next scheduled maintenance was due in 19.2 hours. The horizontal situation indicator was unserviceable and had been placarded as such, with the defect being recorded in the maintenance release; however, that did not preclude the conduct of VFR flight.

No defects that could have contributed to the accident were found in the airframe or flight control systems. An examination of the engines and their associated systems did not reveal any defects that could have led to the loss of power. The right engine fuel control unit was found to be serviceable but worn. Bench tests indicated that it provided a fuel flow 10% greater than normal (approximately 6 L/h).

The right propeller had been feathered before the ditching; however, the propeller blades had not moved to the fully feathered position. Examination of the propeller dome revealed that oil sludge had prevented the propeller piston from driving the blades to the fully feathered position.

It was determined that the aircraft had been operated within its normal weight-and-balance range throughout the accident flight

The fuel system of the Shrike Commander consisted of five interconnected tanks, with one fuel quantity indicator receiving an electrical signal from a float-type sensor mounted in the fuselage tank. The flight manual specified that a fuel quantity indicator was a mandatory instrument for operation of the aircraft.

A single fuel filler point was situated on the upper surface of the right wing, inboard of the engine, and connected to the right forward wing tank. It was not possible to assess the fuel quantity by "dipping" the fuel tank through the fuel filler point. After the aircraft had been recovered from the sea the fuel system was drained and found to contain approximately 0.75 L of aviation fuel and approximately 100 L of seawater. The fuel quantity indication system was examined. A wire that connected to the wiper arm in the fuel transmitter unit was found to be broken under its insulation, causing an intermittent open circuit, which resulted in a fluctuating fuel quantity indication. When the wire was repaired the fuel indication system operated normally. The wire to the wiper arm in the fuel quantity transmitter had been repaired on 7 August 1998 by resoldering the wire onto the wiper arm. The maintenance manual for the Shrike Commander provided instructions for removal and replacement of the transmitter unit; however, there were no instructions for disassembly and repair of any components within the unit. No other defect was found in the fuel quantity indication system.

A piece of adhesive paper was found covering the fuel quantity indicator. The pilot reported that he had covered the indicator before the flight because he noticed that its indications had been intermittent on a flight the previous day, and believed that the fluctuating indications might have alarmed the passengers.

Fuel planning and consumption

Company operations in the Torres Strait involved transporting passengers and freight on flights between the islands. Pilots would frequently undertake two or three flights each day, with up to five sectors per flight. The Shrike Commander was normally flown with less than full fuel tanks in order to permit greater payloads.

An examination of the aircraft fuel records since the fuel tanks were last filled on 13 October 1998 revealed that the average fuel consumption rate was 143 L/h, with an average sector time of 22 minutes. The company operations manual specified the procedure to be used for fuel planning. That procedure stipulated that the fuel consumption rate for the Aero Commander was to be calculated at a rate of 110 L/h, with an additional allowance of 20 L for each takeoff. The fuel log found in the aircraft revealed that, in practice, pilots had used a consumption rate of 120 L/h without any additional allowance for takeoff's.

A fuel log was maintained for each flight; however, during the investigation significant inconsistencies in the recording of fuel quantities were repeatedly found between consecutive fuel log records. The fuel log indicated that before the aircraft was partially refuelled prior to the accident flight, the fuel tanks appeared to have 170 L of fuel remaining. Investigation revealed that the actual quantity was substantially less.

Survival aspects

During the impact sequence, the passenger in the rear left seat was thrown over the centre seats into the front right seat, which was unoccupied at the time. The passenger in the centre right seat received a back injury. Both windscreens were shattered by the impact. The pilot pushed out the remaining pieces of perspex on the left windshield with his hands, cutting his finger in the process, and the passenger who had been thrown into the front right seat was able to kick out the remaining perspex pieces of the right windshield. The pilot and the three passengers in the front of the cabin exited the aircraft through the open windshields. The passenger in the rear right seat escaped through the emergency exit window. The cabin rapidly filled with water. All the occupants then swam ashore, assisting the injured passenger.

All the aircraft seating and seat-belt assemblies were found to be securely attached to the airframe. Surface corrosion was present on seat-belt end fittings, which was consistent with salt-water immersion, and all except one operated normally. The left rear passenger lap-belt end fittings were stiff to operate, and difficult to close properly. The end fittings could be easily placed together incorrectly, allowing improper locking of the assembly.

The aircraft was not equipped with life jackets, nor was that a requirement for the intended operation.

Organisational and management information

The company had expanded rapidly over a short period. At the time of the accident, it was operating 13 aircraft of various types. The company structure consisted of a managing director who was based in Melbourne, an operations manager who controlled sales and the allocation of tasks to aircraft, a chief pilot who managed the aircrew and assigned their duties, and a total of seven pilots. The chief pilot had worked for the company for six weeks, and was his first appointment as a chief pilot. During the course of the investigation, it became apparent that he had had minimal experience or guidance in the management of operational personnel. There was evidence that the new chief pilot had experienced difficulty in establishing practices that ensured compliance with safety requirements.

The pilot had been approved as a chief pilot in accordance with the procedures contained in the Civil Aviation Safety Authority (CASA) Air Operator Certification Manual. The guidelines in appendix 16 stated that it was preferable to have a chief pilot who could "manage the system" rather than one with the best manipulative skill. A candidate for the position of chief pilot was required to demonstrate to a CASA Flying Operations Inspector (FOI) an ability to operate within the regulatory framework. The checklist for the approval process contained a list of regulatory knowledge required of a chief pilot, however, no guidance was provided to an FOI in assessing the overall capability of an applicant to manage the objectives of the operator, within the boundaries imposed by aviation safety legislation.

No formal system of responsibility for maintenance control existed within the organisation. Unscheduled maintenance was recorded on a whiteboard in the operations room, but responsibility to ensure that the whiteboard was kept up to date was not a delegated duty of any of the company personnel.

Pilots verbally reported defects to the chief pilot, who would then approach the relevant maintenance organisation to arrange for rectification. The company used four different suppliers of third-party maintenance, depending on the aircraft. The remoteness of the location meant delays would frequently occur while spare parts were sourced.

Occurrence summary

Investigation number 199804432
Occurrence date 21/10/1998
Location Horn Island, Aero.
State Queensland
Report release date 19/05/2000
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Ditching
Occurrence class Accident
Highest injury level Minor

Aircraft details

Manufacturer Aero Commander
Model 500
Registration VH-YJT
Serial number 3089
Sector Piston
Operation type Charter
Departure point Boigu Island, QLD
Destination Horn Island, QLD
Damage Substantial

Lockheed L-1011, HS-LTA

Safety Action

As a result of this occurrence, the Bureau of Air Safety Investigation is currently monitoring a perceived safety deficiency. The deficiency relates to the layout of flight documents for Melbourne international airport.

Since this occurrence, Airservices Australia has approached Jeppesen on the matter. As of 4 December 1998, Jeppesen has changed the layout of the Melbourne 16 RADAR FOUR instrument departure plate in order to reduce the potential for confusion.

Summary

The Lockheed "Tristar" was cleared to depart from Melbourne on a runway 16 RADAR FOUR standard instrument departure (SID). Following departure, the pilot turned right onto a heading of 300 degrees at the upwind end of the runway. The SID required the crew to maintain the aircraft on a heading of 160 degrees until 4NM from the airport, before taking up its assigned heading. There was no breakdown in separation standards.

There have been a significant number of similar occurrences involving this particular SID. Airservices Australia are presently discussing the layout of the relevant operational charts with Jeppesen, in order to reduce the potential for misinterpretation of the charts.

Occurrence summary

Investigation number 199804358
Occurrence date 15/10/1998
Location Melbourne, Aero.
State Victoria
Report release date 15/07/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Lockheed Aircraft Corp
Model L-100
Registration HS-LTA
Sector Jet
Operation type Air Transport High Capacity
Departure point Melbourne, VIC
Destination Den Pasar, INDONESIA
Damage Nil

Fairchild SA227-DC, VH-KEU

Safety Action

Local safety action

  1. The aerodrome operator will ensure that a NOTAM is issued detailing the configuration and use of the grass strips;
  2. The aerodrome operator will investigate whether radio communications to and from aircraft operating from the grass strips are masked from aircraft on final approach to runway 18; and
  3. The flying school operator will ensure that the antenna configuration on the Cessna is not contributing to masking when the aircraft is operating from the grass strips

Summary

A Metro 23 aircraft was conducting Global Positioning System (GPS) approaches to runway 18 at Avalon. Whilst in the holding pattern north of the aerodrome the crew heard a radio broadcast from a Cessna 150 taxiing at Avalon. On leaving the holding pattern, the crew made a broadcast on the Avalon mandatory broadcast zone (MBZ) frequency advising their intentions. There was no response from any other traffic. At 5 NM on final approach to runway 18, the crew made a broadcast advising their intention to conduct a missed approach over the runway 18 threshold. Again, there was no response from any other traffic.

Overhead the threshold, at a height of about 500 ft, the crew heard a broadcast from Avalon Flying Operations (UNICOM) to the pilot of a Cessna, advising that there was a Metro inbound to his right. The Cessna had just become airborne from a grass strip, tracking to the west. The Metro crew sighted the Cessna and had to make a hard right turn and climb to avoid the aircraft.

The Cessna was being operated by a flying training organisation based at Avalon and had departed from an east-west grass strip located to the east of the runway 18 threshold. The grass strip is one of series of strips that were prepared and used by a previous manufacturer based at Avalon; however, none of the strips were depicted on any of the relevant aerodrome charts.

The Metro crew advised that they were not aware of any grass strips at Avalon. Accordingly, the Metro crew may not have associated any broadcasts that included reference to runway 27 as being applicable to Avalon.

The pilot of the Cessna advised that he made taxiing, entering and backtracking, and departure reports but did not get a response, nor did he hear any broadcasts from the Metro. He did, however, receive and respond to a broadcast from the Metro crew while in flight after the incident. Although the Metro crew heard the taxiing call, a number of hangars in the area may have masked radio reception by both aircraft when the Cessna was operating in the area of the grass strips.

Occurrence summary

Investigation number 199804347
Occurrence date 04/10/1998
Location Avalon, Aero.
State Victoria
Report release date 09/08/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Near collision
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Fairchild Industries Inc
Model SA227
Registration VH-KEU
Serial number DC-846B
Sector Turboprop
Operation type Air Transport Low Capacity
Departure point Melbourne, VIC
Destination Avalon, VIC
Damage Nil

Aircraft details

Manufacturer Cessna Aircraft Company
Model 150
Registration VH-WXY
Serial number 15079205
Sector Piston
Operation type Flying Training
Departure point Avalon, VIC
Destination Avalon, VIC
Damage Nil

Airbus A320-211, VH-HYF

Safety Action

As a result of this occurrence, the Bureau of Air Safety Investigation is currently investigating a perceived safety deficiency. The deficiency relates to wake turbulence separation standards between aircraft operating within controlled airspace and those operating at or below the lower limit of controlled airspace.

Any safety output issued as a result of this analysis will be published in the Bureau's Quarterly Safety Deficiency Report.

Summary

The crew of an Airbus A320, operating under instrument flight rules (IFR), was cleared to descend to 4,000 ft on a BROOK TWO standard arrival route. The approach radar controller advised the A320 crew of two other aircraft, operating outside controlled airspace, on the reciprocal track to their aircraft. The controller reported a primary radar return only on the first aircraft and that the second aircraft was indicating an unverified Mode C altitude of 3,500 ft. The lower limit of controlled airspace in the area was 3,500 ft and was available for use by aircraft outside controlled airspace.

The pilot of the A320 levelled the aircraft at 4,300 ft and maintained that altitude until both pilots sighted the first aircraft. The A320 crew then received a Traffic Alert and Collision Avoidance System (TCAS) traffic advisory alert on the second aircraft. The TCAS indicated that the second aircraft was 800 ft below the A320. The crew then sighted that aircraft.

The minimum vertical separation requirement between an IFR aircraft in controlled airspace, and an aircraft operating under visual flight rules outside controlled airspace is 500ft. This spacing may on occasions be insufficient to prevent activation of a TCAS alert, or to provide adequate wake turbulence separation between aircraft.

Occurrence summary

Investigation number 199804285
Occurrence date 06/10/1998
Location 28 km SE Perth, Aero.
State Western Australia
Report release date 04/08/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category ACAS warning
Occurrence class Accident
Highest injury level None

Aircraft details

Manufacturer Airbus
Model A320
Registration VH-HYF
Serial number 027
Sector Jet
Operation type Air Transport High Capacity
Departure point Melbourne, VIC
Destination Perth, WA
Damage Nil

Aircraft details

Manufacturer Unknown
Model Aeroplane
Departure point Unknown
Destination Unknown
Damage Nil

Cessna 210R, VH-MOK

Summary

While flying at 350 feet, during a final test line run for a geo-survey operation, the pilot of a Cessna 210 transmitted a distress message stating that the aircraft's engine had failed. The pilot conducted a forced landing in a nearby field. He later reported that he had selected an alternative fuel tank in an unsuccessful attempt to restart the engine prior to conducting the forced landing.

In consultation with BASI, an assessment of the aircraft fuel quantity and engine condition was carried out by a representative of the aircraft's insurer. This assessment indicated that the aircraft's fuel quantity had been approximately 70 L in the left tank and nil detectable fuel in the right. The examination of the engine revealed no identifiable problems that could have contributed to the engine failure.

The aircraft was fitted with long-range fuel tanks. The pilot reported that the refuelling operation had been carried out on a sloping surface and therefore, the aircraft may not have been laterally level. He was aware that there was a 'Caution' in the aircraft flight manual which stated that, 'indication errors of up to 14 gallons [53 L] per tank may result from a one-degree lateral deviation from level'.

The reason for the reported engine failure could not be determined.

Occurrence summary

Investigation number 199804254
Occurrence date 10/10/1998
Location 15 km W Cobar, Aero.
State New South Wales
Report release date 29/07/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Forced/precautionary landing
Occurrence class Accident
Highest injury level None

Aircraft details

Manufacturer Cessna Aircraft Company
Model 210
Registration VH-MOK
Serial number 21064933
Sector Piston
Operation type Aerial Work
Departure point Cobar, NSW
Destination Cobar, NSW
Damage Substantial

Boeing 747-438, VH-OJP

Safety Action

Local safety action

The operator issued a standing instruction to all crews reminding them to ensure that company procedures were adhered to when communicating to air traffic control via the CPDLC.

Bureau of Air Safety Investigation safety action

As a result of this and similar occurrences, the Bureau of Air Safety Investigation is investigating a perceived safety deficiency. The deficiency relates to the use of controller pilot datalink communication (CPDLC) messages by air traffic control and pilots for the exchange of operational information.

Any safety output issued as a result of this analysis will be published in the Bureau's Quarterly Safety Deficiency Report.

Summary

A Boeing 747 (B747) was en route from Auckland to Melbourne, maintaining flight level (FL) 330. The aircraft was experiencing some turbulence. The crew were communicating with Auckland air traffic control via controller pilot data link communications (CPDLC) and were awaiting a response to a request to climb to FL350.

The crew had observed on their traffic alerting and collision avoidance system (TCAS) that another aircraft was crossing their route from the south-east to the north-west at FL350. They were aware that a clearance to climb to FL350 would not be available until that aircraft had passed. The other aircraft was a B737 en route from Wellington to Brisbane. The air routes intersected at the VIMAV reporting point. At 2002 the B737 crew reported at VIMAV maintaining FL350. At 2005, the B747 passed VIMAV.

At about 2010, the B747 crew received a conditional clearance to climb to FL350 at 2018. The delay in the climb approval was required to establish a 15-minute time standard between the two aircraft at the intersection of the air routes. The B747 crew immediately commenced climb to FL350 after the message was received. At 2012 they dispatched a message reporting they were maintaining FL350. When air traffic control notified the crew via high-frequency radio that they had not complied with the clearance, the crew descended the B747 to FL330. The B747 TCAS did not register an alert during the period that separation was infringed.

Normal company CPDLC practice for the B747 crew was for the non-flying pilot to read out the message on the screen, and for this to be confirmed by the flying pilot. Once the message and the subsequent response were confirmed by the two crew members the non-flying pilot dispatched the message to air traffic control.

The investigation found that the crew, for reasons unknown, had mis-interpreted the datalink message as an immediate clearance to climb. It is possible that, due to the turbulence being experienced, the crew acted hastily to acknowledge the message and climb the aircraft to reduce passenger discomfort. It is likely that either one or both of the crew were not as vigilant in their checking of the message as they would have been under less demanding circumstances.

Occurrence summary

Investigation number 199804135
Occurrence date 25/09/1998
Location 19 km W VIMAV
State International
Report release date 15/07/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Loss of separation
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer The Boeing Company
Model 747
Registration VH-OJP
Serial number 25545
Sector Jet
Operation type Air Transport High Capacity
Departure point Auckland, NEW ZEALAND
Destination Melbourne, VIC
Damage Nil

Aircraft details

Manufacturer The Boeing Company
Model 737
Registration ANZ161
Sector Jet
Operation type Air Transport High Capacity
Departure point Wellington, NEW ZEALAND
Destination Brisbane, QLD
Damage Nil