de Havilland Canada DHC-6-320, VH-FNU

Summary

The crew of the DHC-6-320 aircraft reported that during descent to Cairns they smelt smoke in the cockpit. They then noticed the battery load meter was at maximum discharge and the right generator light was illuminated. The left generator switch was moved to the OFF position, however, the generator remained on-line.

Subsequent in-flight inspection revealed that the smoke was coming from behind the right cabin roof panel, which had begun to melt and bubble. The pilot in command then contacted Cairns approach control reporting a fire in the cabin and the aircraft was cleared to track direct to Cairns. The co-pilot accessed the cabin fire extinguisher and extinguished the fire. At approximately 4NM from the airport, the co-pilot reported that the fire was an electrical fire and had been extinguished. After landing, the crew stopped the aircraft on the runway and shut down the right engine to allow the fire fighters access to the cabin. Following confirmation that the fire was extinguished the aircraft was taxied to the terminal.

Investigation by the owner's maintenance organisation found that the left reverse current relay had severe heat damage. Other components and wiring near the left reverse current relay were also heat damaged. The reverse current relay was disassembled by the maintenance organisation's engineers, but they were unable to determine the reason for the failure due to the severity of the heat damage.

The Bureau did not conduct an on-site investigation of this occurrence.

Occurrence summary

Investigation number 200001876
Occurrence date 20/05/2000
Location 28 km E Cairns, Aero.
State Queensland
Report release date 24/08/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fire
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer De Havilland Canada/De Havilland Aircraft of Canada
Model DHC-6
Registration VH-FNU
Serial number 286
Sector Turboprop
Operation type Aerial Work
Departure point Mackay, QLD
Destination Cairns, QLD
Damage Minor

Cessna 402C, VH-NMQ

Safety Action

Several safety deficiencies were identified during the initial phase of the investigation. Local safety action was agreed to and addressed by the operator prior to publication of the final report. Those safety actions were as follows:

Issue of company Maintenance Alert MA/C400/2, which required a detailed inspection and functional check of the fuel selector system of all the operator's Cessna 402C aircraft.

A second Alert MA/C400/2 amendment 1, was issued a short time later after the initial fleet inspection found that the fuel selector valves for a second aircraft were out of synchronisation with the selector indicator. This alert detailed further inspection and rectification instructions.

The operator has undertaken to re-examine the company operations manual with a view to improving the guidance information on fuel planning and reserves.

The operator has agreed to re-examine the need for the cross-feed and shut-off checks. If they are considered necessary, then a procedure to ensure that the desired outcome is achieved will be devised and introduced.

The operator's maintenance controller has introduced procedures to ensure that all trip records are now vetted daily. Any endorsement item considered to have the potential to affect the safety of flight will now be subject to immediate maintenance rectification.

The operator has amended and amplified the incident and accident reporting section of the company Policy and Procedures Manual to better reflect the correct reporting procedures.

The Operator has introduced the Daniel System Australia, Integrated Aviation Software (IAS) in the company's electronic maintenance control system. This software has the ability to monitor and identify repetitive defects. The company Maintenance Control manual Vol 1, section 9 has been changed to reflect the changed procedures.

Analysis

The fuel selector system defect need not have led to a situation in which the safety of the flight was not assured.

The problem was recognised by the pilot early in the flight, and, despite attempts to resolve it, was confirmed when about mid-way. Consequently, without fuel from the right tank, there was insufficient fuel available for the planned flight fuel requirement, let alone the required reserve fuel. The pilot considered that a landing at an alternate aerodrome may have been necessary. However, the need to maintain adequate reserve fuel to ensure safety of the flight was apparently not recognised. As the flight progressed, the quantity of fuel required was assessed only in the context of a direct approach and landing at Darwin.

After landing, the fuel gauge indicated that the left tank contained about 20 lb of unusable fuel. The pilot had therefore made the decision to overfly an alternate aerodrome when in reality, only about 20 lb (or about 6 minutes) of fuel was available.

Maintenance oversight of the aircraft was inadequate. This is evidenced by:

  • the number of reported occurrences of fuel system problems; and
  • the deferral of rectification of 3 such problems because they were regarded as "not major defect".

The repetition of reports and the request entered on the maintenance release to "please report further", suggest that the focus of maintenance rectification action was deficient.

The late reporting of the occurrence to the ATSB and to the operator's maintenance controller arose through breakdowns in the operator's reporting procedures following staff changes.

Summary

History of the flight

The pilot of a Cessna 402C aircraft, VH-NMQ, was conducting a scheduled passenger service from Tindal to Darwin, with 4 passengers.

During the climb to the planned cruise altitude of 8,000 ft, the fuel quantity gauges indicated that fuel was being consumed from the left tank only. At the top of climb, the fuel gauges indicated 100 lb in the left tank and 200 lb in the right tank. Once established in the cruise the pilot tried to balance the fuel load by positioning the left fuel selector to allow the left engine to be supplied with fuel from the right tank.

Approaching the midway point between Tindal and Darwin, the fuel gauges confirmed that the imbalance remained. The pilot assessed that sufficient fuel was available to continue to Darwin. As the flight approached the last suitable alternate aerodrome, the pilot calculated that 13 lb of fuel was needed to reach Darwin from that point, based on the current consumption rate. The left fuel tank gauge showed 40-lb remaining.

The pilot requested and was given a direct approach to runway 29. During the landing roll the left engine stopped, and the right engine stopped soon after the aircraft cleared the runway. The fuel quantity gauges showed 20 lb for the left tank and 200 lb for the right tank.

The operator's ground support staff then towed the aircraft to the terminal area where the passengers disembarked normally.

The aircraft had flown from Darwin for Tindal the previous day with 650 lb of fuel on board. The pilot's navigation log showed that 365 lb was required for the flight from Tindal to Darwin. This comprised 230 lb flight fuel (59 minutes), 100 lb fixed reserve (30 minutes), 25 lb variable reserve fuel, and 10 lb taxi fuel. The navigation log also showed the total fuel on-board at Tindal before departure for Darwin was 385 lb. The pilot reported that before departure from Tindal, the aircraft fuel quantity gauges showed 185 lb in the left tank and 200 lb in the right. The pre-flight check of the fuel cross-feed was normal.

A landing at an alternate aerodrome was not considered necessary, as the pilot had calculated sufficient fuel was available to continue to Darwin, and was conscious of the operating schedule for the aircraft. However, company management stated that there was no instruction or pressure on pilots in this regard.

The pilot held a current commercial pilot licence, a command multi-engine instrument rating a valid medical certificate, and had logged 2,454 hours aeronautical experience. This included 150 hours on Cessna 402C aircraft. The pilot's last proficiency check was on 8 March 2000.

On the day of the occurrence, 5 May 2000, the pilot did submit an incident report to the operator. However, due to a breakdown in the operator's reporting procedures following staff changes, the ATSB was not notified of the occurrence until 15 May. As a result, it was unable to conduct an examination of the fuel selector system fitted to NMQ before the aircraft was returned to service.

Background

The then Civil Aviation Authority of Australia issued Civil Aviation Advisory Publication No: 234-1 (0) in March 1991. It provided advice about the quantity of fixed reserve fuel to be carried, and noted the use of fixed reserve fuel was limited to unplanned manoeuvring in the vicinity of the destination aerodrome. It further noted that fixed reserve fuel would normally be retained in the aircraft until the final landing.

The operator's fuel policy stated that in all foreseeable circumstances an aircraft should complete a flight with at least the fixed reserve fuel intact. The standard fixed reserve for the operator's Cessna 402C fleet was 100 lb of fuel for 30 minutes of flight.

Cessna 402C Fuel Selector System

The two fuel selector controls are attached to the cabin floor between the pilot and co-pilot seats. The selectors enable the fuel selector valves, located behind the engine firewalls, to be positioned to the corresponding tank, crossfeed, or off. The arrow-shaped ends of the selector control handle points to the position on the selector placard that corresponds to the control valve position. Each handle connects directly to a gearbox located under the floor. Cables connect each gearbox to their respective fuel selector valve.

An inspection by the maintenance provider in Darwin confirmed that the pilot had positioned the right fuel selector handle to the right tank. However, the cable connecting the gearbox to the fuel selector valve did not position the valve to the right tank.

The right fuel selector gearbox was removed, the selector gearing adjusted and the selector cable re-rigged. The aircraft was returned to service after the fuel selector system was ground tested.

The Pilot's Operating Handbook for the aircraft contained a description of the fuel system and it's operation. In the Normal Procedures section of the handbook, pilots were cautioned that they should "Feel for (the) detent" when placing the fuel selector at the desired position.

Maintenance action

The operator's maintenance controller was located at Alice Springs. A sub-contract maintenance provider conducted maintenance at Darwin. The operator's maintenance controller was not advised of the occurrence until 23 May, and was therefore unable to specify extra inspection procedures for the operator's Cessna 402C fleet until that time. The maintenance controller issued maintenance alert MA/C400/2 on 25 May. It was applicable to all Cessna 402C aircraft used by the operator and its associate company, and required a detailed inspection of the fuel selector system. These checks were to be conducted at each scheduled inspection until the requirements were included in the operator's System of Maintenance.

During one such check of the fuel selector system on another of the company aircraft, VH-TZH, the screws securing the selector cable lever arm/travel stop to the sector gear were found to be loose. This allowed the travel stop to slide under the base-plate and the sector gear to move beyond the end of its travel, resulting in loss of synchronisation between the selector handle and the selector valve.

The operator immediately issued an amendment to maintenance alert MA/C400/2 that included photographs of the defective fuel selector on TZH. The alert specified that the selector gearbox was to be checked if the fuel selector valve was found not synchronised with the selector indicator. During the investigation the fuel selectors of two other of the operator's Cessna 402C aircraft were found to lack an effective detent.

At the time of the occurrence, the maintenance release for NMQ contained an annotation arising from a previous report of uneven fuel consumption from the left tank. Examination of the fuel system related maintenance documentation for the aircraft revealed 17 events since December 1999. Seven involved reports of the aircraft using more fuel from the left tank than the right when the fuel selectors were correctly positioned. There was one report of greater fuel usage from the right tank. The rectification section for four of the entries stated that the fuel selector system was re-rigged. The reported defect for three of the entries was annotated "not major defect" and transferred to the deferred defects list. The fuel related defect entry for the 18 April 2000 stated "fuel not feeding correctly. Fuel noted to be crossfeeding some fuel in level flight - report further".

The last reference to fuel transfer problems, prior to the incident, was on 20 April. The endorsement on the trip record stated "both engines draw fuel from the left tank only". The rectification section of the record noted the fuel selector valve was removed, lubricated, refitted and pressure tested. The selector cable was re-rigged, and the system operated satisfactorily during ground testing.

Fuel system pre-flight checks

The fuel system pre-flight checks specified in the operator's Cessna 402C Operations Manual differed from the procedures specified in the manufacturer's Pilot's Operating Handbook.

The operator's standard operating procedures required pilots to operate the fuel supply cross feed for 60 seconds to verify normal operation. Also, pilots were to ensure normal operation of the fuel valves by positioning the fuel selectors to the off position to observe a decrease in fuel flow. Following these checks, pilots were to position the fuel selectors to the main tanks.

The manufacturer's Pilot's Operating Handbook did not specify checks for crossfeed operation or positioning the fuel selectors to the off position to observe a decrease in fuel flow.

The pilot did not move the fuel selectors to the off position as part of the pre-flight checks. This was because the Fleet Manager had advised his intention to amend the pre-flight check to delete the requirement. The pilot reported awareness of the need to feel for the detent when moving the fuel selectors, and was confident the detent was achieved during the pre-flight check.

On 16 May the operator issued a memo on the occurrence to its Cessna 402 pilots, and included new instructions for pre-flight operation of the fuel selector. The memo cancelled the previous requirement for pilots to position the fuel selectors to the off position to confirm a decrease in fuel flow.

Occurrence summary

Investigation number 200001827
Occurrence date 05/05/2000
Location Darwin, Aero.
State Northern Territory
Report release date 23/05/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fuel starvation
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Cessna Aircraft Company
Model 402
Registration VH-NMQ
Serial number 402C0451
Sector Piston
Operation type Air Transport Low Capacity
Departure point Tindal, NT
Destination Darwin, NT
Damage Nil

Piper PA-31, VH-FMU

Summary

The pilot was tasked to convey six passengers from Brisbane to Miamba, about 165 NM WNW of Brisbane, and return. The aircraft was parked at Archerfield and the passengers were to be picked up at Brisbane Airport.

The aircraft operator had no formal system of recording the amount of fuel remaining in the aircraft at the end of each flight. Normally, the fuel state was discussed between the pilots of the previous and next flights. In this instance, however, the pilot did not speak to the person who last flew the aircraft. The pilot said that it was his practice to use the fuel gauges and the fuel gauge calibration chart to determine the amount of fuel in the aircraft.

The weather forecast obtained by the pilot indicated the 7,000 ft wind as 110 degrees at 15 kts, and the 5,000 ft wind as 120 degrees at 20 kts. The pilot calculated the following flight times and fuel requirements for the intended flights, assuming a fuel consumption rate of 140 lt per hour:

Archerfield - Brisbane 5 mins, 27 lt
Brisbane - Miamba 59 mins, 174 lt
Miamba - Brisbane 59 mins, 174 lt
Total 123 mins, 375 lt

Before the flight, the pilot obtained information about the destination airstrip and decided to have the aircraft refuelled to full main tanks (415 lt). The fuel gauges for the auxiliary tanks were indicating half full. Using the lesser of the aircraft flight manual and the fuel calibration card figures, the pilot assessed that the auxiliary tanks contained 147 lt. From this information, he calculated that the aircraft contained 562 lt of fuel - sufficient for about 4 hours of flight.

Because of air traffic control requirements and the prevailing weather conditions, the flight from Archerfield to Brisbane took about 30 minutes.

During the flight to Miamba, the pilot selected the auxiliary tanks for a period during cruise at 8,000 ft, but did not record the times when these selections were made. Flight duration was about 66 mins.

At Miamba, the pilot estimated (from the fuel gauges) that there was 280 lt fuel remaining for the return flight to Brisbane. At top of climb (7,000 ft) he again selected the auxiliary tanks. Because the gauge indications reduced faster than he anticipated towards empty, he allowed the auxiliary tanks to empty before re-selecting the main tanks. The pilot said that the fuel quantity gauges indicated about 1/8 when the auxiliary tanks were empty. Because of headwinds, the pilot descended to 5,000 ft to try to achieve a higher ground speed but to little effect. At that altitude, the aircraft was in cloud.

At about 30 nm from Brisbane, with the gauges indicating about 1/8, the pilot became concerned that there might not be sufficient fuel to complete the flight to Brisbane. He descended to 4,000 ft, again seeking a better ground speed. The pilot then elected to divert to Archerfield (which was closer) and told air traffic control that he did not wish to descend further until close to Archerfield. Shortly after being cleared to turn towards Archerfield, the left engine surged and then ceased operating. The pilot feathered the propeller and informed air traffic control that he required an immediate landing at Amberley. He did not declare an emergency.

Soon after the left engine failed, the aircraft flew clear of cloud and the pilot saw Amberley aerodrome. He conducted a straight-in approach to runway 15 at Amberley. He manually extended the landing gear with assistance from the passenger in the right control seat. The aircraft touched down about 5,000 ft along the runway and the pilot deliberately steered the aircraft off the runway edge on to grass late in the landing roll. There was no damage to the aircraft. The flight from Miamba had taken about 84 minutes. After refuelling, the engines operated normally.

Investigation revealed that the aircraft actually contained about 477 lt on start-up at Archerfield - 85 lt less than the pilot believed. That included 220 lt remaining from the previous flight, and 257 lt added during refuel. The aircraft operator said that his company used a rate of 150 lt per hour for flight planning purposes. Based on that figure, there was sufficient fuel on board the aircraft for about 190 minutes flight. From the total flight time of about 180 minutes, the aircraft had achieved an actual fuel usage rate of about153 lt per hour (allowing about 30 minutes ground operating time), close to the planning figure used by the operator. It is logical to conclude, therefore, that the engines performed normally during the flight, and that the fuel supply to the left engine was exhausted, causing it to cease operating. It is likely that the fuel supply to the right engine would also have been exhausted within a few minutes if the pilot had not shut the engine down.

The pilot said that, based on the handling notes for the aircraft, 126 lt fuel per hour would be consumed at 65 per cent engine power (31 inches MAP and 2,200 rpm). He had used a rate of 140 lt per hour in planning for the flight, which he considered more than adequate. Although the pilot's aeronautical experience was significant, over 90 percent of it was as a flying instructor on single engine aircraft. The pilot had little experience in charter operations. His experience on the aircraft type was also low.

Occurrence summary

Investigation number 200002018
Occurrence date 23/05/2000
Location 31 km N Amberley, (NDB)
State Queensland
Report release date 01/06/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fuel exhaustion
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Piper Aircraft Corp
Model PA-31
Registration VH-FMU
Serial number 31-8212015
Sector Piston
Operation type Charter
Departure point Miamba, QLD
Destination Brisbane, QLD
Damage Nil

Fairchild SA227-AC, VH-IAW

Safety Action

As a result of the investigation into this and related occurrences, the Australian Transport Safety Bureau is currently investigating a safety deficiency involving the Fairchild SA-226/SA-227 type of aircraft that relates to replacement of certain hydraulic piping and ongoing inspection procedures for the hydraulic piping.

Any safety output issued, as a result of this analysis will be published in the Bureau's Quarterly Safety Deficiency Report.

Summary

The crew of the Fairchild Metroliner was conducting endorsement training in the Cowra area when they advised air traffic services (ATS) that their aircraft had a hydraulic failure and they were returning to Bankstown. An uncertainty phase was declared by ATS and the aircraft returned to Bankstown where a flapless landing was carried out.

The subsequent maintenance inspection found a cracked hydraulic pipe in the left landing gear wheel-well that had allowed the loss of the hydraulic oil contents from the power pack. The crack was in the bend radius of the pipe and was not visible to the naked eye. The crack only became apparent with the application of more than 800 psi of hydraulic pressure to the system during the maintenance inspection. The pipe was changed and the aircraft returned to service.

The pilot in command reported that he had experienced two similar hydraulic pipe failures in this aircraft type and the company fleet had five or six similar failures in the preceding twelve months. He also reported that he had a concern that the escaping oil in this situation could have started a wheel-well fire.

The design of the hydraulic system is such that, when a failure occurs in one of these hydraulic pipes, there is no redundancy. As a result, the leak drains the contents from the hydraulic reservoir, which is the common source of hydraulic fluid for both the left and right engine-driven hydraulic pumps. Without hydraulic services, nosewheel steering, anti-skid braking, flap operation and normal landing gear retraction and extension would not be available to the pilot.

Occurrence summary

Investigation number 200001657
Occurrence date 10/05/2000
Location 1 km S Cowra
State New South Wales
Report release date 02/04/2000
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Hydraulic
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Fairchild Industries Inc
Model SA227
Registration VH-IAW
Serial number AC-600
Sector Turboprop
Operation type Air Transport Low Capacity
Departure point Cowra, NSW
Destination Cowra, NSW
Damage Nil

Boeing 767-338ER, VH-OGA

Summary

On final approach to land at Auckland, the crew of the Boeing 767 observed the right alternating current (AC) electrical bus fail indication. The crew started the auxiliary power unit (APU) to supply additional electrical power and the approach and landing were completed without further incident. The non-normal checklist was actioned on the ground and the right AC bus power was restored. The customer service manager later advised the pilot in command that the emergency lighting illuminated briefly during the failure but then went out. This left the cabin in total darkness throughout the incident until right AC power was restored.

Maintenance investigation could not fault the electrical systems during ground tests. It is likely that there may have been an electrical earth occurring in the right generator feeder wires or terminal. The right generator control unit (GCU) would then have isolated the right generator, leaving the right AC bus without power. A fault would then be automatically detected in either the current to or from the right AC bus and the right bus tie breaker (BTB) would remain open. This would ensure the right AC bus was isolated and could not be powered by the left engine generator. The APU generator came on-line just before touchdown and automatically powered the right AC bus, however not all the engine indicating and crew alerting system (EICAS) messages were cleared with the APU powering the right AC bus. The messages cleared when the non-normal checklist was completed.

On this production series B767 aircraft, if power to the right AC bus fails then all cabin lighting is extinguished. On later production series B767, the left AC bus supplies cabin side wall lighting and the right AC bus supplies cabin overhead lighting, therefore there is some cabin lighting if either AC bus fails.

When the right AC bus lost power so too did the right direct current (DC) bus. However, as no faults were sensed in the DC electrical system the DC tie relay automatically closed to power the right DC bus from left DC bus. This sequence normally takes 11.5 seconds. The emergency lighting circuit, sensing initially there was no DC electrical power, momentarily activated while electrical system switching took place (the 11.5-second changeover). Once the DC tie relay closed the right DC bus became powered by the left DC bus and the emergency lighting then automatically extinguished. The emergency lights are designed not to light up continuously unless all DC electrical power is lost.

As no definite fault could be isolated for the right AC bus failure, the performance of the aircraft electrical system was being monitored by Engineering Maintenance Watch and the company Flight Safety Department

Occurrence summary

Investigation number 200001647
Occurrence date 10/05/2000
Location Auckland, ILS
State International
Report release date 01/08/2000
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer The Boeing Company
Model 767
Registration VH-OGA
Serial number 24146
Sector Jet
Operation type Air Transport High Capacity
Departure point Sydney, NSW
Destination Auckland, NEW ZEALAND
Damage Nil

Piper PA-34-220T, VH-YSG

Significant Factors

  1. The pilot's fuel planning was based on incorrect fuel content and weight considerations.
  2. The pilot did not include the Sydney Harbour scenic flight in his flight planning.
  3. The pilot diverted from the recommended in-flight fuel management practices.



 

Analysis

The aircraft had been assessed as having 280 L of fuel on board prior to departure from Canberra, based upon the delivery pilot's calculation. ATSB calculations, using the operator's own fuel planning figures, indicated that the amount of fuel consumed during the 1.8 hour delivery flight from Tamworth would likely have equated to a fuel remaining figure of approximately 265 L. In addition, no allowance was able to be determined for the amount of fuel consumed during the engine ground runs at Tamworth, between the time of the last recorded refuel and the delivery flight. Accordingly, the actual fuel tank contents on departure from Tamworth for the delivery flight could not be accurately determined and would probably have been an amount less than the maximum useable.

While planning for the accident flight utilising a computer-based application, the pilot used an incorrect figure (465 L) with respect to total versus useable fuel tank contents (454 L). That led the pilot to include 11 L of fuel, which was unavailable for engine consumption. In addition, he omitted to plan an allowance for fuel consumption during the approximately 12-minute Sydney Harbour scenic flight. Using the operator's fuel consumption planning figure, this may have involved consumption of up to 20 L of additional fuel.

The pilot's use of the computer-based flight planning application included calculations for aircraft weight and balance. His utilisation of the full fuel planning figure in these calculations, instead of the assessed fuel load figure of 280 L, may have led to an erroneous perception that he would be overweight following embarkation of the five passengers at Bankstown, if he added fuel prior to take-off from either Bankstown or Canberra. Had the pilot used the assessed fuel tank content figure, he would have realised that he could have added fuel and remained within aircraft weight limitations.

The manufacturer's fuel usage figures are determined using a recommended technique for leaning of the fuel mixture supplied to the engines. During the accident flight, the pilot deviated from the recommended technique. That deviation would likely have increased the engine fuel consumption.

Technical investigation of the right engine indicated that it was capable of normal operation. Examination of the left engine indicated that it should still have supplied at least partial power in flight. The failure mode of the exhaust valve rocker stud and the bending of the inlet valve pushrod were examined in consultation with a representative of the engine manufacturer and engine overhaul specialists. Although an exact reason for the failure could not be determined, it is possible that the damage may have occurred following the loosening of one or both of the rocker pivot retaining nuts. As the nut(s) loosened during engine operation, the exhaust valve rocker would have lifted, preventing the exhaust valve from opening. During the valve overlap stage of the engine operating cycle, prior to the start of the induction stroke, the ignited and expanding combustion gasses may have been unable to escape through a now closed exhaust valve. That scenario would have greatly increased internal cylinder pressure which could have prevented the inlet valve opening and, consequently, resulted in the bending of the inlet valve push rod as it tried to move the valve. The damage to the inlet valve pushrod was also considered to have been consistent with the rotation of the engine with a "hydraulic lock" situation existing in the cylinder. Such a condition may occur in the cylinder if the engine was over primed prior to an engine start.

It is likely that the engine failures occurred as a result of fuel exhaustion.

Factual Information

The Piper PA34 Seneca III, took off from Canberra for Bankstown under the Visual Flight Rules (VFR). The pilot in command had planned to embark five passengers at Bankstown then to conduct a scenic flight around Sydney Harbour, proceed to Cessnock for lunch and return to Bankstown where he intended to disembark the passengers before returning to Canberra.

The flight to Bankstown was uneventful. On departure from Bankstown, the pilot proceeded southeast to the coast and then north, at low level, along the VFR coastal route to Manly. A delay was experienced at Manly, prior to turning south and entering Sydney Harbour. The Sydney Harbour scenic flight was then conducted, completing a circuit of the Harbour Bridge to Rushcutter's Bay loop. The pilot then returned to South Head and proceeded north via Aeropelican for a landing at Cessnock.

During the return flight, the pilot deviated west of the planned track in order to avoid severe weather that had been indicated on the aircraft's weather radar. Shortly after passing Brooklyn Bridge, which was the start point for the northern inbound VFR track to Bankstown, at an altitude of 2,500 ft, the pilot reported that the left engine suddenly stopped. The pilot reported that he then carried out the engine failure checks from memory, feathering the propeller. Approximately one minute later, the right engine began to gradually lose power, before stopping after approximately a further 20 seconds. The pilot reported that he then pushed all of the engine and propeller controls forward and attempted to restart the engines. That action resulted in the inadvertent unfeathering of the left propeller due to operation of the unfeathering accumulator.

The pilot conducted a forced landing into a treed area beside a main road. The aircraft struck the trees, rotated to the right and impacted the ground left wing forward. Four of the six occupants sustained serious injuries and the aircraft was destroyed.

Pilot information

The pilot was appropriately licensed for the flight and had accumulated a total of 270 hours flying experience with 14 hours on the aircraft type.

Flight and fuel planning

The aircraft arrived on the operator's flight line five days before the accident, after delivery from Tamworth. The technical log indicated that the last recorded refuel had been conducted at Tamworth on 13 March 2000. Between that time and the delivery flight to Canberra the aircraft had undergone a 15-minute dual engine run following a propeller change. The engine run included a period of one to one and a half minutes with both engines at full power. Prior to departure from Tamworth, the delivery pilot reported that he visually assessed the fuel tanks as full. Upon arrival at Canberra, the fuel tank content was assessed as 280 L, using flight time and fuel usage calculations.

The pilot planned the accident flight utilising a computer-based flight planning application. He did not plan for any aerial work at Sydney Harbour, despite having an intention to conduct a scenic flight in that location. Air Traffic Services (ATS) radar data indicated that the scenic flight duration was approximately 12 minutes. In addition, he planned the flight using figures for full fuel tanks, however he used the total fuel tank content figure of 465 L instead of the useable fuel tank content figure of 454 L. Further, he was aware that the aircraft had only an assessed 280 L of fuel on board and considered that that amount was sufficient for the flight from Canberra to Cessnock and for the return flight to Bankstown. He had decided not to add fuel prior to departure from Canberra due to a perception that the aircraft would be over Maximum Take-off Weight at Bankstown or Maximum Landing Weight at Cessnock, after the addition of the five passengers.

Fuel management

The pilot reported that he visually checked the fuel tank contents at Canberra before departure, with fuel just visible through the fuel cap opening. That quantity was then cross-checked with the aircraft fuel gauges and it appeared to agree with the previously calculated total. An attempt was also made to check the fuel tank contents using the aircraft's fuel dipstick, however, that was unsuccessful as the fuel level was well below the lowest graduated scale on the stick. The pilot reported that he again checked the fuel level on arrival at Bankstown. At that time the level was out of sight of the fuel caps, however, the total fuel remaining on the fuel gauges appeared to agree with his assessment. Prior to landing at Cessnock the fuel gauges were again checked, with the pilot considering that the indicated fuel level was what he expected from his mental calculations to allow for the return flight to Bankstown.

ATS radar data indicated a total flight time of 159 minutes from take-off at Canberra to the accident site. That figure did not include any allowance for ground taxi at Canberra, Bankstown and Cessnock. Using the operator's recommended fuel usage planning figure of 100 L per hour, 159 minutes flight time would have consumed 265 L of fuel.

The aircraft manufacturer's recommended engine fuel leaning procedure for cruise flight was detailed in Section 4 (Normal Procedures) of the Pilot's Operating Handbook, which stated:

"For 45, 55 and 65% power the mixture should be leaned to 25 [degrees] F rich of peak E.G.T. [Exhaust Gas Temperature] but not to exceed 1,650 [degrees] F E.G.T.", and "For maximum engine service life, cylinder head temperatures should be maintained below 420 [degrees] F..."

The pilot reported that he had been taught to lean the fuel mixture to the top of the green arc on the exhaust gas temperature gauge. The green arc on the gauge extended from 1,200 to 1,525 degrees F. He reported that during the accident flight he leaned the mixture according to that method, however he had subsequently enriched the mixture one or two graduations below the top of the green arc. Advice from the aircraft manufacturer and other Seneca III operators, indicated that that action may have increased the fuel flow by up to approximately 10 L per hour.

Approximately one litre of fuel was recovered from the aircraft wing tanks, however the fuel tanks had been substantially damaged during the impact sequence. There was no evidence of fuel leakage on the ground. Inspection of the fuel system components revealed no evidence of fuel contamination. The left engine fuel selector control was positioned at the OFF position and the right engine selector was positioned at ON.

Engine and fuel system information

Both engines had recently been overhauled and had flown 57.3 hours since fitment to the aircraft.

During the flight, a short time after passing Aeropelican, the pilot reported that the left engine had required increased throttle to maintain the selected manifold pressure. While taxying after landing at Cessnock the left engine appeared to idle slower than before and the alternator light flickered on and off. The light had extinguished when the pilot increased engine RPM. After vacating the aircraft, the pilot noticed evidence of an oil leak along the outboard side of the left engine cowling, on the underside of the left wing and on the left flap. A check of the left engine oil quantity revealed that the engine had used about half a quart during the flight. Confirmation with the operator by telephone indicated that the oil level was within tolerances. The source of the oil leak was not able to be located. The pilot reported that operation of both engines from departure at Cessnock to the point of engine failure appeared normal.

Technical investigation at the accident site revealed that the left engine number 4 cylinder exhaust rocker pivot was loose and that the rocker had contacted and holed the inside surface of the rocker cover. The forward rocker pivot-retaining stud had sheared flush with the surface of the head with evidence of a fatigue failure on the stud fracture surface. The number 4 cylinder inlet valve push rod had also failed close to the outboard tip of the rod. Detailed technical examination of both engines at an engine overhaul facility noted that the exhaust valve on the number 4 cylinder of the left engine remained closed during rotation of the crankshaft and the inlet valve on the same cylinder only opened a small amount. Both engines were then test run in an engine test cell. The test run of the right engine revealed no condition that would have contributed to the in-flight loss of power. The test run of the left engine indicated that it was capable of operation, however it's performance was affected by the damage evident on the number 4 cylinder's valve mechanism.

Occurrence summary

Investigation number 200001434
Occurrence date 25/04/2000
Location 13 km S Brooklyn Bridge, (VTC Check Point)
State New South Wales
Report release date 10/04/2002
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fuel exhaustion
Occurrence class Accident
Highest injury level Serious

Aircraft details

Manufacturer Piper Aircraft Corp
Model PA-34
Registration VH-YSG
Serial number 34-48020
Sector Piston
Operation type Private
Departure point Cessnock, NSW
Destination Bankstown, NSW
Damage Destroyed

Boeing 737-476, VH-TJY

Summary

While on final approach to Brisbane at about 1,000 ft, the crew of the Boeing 737 reported feeling a 'kick' in the rudder pedals accompanied by a minor aircraft yaw oscillation. It was reported that there was no aircraft ahead to cause wake turbulence.

Investigation by the aircraft operator suggested a problem with the rudder power control unit. The aircraft manufacturer recommended that the standby rudder actuator and the standby input rod bearings should also be examined for wear; no wear was evident.

The rudder power control unit had accumulated 3,064 hours since its overhaul by the manufacturer in May 1999. It was removed from the aircraft and forwarded to the USA for examination.

The examination was conducted by the component manufacturer and supervised by the National Transportation Safety Board of the USA on behalf of the Australian Transport Safety Bureau. No discrepancies that may have led to the anomaly in the operation of the rudder power control unit were found. The internal and external components contained no evidence of excessive wear, damage or overtravel and met the manufacturer's standards for in-service units.

In support of the investigation, the National Transportation Safety Board also conducted a performance simulation study based on the actual aircraft configuration data at the time of the incident. The study concluded that the rudder had oscillated.

The investigation was unable to determine why the rudder reportedly oscillated.

Occurrence summary

Investigation number 200001362
Occurrence date 18/04/2000
Location Brisbane, Outer Marker
State Queensland
Report release date 06/02/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Flight control systems
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer The Boeing Company
Model 737
Registration VH-TJY
Serial number 28151
Sector Jet
Operation type Air Transport High Capacity
Departure point Melbourne, VIC
Destination Brisbane, QLD
Damage Nil

Boeing 767-338ER, VH-OGS

Summary

The position of the Boeing 767 was displayed incorrectly on the Brisbane sector controller's Air Situation Display (ASD). The aircraft passed ATMAP at 0404 Coordinated Universal Time and was estimating Curtin at 0503. At 0404 the aircraft was displayed on the ASD just south of Bali with an estimate for Bali of 0404. Bali ATC had previously advised Brisbane ATC that the aircraft was estimating ATMAP at 0404. As the aircraft was not within radar coverage and not fitted with Automatic Dependant Surveillance equipment, the ASD displayed the aircraft position consistent with the input data, not the aircraft's actual position.

The investigation revealed that the controller had used the electronic strip intending to enter the time of 0404 for ATMAP, but instead entered 0404 as the time overhead Bali.

There was no infringement of separation standards.

Occurrence summary

Investigation number 200000933
Occurrence date 02/03/2000
Location Atmap, (IFR)
State International
Report release date 25/07/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category ANSP info/procedural error
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer The Boeing Company
Model 767
Registration VH-OGS
Serial number 28725
Sector Jet
Operation type Air Transport High Capacity
Departure point Singapore
Destination Sydney, NSW
Damage Nil

Cessna 172M, VH-SXK

Analysis

The flight to Shepparton appears to have proceeded normally up to and including the circuit entry for runway 18. It is not possible to precisely describe the wind affecting the aircraft during the attempted landing. However, the crosswind component was probably about 7-15 knots and the tailwind component about 5-12 knots.

The go-around was commenced at a late stage as the aircraft was approaching the trees at the far end of the aerodrome. Due to the late decision to go-around, the pilot was possibly distracted by the need to avoid the trees. The airspeed was low and the pilot may have been experiencing difficulty with climb performance.

The reason for the sharp left turn could not be determined. That turn resulted in the aircraft flying downwind with a reduced climb angle performance and decaying airspeed as the pilot tried to increase height. At which stage the flaps were retracted remains unknown, but fully retracting the flaps at such a low level would have seriously degraded the aircraft's immediate climb performance.

Retracting flap with a high nose attitude probably reduced the aircraft's speed such that the wings stalled at a height that was insufficient to allow recovery before the aircraft impacted the ground.

Summary

The pilot of a Cessna 172M was conducting a private visual flight rules (VFR) flight, with two passengers, from Narromine to Shepparton. The passenger seated next to the pilot was also a qualified private pilot and the owner of the aircraft.

On arrival at Shepparton, the aircraft overflew the aerodrome. After noting from the aerodrome windsock that the wind was a moderate westerly, the pilot decided to use runway 18 for landing. The owner of the aircraft observed that the aircraft was high on the base leg and on final approach. He remarked that the pilot was having difficulty with the crosswind conditions, since the aircraft was drifting left during the landing attempt.

Witnesses noticed from several locations around the aerodrome that the aircraft was flying erratically 3 or 4 metres above the level of the runway, with a pronounced nose-up attitude. It was flying slowly and making apparently repeated attempts to touch down on the runway. Its height was varying slightly and its wings were rocking from side to side. This was confirmed by the pilot of a following aircraft who noticed that the Cessna 172 was only a few metres above ground level, three-quarters of the way down the runway and drifting out across the grass to the eastern side of the runway. A second witness, who was a private pilot endorsed on Cessna aircraft, reported seeing some flap but could not remember how much.

A go-around from the attempted landing was commenced as the aircraft neared the end of runway 18. The aircraft continued south beyond the runway, drifting east with the wind and out over the boundary fence at the southern end of the aerodrome. The witnesses feared that the aircraft would not clear a line of trees, approximately 20 metres tall, running approximately east-west beyond the aerodrome boundary. The aircraft then turned to the left while banking sharply and tracked eastwards at very low altitude with its wings rocking and a pronounced nose-high attitude. Its nose then suddenly dropped and it adopted a steep nose-down attitude before impacting the ground. Witnesses attended to the seriously injured occupants while waiting for the local emergency services to arrive. The pilot died in hospital from his injuries.

The owner, who had flown regularly with the pilot, said he was very meticulous with his procedures and that his late decision to go around was out of character. The owner only vaguely remembered the go-around procedure but said he believed that the pilot's actions were standard.

The aircraft came to rest in an open field about 600 metres south of the departure end of runway 18. Ground scars and propeller slash marks showed that the aircraft had impacted in a steep, nose-down, almost wings-level attitude with little forward velocity. It had then bounced about 9 metres to the south-east, where it came to rest. Impact forces severely disrupted the forward section of the fuselage. Post-accident inspection of the airframe indicated that it was intact when it struck the ground.

Approximately 25 litres of clean avgas was drained from each fuel tank 2 days after the accident. Tests revealed no indication of fuel contamination. The weight and balance of the aircraft was calculated to be within limits for landing at Shepparton.

No defects or deficiencies were identified with the aircraft engine or the aircraft's systems that may have compromised its performance or contributed to the accident. The flaps were in the fully retracted position when the aircraft struck the ground and this was verified by the position of the flap position actuator. Damage to the propeller and the ground slash marks made by the propeller at the impact point indicated that the engine was under power at the time of impact. Several witnesses described the engine sound as being normal for an engine at high power.

The Bureau of Meteorology had installed an Automatic Weather Station (AWS) at Shepparton aerodrome. The AWS provided 1-minute averaged data for wind direction and speed and automatically recorded the data for future reference. At the time of the accident the surface wind, as measured by the AWS, was 310 degrees at 9 knots, with a maximum gust within the previous 10 minutes of 20 knots. An experienced private pilot who was flying his aircraft in the Shepparton circuit area at the time of the accident described the wind as a moderate westerly of approximately 15 knots. He noted that he experienced a combination of both mechanical and thermal turbulence, particularly at low level.

With the wind from the west and a turn to the east from a runway heading of 180 degrees, the aircraft will drift downwind while turning. This can create visual illusions that may result in mishandling of the flight controls which, combined with turbulence and wind gusts, may result in height loss, particularly if the aircraft is operating at a high angle of attack.

Occurrence summary

Investigation number 200001153
Occurrence date 03/04/2000
Location Shepparton, Aero.
State Victoria
Report release date 24/07/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Collision with terrain
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Cessna Aircraft Company
Model 172
Registration VH-SXK
Serial number 17267571
Sector Piston
Operation type Private
Departure point Narromine, NSW
Destination Shepparton, VIC
Damage Destroyed

Embraer EMB-110P1, VH-UQD

Safety Action

The maintenance organisation has indicated that it will ensure that the sealant on the fire detection sensors is adequate to seal against moisture ingestion.

Summary

During descent into Cairns, the pilot of the Embraer EMB-110 observed the right engine fire warning annunciator illuminate. The pilot then conducted the quick reference handbook `fire during flight phase' checks, which included shutting down the right engine. During these checks the fire warning annunciator extinguished, and as there was no visual indication of fire or smoke, the pilot elected not to discharge the engine fire bottle. The quick reference handbook allows for an 8-second wait after the engine is shut down. If the fire warning persists then the fire extinguisher should be discharged. The pilot advised Air Traffic Control and the aircraft passengers of the engine shutdown. An uneventful single engine approach and landing was successfully completed.

The engine fire detection system consists of two independent circuits for each engine. The sensors are located in the hot section, accessories section and the generator cooling air discharge, and are connected to a control box. When a fire or overheat condition is detected a fire warning light will illuminate in the T handle for the affected engine, the master caution light will illuminate, and the fire horn will sound.

Investigation by the operator's maintenance organisation found that three fire detector sensors had failed, resulting in a false fire warning. The failed sensors were found to contain moisture. The operator indicated that the aircraft had operated in rain shortly before the incident flight.

Occurrence summary

Investigation number 200001335
Occurrence date 19/04/2000
Location 52 km W Cairns, Aero.
State Queensland
Report release date 30/04/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Embraer-Empresa Brasileira De Aeronautica
Model EMB-110
Registration VH-UQD
Serial number 110-208
Sector Turboprop
Operation type Air Transport Low Capacity
Departure point Normanton, QLD
Destination Cairns, QLD
Damage Nil