Bell 206L-3, VH-CKP, Tartrus Station, Queensland

Summary

In preparing the aircraft for the next flight, the pilot turned on the valve for the medical oxygen system. Witnesses then heard a loud bang and gas escaping as the pilot was thrown clear of the aircraft, which caught fire and burned. The pilot received significant ear and chest injuries in the blast.

The Bureau recommends that the Civil Aviation Safety Authority:
(i) conduct an audit of all emergency medical service oxygen-equipped aircraft to determine the equipment standards in Australian registered aircraft;
(ii) issue design standards for emergency medical service oxygen equipment installations;
(iii) issue maintenance requirements for emergency medical service oxygen equipment;
(iv) provide surveillance requirements for emergency medical service oxygen equipment in the Aviation Safety Surveillance Program;
(v) ensure flight crew are provided with appropriate instructions in the use of emergency medical service oxygen equipment in aircraft flight manuals or company operations manuals; and
(vi) provide educational material to the aviation industry on the installation, operation and maintenance requirements of emergency medical service oxygen systems.'

Occurrence summary

Investigation number 199701421
Occurrence date 02/05/1997
Location Tartrus, (ALA)
State Queensland
Report release date 08/09/1998
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fire
Occurrence class Accident
Highest injury level Serious

Aircraft details

Manufacturer Bell Helicopter Co
Model 206
Registration VH-CKP
Serial number 51373
Sector Helicopter
Operation type Aerial Work
Departure point Tartrus Station, QLD
Destination Rockhampton, QLD
Damage Destroyed

Boeing 747-300, N124KK

Safety Action

As a result of the investigation, the Bureau of Air Safety Investigation issued recommendation R970128, to Qantas and Ansett on 29 September 1997. The recommendation stated:

"The Bureau of Air Safety Investigation recommends that Australian operators of aircraft manufactured by the Boeing Commercial Airplane Company:

  1. develop a simulator training procedure to ensure that aircrew are familiar with the procedures to be used in the event of lateral control jamming; and
  2. ensure that aircrew are aware of the control wheel forces required when the override mechanism is being operated in the event of jammed lateral controls".

A similar recommendation (R970145) was issued to the Boeing Commercial Airplane Company on 29 September 1997.

The following response was received from Qantas on 26 November 1997:

"I refer to your letter reference B97/099 which detailed a recommendation that a simulator training procedure be developed to ensure that all aircrew are aware of the procedure to be used, and control forces required, in the event of aileron control jamming.

Qantas simulators (with the exception of the B767-200 simulator) are equipped to simulate aileron control jamming and the control wheel forces required to override and regain control.

This scenario will be made a subject, both for discussion and demonstration, in the first available recurrent training simulator session. This will apply to the Boeing 747-400, 747-200/300, 767, 737 and Airbus A300 fleets".

Response classification: CLOSED - ACCEPTED.

The following response was received from Ansett on 24 June 1998:

"I refer to the above recommendation, which resulted from an incident involving a Boeing 747 aircraft at Sydney on 2 May 1997, and provide the following response to that recommendation.

The company conducts ground training for technical crews that includes instruction on aileron control jamming procedures. Additionally, simulator training is presently conducted for Boeing 737 aircraft and will be conducted in the Boeing 767 simulator when that simulator is upgraded to allow such training. For the Boeing 747, training is conducted in the aircraft, whilst on the ground, during type endorsement".

Response classification: CLOSED - ACCEPTED.

The following response was received from the Boeing Commercial Aeroplane Company on 13 February 1998:

"We have not yet committed any changes in our simulator training procedures or manuals. We are reviewing the reported event and looking at possible training and manual changes which would be implemented for all applicable Boeing models, not just 747.

However, additional time is necessary for this review before we can come to any conclusion. I anticipate that this review may take three more months. We plan to keep your office advised of the progress of our review".

A further response was received on 27 May 1998, and stated:

"Earlier this month I reviewed proposed changes to our operational documentation concerning flight control jams across all our various model airplanes. This has been a slow process trying to get agreement on. I anticipate that we will have some changes to be released in a couple of months. These changes would affect the Flight Manual, the Flight Crew Training Manual, the Operations Manual and the QRH".

Response classification: OPEN.

Local safety action

Boeing have also advised that Service Letter 747-SL-27-134, which addresses the need to replace deteriorated cable guards, is to be upgraded to service bulletin status in the near future to add more emphasis to this discrepancy.

Significant Factors

  1. The aircraft maintenance organisation had not replaced deteriorated parts with improved parts as suggested by the aircraft manufacturer.
  2. A cable guard had deteriorated to the extent that it failed and resulted in high control forces in the lateral control system.
  3. The operating crew were not aware of the high control inputs required to overcome the load limiter in the lateral control system.

Analysis

The deteriorated condition of the plastic cable guards, and the use of tape to effect a "repair", suggests that the manufacturer's advice regarding replacement of the guards had not been heeded during major maintenance inspections.

It is likely that, when the plastic cable guard failed, a piece or pieces of plastic lodged in the left side cable run aileron control pulley, restricting the cable movement in one direction. The debris probably dislodged when the aircraft was at about 400 ft on final approach.

Summary

The aircraft was being operated as a scheduled passenger service from Sydney to Seoul, with the co-pilot as the handling pilot. The crew reported that the pre-departure flight control checks were normal. Shortly after becoming airborne from runway 34L, the co-pilot advised the pilot in command (PIC) that his control wheel had become jammed when attempting to make right wing down aileron inputs. The PIC took control of the aircraft and confirmed that his control wheel also had become jammed. He retained control of the aircraft and the co-pilot advised Air Traffic Services (ATS) that the aircraft was unable to turn to the right. He requested left turns and radar vectors to the south for fuel dumping prior to returning to land. ATS initiated a distress phase. The crew actioned the emergency/abnormal checklist for jammed or restricted flight controls, which includes the statement "use maximum force, including a combined effort by both pilots, if required", but they reported that their attempts made no change to the system. After fuel dumping was completed, the aircraft was vectored, using left turns only, to the runway 34L localiser and configured for the landing. At about 400 ft on final approach, the aileron controls became free and an uneventful landing was carried out.

Inspection by ground engineers determined that a plastic cable guard in the left aileron control cable system had broken. Pieces of shattered plastic were found in the vicinity of the left lower cable pulley system in the vertical cable run behind the cabin sidewall, forward of door 1L. The debris and all the remaining guards were removed from both left and right side vertical cable runs. The lateral control system, including the load limiter system, could not be faulted during full system testing. As there were no replacement cable guards available, the aircraft was approved to return to service with the guards removed.

The lateral controls on the aircraft consist of hydraulically powered inboard and outboard ailerons and flight spoilers on each wing. The controls are connected to the cockpit control wheels by cables, for pilot input. The cable runs are duplicated on each side of the aircraft. The left and right cable runs terminate at quadrants at the bases of the left and right control columns respectively. The control columns are interconnected by a cable loop connected to separate quadrants at the bases of the columns. The right quadrant includes a load limiter which consists of a detent and spring-loaded cam assembly. The load limiter is designed to "break away" under applied force by the crew to enable one control wheel to provide lateral control input should the other side jam for any reason. Roll control is then available, but considerable force is required to overcome the detent cam in the load limiter. Other Boeing aircraft types utilise similar systems.

The aircraft manufacturer issued a Service Letter, 747-SL-27-134, in December 1993, advising that broken cable guards could result in high control wheel forces and suggesting that operators should replace the guards with improved parts when replacement is required. The guards on the right control system on the incident aircraft showed evidence of deterioration, as one guard had been previously repaired with adhesive tape.

The aircraft was leased from an overseas operator. Under the terms of the lease agreement, all major maintenance was conducted by the lessor. The last major maintenance inspection was completed on 25 August 1995. At the time of the incident the aircraft total time in service time was 50,400 hours.

The crew remained at the aircraft whilst the defect was rectified. Both crewmembers remarked that they were surprised at the force required to overcome the load limiter when the system was tested. Though they were aware of the load limiting system from ground training instruction, they had never been physically exposed to the forces required to operate the system.

Occurrence summary

Investigation number 199701423
Occurrence date 02/05/1997
Location 5 km N Sydney, Aero.
State New South Wales
Report release date 01/02/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Control - Other
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer The Boeing Company
Model 747
Registration N124KK
Serial number 23244
Sector Jet
Operation type Air Transport High Capacity
Departure point Sydney, NSW
Destination Seoul, ROK
Damage Nil

North American Aviation Inc T-6 MK IV, VH-YES, Tindal Aerodrome, Northern Territory

Summary

The pilot initiated the take-off with 4,500 ft to run on runway 32. Soon after liftoff, the Tower controllers noticed that the aircraft was trailing white smoke. At about 300 ft AGL the aircraft appeared to enter a left descending turn. The left bank increased until the aircraft was almost vertical before it impacted with the ground.

The complete single piece wing structure broke free from the fuselage during the impact. A fire developed in the engine bay which spread to the separated wing structure. The back seat passenger was not seriously injured and was able to extricate himself from the rear cockpit and pull the pilot free of the wreckage.

The pilot did not survive the crash.

Occurrence summary

Investigation number 199700744
Occurrence date 06/03/1997
Location Tindal, Aerodrome
State Northern Territory
Report release date 09/07/1998
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Collision with terrain
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer North American Aviation Inc
Model T-6
Registration VH-YES
Serial number T-6 MK IV, 14482
Sector Piston
Operation type Private
Departure point Tindal, NT
Destination Tindal, NT
Damage Destroyed

Hughes Helicopters 369HS, VH-XAX

Safety Action

The helicopter operator amended the company operations manual Section D8 - Marine Pilot Transfer to more clearly document the procedures already carried out by company pilots flying marine pilot transfers. The amended text reads as follows:

"After landing, while waiting for the marine pilot or after the marine pilot has disembarked, the pilot shall recheck any obstructions, confirm the departure route...etc.

When in the hover, check the centre of gravity, and hover power prior to flying the planned departure. Ships with obstructions require a transition between the obstructions via an over-water final approach and take-off area before initiating an altitude over airspeed take-off profile. Night departures then require an instrument take-off and climb to 500 ft before a turn is commenced. During the hover or transition the helicopter may be weather-cocked as necessary".

The Bureau of Air Safety Investigation suggested that the marine pilot's employer subject its organisation to an independent audit by an aviation consultant. The employer, in consultation with the helicopter operator, has since incorporated the following safety improvements:

  1. The marine pilot organisation has retained the services of an aviation consultant to audit all aspects of helicopter transfers of their marine pilots.
  2. Marine pilot transfers are now conducted by this company in a McDonnell Douglas 500E helicopter, which has been audited by the aviation consultant. (Any replacement helicopters must also be audited before use for marine pilot transfers.)
  3. A left and right cockpit door jettison system has been installed in the helicopter.
  4. Consideration was given to relocating the life raft to the front of the helicopter for better access but, according to the helicopter operator, this has proven to be impractical.
  5. A 360-degree rotatable 400,000 candlepower searchlight has been mounted on the underside of the fuselage.
  6. The second attitude indicator is now powered by its own independent battery.
  7. Underwater emergency exit lighting has been installed.
  8. A 406 M Hz emergency locator beacon has been fitted to the helicopter and the helicopter pilot must carry a SABRE Type 6 voice capable survival beacon.
  9. Minimum experience requirements for helicopter pilots have been increased for marine pilot transfer operations.
  10. All company helicopter pilots engaged in marine pilot transfers must be endorsed on fixed/utility floats, as well as being subjected to an annual proficiency check involving autorotative touchdowns onto water by day.
  11. Periodic pilot check-and-training flights will include very high frequency (VHF) omni directional radio range and non-directional beacon approaches under simulated instrument meteorological conditions.
  12. Marine pilot helicopter underwater escape training has been enhanced.
  13. All persons on board the helicopter now wear Civil Aviation Safety Authority approved dual-chamber life jackets, each with a survival beacon attached.
  14. Radio communications have been enhanced by improved helicopter to ship radio procedures: VHF or frequency modulated (FM) side-tone has been added to all communication stations in the aircraft.
  15. Survival equipment within the four-man life raft has been improved and a register of survival equipment is now kept up to date.
  16. The minimum length/width of midship helicopter landing sites and the final approach and takeoff areas has been increased to 20 m.
  17. No marine pilot transfers are permitted unless rescue equipment on board the vessel (including fire-fighting equipment, rescue boats etc.) is in position and ready for immediate use during helicopter transfers.
  18. Subject to re-assessment, the operator, in conjunction with the marine pilots, has decided that marine pilot transfers will only be performed when the helicopter's approach and departure can be made from ships with cranes stowed in their normal sea-going position or, if swung, are within the lateral confines of the vessel and the pulley block is fastened to the vessel.

Factual Information

Pilot information

The helicopter pilot held a commercial pilot licence, a valid class 1 medical certificate and a NVFR rating. He was endorsed to fly Hughes 500 helicopters (also known as Hughes 369HS) and was current at night flying. He held a helicopter float endorsement and had successfully undergone helicopter underwater escape training on 30 April 1995.

At the time of the accident the pilot had a total flying experience of 8,462 hours, of which 7,882 were in helicopters, including 1,408 hours in Hughes 500 helicopters. He had flown a total of 545 hours at night, and his total instrument flight time was 10 hours. A biennial flight review had been conducted on 8 March 1996, and his most recent company flight check was conducted on 14 January 1997. In the four years prior to the accident, the pilot had flown in excess of 800 marine pilot transfers at night. Most of those had been in Hughes 500 helicopters. The pilot described the helicopter landing sites on the sister ships as more than adequate for a Hughes 500 helicopter, which had a main rotor diameter of 8 m.

The pilot had been rostered for duty in accordance with an exemption against Civil Aviation Order (CAO) 48 - Duty Times which applied to company pilots engaged solely in marine pilot transfer operations. At the time of the accident, the helicopter pilot had been on call solely for marine pilot transfers for the previous two days, following two days off. After awaking at 0730 on 25 February 1997, he flew the first marine pilot transfer for the day between 1830 and 2030; the flight time was about 0.4 hours. He then slept, before departing Gladstone at about 0058 on the accident flight. The pilot reported that he had not engaged in any strenuous activities during the rostered duty period and had flown only 0.7 hours in the 24 hours before the accident.

In recounting the accident, the pilot expressed the view that conditions on the night of the accident were such that no part of the flight would have been considered difficult for an experienced marine transfer helicopter pilot in a Hughes 500 helicopter. He reported that the flight to the ship was normal. After the passenger had boarded the helicopter, the pilot checked for obstructions in the intended direction of taxi and takeoff and noted the crane jib. He planned to depart to the north-east after clearing the left side of the ship and noted that two ships positioned to the north, as well as the lights of Gladstone to the west, would give him a good visual reference.

The pilot's position in the left front seat of the helicopter provided an excellent view forward across the deck, to the left and above, and above to the right. His view immediately to the right would have been slightly restricted by the passenger.

The pilot reported that he took-off and manoeuvred the helicopter into a low hover, then taxied across the hatch towards the left side of the ship. He yawed the helicopter slightly right in anticipation of weathercocking as the helicopter cleared the ship to the left side. The helicopter weathercocked as expected. The pilot said that he then stabilised the aircraft alongside the ship briefly, maintaining a constant altitude and keeping pace with the ship. This was in accordance with company procedures for departing from ships with obstructions. With the ship to his right and the lights of two other ships in the forward left quarter of his field of view, he reported that he established a zero-bank/zero-yaw attitude in preparation for transferring to flight by sole reference to the cockpit instruments. To be sure the helicopter would move away from the ship, he yawed 10 to 15 degrees left, then simultaneously increased power and moved the cyclic control forward to accelerate and climb away. Within a few seconds of initiating this sequence, he felt a jolt and the helicopter pitched nose-up and rolled to the right. Despite flight control inputs, he was unable to counteract the roll to the right. The helicopter then struck the water. The pilot believes that the ship's crane was swung into the helicopter's rotor arc as he took off from the ship.

Aircraft information

The Hughes 369S is equipped with an articulated main rotor system, which permits the rotor blades to feather (change pitch angle), flap (move up and down vertically) and to lead and lag in the plane of rotation. The blades also have washout to equalise lift across the blade. When the blades are rotating, aerodynamic and centrifugal forces act on the rotor disc. These forces are finely balanced to keep the rotor disc stable and acting in the desired manner. If a critical component, such as a rotor blade, is damaged, the rotor disc is likely to become immediately unstable and its action unpredictable. During the investigation the pilot supplied a report, which proposed a mathematical model to verify his evidence. The report's author was not qualified as a helicopter aerodynamicist or as an accident investigator.

The helicopter was loaded within its approved centre-of-gravity and gross weight limits at the time of the accident.

The approved flight manual for the Hughes 369 states that controllability during hovering downwind, and both sideward and rearward flight, has been demonstrated to be adequate in winds up to 20 kts. The Hughes 369 also has a reputation for being fully controllable in much stronger crosswind and tailwind conditions.

Wreckage and survivability information

Examination of the wreckage did not reveal any fault that might have contributed to the accident. All flight control system damage was typical of main rotor and drive train sudden stoppage. The main rotor head assembly had suffered extensive damage, indicative of main rotor blade contact with a solid object while the rotors were being driven. The four main rotor blades and their grips were torn off the rotor head at the strap pack as a result of the blades impacting the pulley block, and the helicopter's subsequent contact with the sea. Both tail rotor blades, the tail rotor gearbox, and part of the tail rotor drive shaft had separated from the aircraft when the aft portion of the tail boom fractured during the impact sequence. Those items were lost at sea.

The engine-to-transmission drive shaft suffered an overload fracture typically caused by sudden stoppage forces. Smearing of the metal fracture surfaces on this drive shaft indicated that it had continued to rotate after the fracture occurred. An in-depth examination of the fuel system was not considered necessary, due to the physical evidence that the engine was performing at a high power setting when the main rotor strikes occurred.

The main damage to the fuselage occurred on the right side, where the fuselage skin exhibited extensive lateral/inward crushing deformation as a result of impact from one or more main rotor blades, as well as from water impact. Both front seat pans were crushed downward, consistent with the high g-loading experienced by both occupants when the helicopter impacted the sea. Both forward cabin doors separated from the aircraft. Most of the fibreglass engine intake fairing was missing after the accident.

Both flight attitude indicators fitted to the helicopter had recently been overhauled. Notwithstanding the extent of impact and salt-water damage, no fault was found with the instruments.

The carrying capacity of the crane was 25 tonnes, with a maximum outreach of 28 m. Marine surveyors subsequently advised that the design of the cables and the pulley block counteracted any tendency for the block to turn and twist the cables. Consequently, the block face that was struck by the rotor blades, was probably facing out to sea at the time of the accident.

The vertical face of the pulley block struck by the helicopter was approximately 1.4 m high by 1 m wide. Contact between the main rotor blades of the helicopter and the pulley block resulted in several distinct impact marks on the face of the block. Four of the marks displayed features that were consistent with contact by the main rotor blade leading edge abrasion strips and threaded tip weights. The sequence of the blade strikes could not be established. However, the presence of the tip weight impact marks on the block face indicated that the main rotor blades had not contacted any solid object before hitting the block.

Multiple scratch marks were found on the opposite face of the block to the main rotor blade strike marks. Those marks were considered to have been a result of contact with the tail rotor, the tail boom or the stabilisers.

No evidence was found of rotor strike marks on the hook, the swivel, the chain, or the cables above the pulley block, nor were any marks found on the upper or lower edges of the block, or on the narrow vertical edges. However, the narrow vertical edge of the block nearest the trailing end of the main rotor strike marks showed evidence of white paint and fibreglass consistent with the engine intake fairing contacting the block. Wreckage evidence indicated that the main rotor blades probably dislodged the intake fairing. Other fibreglass items attached to the airframe were relatively undamaged and showed no evidence of contacting the block.

The helicopter manufacturer reported that, "Once the first main rotor blade struck the pulley block, all blades would have been affected by the tremendous forces generated. The sudden stoppage forces imparted and damage done to the main rotor system would have resulted in severe main rotor imbalance and caused the blades to go divergent in the lead/lag axis and possibly in the flapping and feathering axis as well; in other words the blades would no longer 'fly' as you would expect normal rotor blades to. The drive train and fuselage would also have been affected by these same forces. Engineering and/or mathematical modelling of the accident scenario then becomes a wild guess, as the performance and/or actions of the fuselage, main rotor system (to include main rotor blades) and drive train are no longer predictable."

The helicopter was fitted with utility floats. A life raft was stowed in the rear passenger compartment. Both the helicopter pilot and the marine pilot wore life vests. Both occupants also wore full harness seat restraints and remained strapped in their seats during the accident sequence. Examination of the wreckage indicated that a main rotor blade had penetrated the cabin area on the right side of the aircraft, fatally injuring the passenger. The pilot was able to escape unaided from the helicopter after the accident.

Other information

Police spoke to the ship's captain by telephone two hours after the accident. The captain reported that the helicopter was almost out of the confines of the ship when it started turning left and the main rotors then struck the crane hook which was hanging in the air.

The ship's crew subsequently reported that the crane operator had turned the jib to the left side of the ship and raised both the jib and the hook before vacating the crane tower and standing on the deck for the landing and take-off of the helicopter. They said that the helicopter initially rose into a hover about 1 m above deck level, where it paused briefly before accelerating across the deck, climbing and turning left at the same time. They reported seeing the helicopter then collide with the pulley block and begin to rotate, before the tail rotor also struck the block. The helicopter then fell into the sea. Shortly thereafter, crewmembers saw the helicopter floating inverted about 15 m from the left side of the ship.

The company operations manual (page D8.10) stated:

"During each take-off, when established in the hover over the deck, a check should be made of power available, centre of gravity and temperatures and pressures before moving clear of the landing area.

At night a climb to 500 ft is to be completed before any substantial turns are made. All turns are to be made at the standard rate. Steep turns are not to be carried out".

CAO part 95, section 95.7.3: Exemption of Certain Helicopters from Compliance with Provisions of Sub-regulation 174B (2) of the Civil Aviation Regulations provides for special requirements for helicopters engaged in charter operations at night for the purpose of marine pilot transfers to/from ships. No evidence was found that the operator or the pilot had not complied with the requirements of CAO 95.7.3.

Significant Factors

The factors contributing to the accident could not be determined with certainty.

Analysis

Although there were main rotor blade strike marks on the seaward face of the pulley block, there was no strike damage on the leading or trailing edges of the block. This evidence appeared consistent with the main rotor hub being forward of a line perpendicular to the seaward block face, and the main rotor blade leading edges impacting the block face at an angle of less than 90 degrees. The ship-facing block face had no evidence of main rotor blade strike damage, however it had sustained impact damage from the tail rotor assembly. Information provided by the pilot and the ship's witnesses indicated that the main rotor disc struck the block before the helicopter began rotating. The evidence was consistent with the main rotor blades hitting the seaward block face and, as a result of the impact, the helicopter rotated clockwise, and the tail rotor assembly then struck the ship-facing block face.

Once one of the main rotor blades was damaged, it was probable that the main rotor system became unstable and its subsequent motion unpredictable due to the variables involved. A complete understanding of the relative movement between the helicopter and the pulley block requires accurate data on the motion of each object with respect to a known frame of reference. Both the ship and the helicopter were moving independently of each other. Although the speed and heading of the ship were reported, as was the sea swell, none of the information was calibrated or recorded to sufficiently fine tolerances. While the extent of the rolling and/or pitching motion of the ship was probably negligible, any movement would affect the variables in any calculation. As a consequence, the movements of the pulley block, as a result of the ship's rolling or pitching, or the influence of wind, could not be precisely determined.

These considerations, associated with the expected unstable behaviour of damaged main rotor blades, precluded an accurate assessment of the relative motion between the rotor disc and the pulley block. As a result, the strike marks on the pulley block provided insufficient physical information to reconcile the significant differences between the accounts of the ship's crew and that of the pilot. Determination of the attitude and position of the helicopter at the moment of collision was therefore not possible and any attempt to do so would be, at best, speculative. The investigation considered that, although the mathematical model proposed by the pilot and his advisors was possible, there was insufficient physical evidence to preclude other scenarios.

Summary

The helicopter was engaged in the ship-to-shore transfer of a marine pilot at night, and was operating in accordance with the night visual flight rules (NVFR). The ship was reported to be steaming at 14.5 kts, steering 044 degrees M. Weather conditions at the time were reported to be fine, with visibility of 4-5 NM. The night was also reported to have been very dark, with some haze. The sea was almost calm, with a swell ranging between 0.25 m to 0.5 m. The wind was about 5 kts from the ENE and the temperature was about 27 degrees Celsius. The moon was waning, and its bearing relative to the accident site was 027 degrees M, at an elevation of 60 degrees above the horizon.

The deck landing area measured approximately 25 m fore and aft, and 20 m across the ship, which was 23 m wide. The landing surface consisted of steel cargo hatch covers. Sea containers were stacked to a height of 5.2 m, immediately forward of the landing area.

A potential obstacle to the operation was a crane immediately aft of the landing area. In its stowed position, the crane jib would normally be aligned along the fore/aft axis of the ship, above and parallel to the landing area surface. The ship's crew reported that the marine pilot requested the crane's jib be turned 90 degrees to the left side of the ship, and elevated to its upper limit. The pulley block of the crane's hook assembly weighed an estimated 1.1 tonnes and was painted with yellow and black stripes. A lifting hook hung below the block. The crane assembly and the deck landing area were floodlit. A light on the jib illuminated the pulley block. The height of the pulley block at the time of the occurrence could not be positively established. If the crane was hoisted as reported by the ship's crew, its height above the ship's deck was about 20 m. Had the crane been swung as reported by the pilot, the height of the pulley may have been lower than 20 m. The ship's crew reported that the crane operator had vacated the crane tower and was on the deck for the arrival and departure of the helicopter. The helicopter approached the ship from the right side and landed on the forward right hatch cover, facing towards the left side of the ship. The marine pilot boarded the helicopter through the right front door and occupied the right seat. During the subsequent take-off, there was a collision between the helicopter and the pulley block, and the helicopter fell into the sea, where it floated inverted, supported by the buoyancy of its utility floats. Small pieces of rotor blade debris were found on the ship's deck. A fisherman heard the ship's master report the accident on the marine radio frequency and, after searching for about 25 minutes, located the wrecked helicopter. The passenger was fatally injured, and the pilot sustained minor injuries.

This was the first time the ship's master had accepted a helicopter marine pilot transfer from this ship. He was familiar with helicopter operations onto larger ships. He was hesitant to agree to a helicopter transfer until the ship's agent and the marine pilot convinced him that the size of the proposed landing site was adequate. This was also the first occasion that the helicopter pilot had conducted a marine pilot transfer with this ship. However, he had previously conducted two marine pilot transfers at night onto the sister ship, the most recent being on 11 February 1997.

Occurrence summary

Investigation number 199700583
Occurrence date 26/02/1997
Location 32 km E Gladstone, Aero.
State Queensland
Report release date 16/12/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Ditching
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Hughes Helicopters
Model 369
Registration VH-XAX
Serial number 530481(S)
Sector Helicopter
Operation type Charter
Departure point 32 km E Gladstone, QLD
Destination Gladstone, QLD
Damage Destroyed

de Havilland Canada DHC-1 T MK 10, VH-RWI

Summary

The aircraft was being used for endorsement training of a foreign tourist. It had been operating in the training area east of Jandakot for approximately one hour and was engaged in general handling manoeuvres and aerobatics. Having completed these manoeuvres, the instructor decided to conduct practice forced landing training. During the first approach, from an altitude of 2,500 ft, the instructor reported that the throttle had been opened twice and the engine had responded normally.

The instructor reported that at 200 to 300 ft, with 30 degrees of flap set, he instructed the student to commence a go-around. He reported that the student raised the nose attitude and opened the throttle but the engine did not respond. The student was flying the approach at 65 knots. The stall speed in the finals configuration was approximately 42 knots. The recommended climb speed was 60 knots.

The instructor reported that he checked that the throttle was fully open. He also noticed the airspeed reducing. He took over and attempted to lower the nose attitude to prevent the aircraft stalling but the aircraft did not seem to accelerate. He called to the student to check that the fuel was on.

The instructor reported that he had turned right, then left to avoid a tree and line up on a paddock. He did not assess the rate of descent as being excessive until he tried to flare the aircraft for landing. He did not recall the engine power recovering before impact.

Wreckage evidence indicated that the engine was delivering high power at impact. The wreckage and ground marks also indicated that the aircraft had struck the ground in a flat attitude at relatively low groundspeed. There was sufficient fuel and the fuel selector had been selected to the left tank.

The engine was a Gypsy Major 10, Mk 2, correctly modified for use in the Chipmunk aircraft. During the subsequent engineering examination, the engine was removed and successfully run on a test stand. An examination of the fuel components including the carburettor, fuel pump and filters indicated that there were no pre-existing faults. The engine's original Fairey metal propeller had been replaced by an approved Hoffman wooden propeller. Operators reported that the wooden propeller appeared to have less "flywheel" effect and although the engine could accelerate faster, it would also stop more readily.

Previously reported problems associated with Gypsy Major engine response during go-arounds was pinpointed to worn needle valve seats causing carburettor flooding. A modification was introduced in 1957 to address the fault. The modification was incorporated in the accident engine and the subsequent examination revealed that the valve seat was not worn.

The Gypsy Major engine does not incorporate an accelerator pump and rapid throttle openings have been known to induce a delay due to the fuel/air mixture becoming, momentarily, lean. Whilst this appears to be a known characteristic of the engine, there is no warning in the aircraft's handling notes relating to the consequences of opening the throttle too rapidly.

Evidence indicated that the engine was delivering significant power at impact. The post-accident engine examination and ensuing test run revealed that it was unlikely that a mechanical fault caused the engine to lack power during the go-around. If, however, the throttle was opened too rapidly during the go-around, the engine may have momentarily lost power through a lean cut. The wooden propeller's low inertia associated with the aircraft's low airspeed may have caused the engine to almost stop, further delaying the power response.

By the time the instructor took over, the airspeed had probably reduced rapidly towards the aircraft's stall speed as a result of the drag generated by the full flap and the pitch attitude. Whilst the manoeuvres conducted by the instructor late in the approach indicated that the aircraft had not stalled, there was probably insufficient airspeed to permit an effective flare before landing. The aircraft may have stalled during the flare, causing it to impact the ground in a near flat attitude at low speed.

Occurrence summary

Investigation number 199700590
Occurrence date 25/02/1997
Location 25 km SE Jandakot, Aero.
State Western Australia
Report release date 06/07/1997
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Forced/precautionary landing
Occurrence class Accident
Highest injury level Serious

Aircraft details

Manufacturer De Havilland Canada/De Havilland Aircraft of Canada
Model DHC-1
Registration VH-RWI
Serial number DHB/F/94
Sector Piston
Operation type Flying Training
Departure point Jandakot, WA
Destination 25 km SE Jandakot, WA
Damage Destroyed

Cessna A188B/A1, VH-MXB, 57 km south-west of Oakey Aerodrome, Queensland

Summary

The Pilot was engaged in aerial spraying operations when the aircraft's right main landing gear struck an 11.000 V powerline (3 wires). The aircraft impacted the ground and burst into flames 60 m beyond first contact with the power line. The crash was not survivable.

The pilot had completed spraying 1 previous load on the same paddock and was observed to fly routinely over the powerline on these runs. The aircraft crashed as the second load was almost expended. The sun was 18 degrees above the horizon at the time of the crash. The last spray run was aligned 223 degrees M, 33 degrees left of the sun.

The aircraft struck all 3 strands in a 90 m span, approximately 10 m left of a 7 m power pole. A spur line ran east from the pole to one near an irrigation pump, 50 m away.

Occurrence summary

Investigation number 199700480
Occurrence date 19/02/1997
Location 57km SW Oakey, Aerodrome
State Queensland
Report release date 09/05/1997
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Collision with terrain
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Cessna Aircraft Company
Model 188
Registration VH-MXB
Serial number 18803433T
Sector Piston
Operation type Aerial Work
Departure point Tyunga, QLD
Destination Tyunga, QLD
Damage Destroyed

Centrum Naukowo-Produkcyjne-PZL M-18A, 1Z024-14

Safety Action

As a result of this occurrence, The Bureau of Air Safety Investigation is further investigating a safety deficiency involving the misinterpretation of the Civil Aviation Safety Authority maintenance schedule, CAR42B Schedule 5.

Any recommendation issued as a result of this deficiency analysis will be published in the Bureau's Quarterly Safety Deficiency Report.

Analysis

Pilot and eyewitness descriptions of events immediately prior to the accident suggest that the engine lost a substantial degree of power, but did not completely fail.

It is likely that the engine power loss was gradual. This was evidenced by the pilot's report of the aircraft's increasing nose-down tendency and its extended flight profile. Examination of the engine indicated that it was producing limited power at impact. There was no evidence of any pre-existing condition that may have adversely affected the serviceability of the engine.

A significant amount of water and other contaminants were found in the firewall fuel filter.

Inspection and testing indicated that the water had been in the filter a significant length of time. The water in the carburettor bowl and the fuel pump was clear and the lack of corrosion or other damage inside the carburettor and the pump indicated that the water had only recently been introduced to those components, possibly during the post-accident firefighting operations. No factors, other than water contamination and the deterioration of the fuel filter, were disclosed during the investigation. Consequently, it is considered that the deterioration of the filter most likely contributed to the engine's loss of power.

There was no evidence to indicate that the fuel filter had been removed and inspected during the periodic inspection conducted for the initial issue of an Australian aircraft maintenance release or at any subsequent time prior to the occurrence. The aircraft maintenance schedule elected by the Certificate of Registration holder would not have required a further inspection of the filter until 100 flight hours had been completed after the initial inspection.

During the investigation, it became apparent that there was a general misunderstanding of the intent of certain aspects of the CASA maintenance schedule contained in CAR42B Schedule 5.

Summary

Two aircraft were being used to suppress bushfires in the Perth basin. At approximately 1027 WST, the aircraft were called to a fire near Maddington, an outer suburb of Perth approximately 6 NM south-east of Perth airport. The pilot of VH-JTD reported that no problems were identified during the pre-take-off checks.

Both aircraft departed at approximately 1035 towards the south. Air traffic controllers in the tower noted that JTD, the accident aircraft, flew a shallower departure profile than the other aircraft. The pilot later reported that the profile resulted from his operating technique and not from any problem associated with the aircraft.

Because the bushfire was relatively close to the airport, both aircraft climbed to only 1,200 ft before descending to conduct the inspection circuit at about 1,000 ft. While communicating with the bushfire ground controllers, the pilots positioned their aircraft in a left circuit pattern to reduce the time during which the aircraft were climbing out over populated areas. The pilots then approached the fire from the south-east. The first aircraft dropped its load of fire retardant without incident.

The pilot of JTD reported that he set up the approach slightly tighter and steeper than usual due to the proximity of housing. Just prior to the base turn, he selected full flap and set the propeller to a fine-pitch setting.

During the base turn, the pilot reported that he needed more elevator control back pressure than usual to maintain the aircraft's nose attitude. The pilot initially thought that the aircraft's trim setting needed adjusting, until the nose dropped further. The pilot levelled the wings and fully opened the throttle: this appeared to have little or no effect and he decided to immediately dump the load of retardant. He could not recall any engine instrument indications. Because the dump system had been set up for a partial dump only, he decided to use the manual lever rather than the electric switch to dump all the fire retardant. Following the loss of engine power, the pilot turned on the emergency fuel pump as required in the emergency checklist, but did not apply carburettor heat.

The pilot reported that the aircraft appeared to travel further than expected during the descent. He flew the aircraft close to the stall at approximately 60 kts during the forced landing, using rudder to control wing drop. Having passed over several streets, the pilot decided to attempt to land the aircraft on a small street, parallel and close to the aircraft's flight path.

The aircraft severed a set of powerlines at the northern end of the street before its right wing struck and broke a power pole. The aircraft then veered right, glanced off the roof of an occupied house, and embedded itself into the next house, which was unoccupied at the time.

Once the aircraft had come to rest, the pilot switched off the fuel and electrical systems. There was no fire. He then exited the aircraft and signalled to the other pilot that he was okay. The pilot was wearing a four-point harness and a flying helmet, both of which were undamaged. However, the pilot received minor injuries to his left leg during the impact sequence. The nature of the impact sequence appeared to have progressively slowed the aircraft, thereby lessening the peak forces suffered by the pilot.

When the other pilot saw that JTD had crashed, he advised air traffic services of the accident and gave directions to enable emergency services to locate the accident site. Emergency services arrived about 5 minutes later. The pilot switched off the operating emergency locator transmitter.

Wreckage examination

The aircraft's forward fuselage was substantially damaged and the main landing gear had collapsed. The wings remained attached to the fuselage although powerlines had severed 2 m of the left wing. The cabin was penetrated by two pieces of wood from the house roof trusses. The engine was torn from its mounts, moving 1 m forward and rotating approximately 90 degrees to the left.

The on-site examination of the engine revealed no abnormality. The carburettor was firmly attached and all four butterfly valves were fully open although their positioning may have resulted from the impact. The propeller remained attached to the engine with all blades bent backwards. The general appearance of the blades indicated that the propeller was rotating at low power at impact.

Meteorological information

The Bureau of Meteorology reported that there was 2 octas of cumulo-form cloud at 4,500 ft. The temperature was approximately 35 degrees C, dewpoint was 16.5 degrees C, and there was a relative humidity of 38% at Perth airport. There was a light wind from the north-east.

Fuel system

The fuel system included two wing tanks connected to a header tank. Fuel from the header tank was drawn by the engine-driven fuel pump and fed through a firewall-mounted filter before entering the carburettor.

The operator reported that the aircraft departed with a fuel load of approximately 700 L and that approximately 40 L of fuel was drained from the left tank soon after the accident. It was estimated that about another 20 L was spilled during the aircraft wreckage recovery. The right wing tank contained no fuel when it was inspected after the accident; however, the fuel would have drained from the fuel lines that were damaged during the collision sequence.

A sample of fuel was drained from the left wing tank and analysed. The analysis confirmed the fuel as Avgas 100/130. Apart from an extremely low Reid Vapour Pressure, it complied with the fuel specification requirements. The fuel sample was taken almost 24 hours after the accident. The fuel manufacturer reported that due to the hot weather in Perth at the time, the lighter fuel fractions may have evaporated from the ruptured tank, resulting in the low vapour pressure.

A small amount of clear water was found in the fuel sample drained from the fuel pump.

Fuel lines to and from the fuel filter, mounted on the firewall, were severed at the filter. The fuel filter did not have an external or cockpit warning to indicate when the filter was blocked and operating in bypass. The aircraft's flight manual noted that the fuel pressure indication dropped when the filter was blocked, but the pilot reported that he did not observe such an indication. A mixture consisting of 50% fuel and 50% black-coloured water was drained from the filter. Chemical analysis of the water found the presence of dissolved impurities.

Examination of the filter element found the lower part saturated with water and heavily contaminated with rust particles to the point that the lower half of the filter was blocked. On the fuel inlet side, there was a significant accumulation of large, flat rust pieces. The lower half of the steel coil inside the element was severely corroded. Analysis indicated that the large rust pieces probably originated from a fuel storage tank. Specialist examination of the filter indicated that the water and subsequent corrosion had been present for an extended period.

Approximately 250 mL of fuel and a similar quantity of water were drained from the carburettor bowl. Both samples were free of sediment. The carburettor was a standard float type, where the pressure difference between the chamber and venturi regulated the amount of fuel drawn. The carburettor was opened and inspected. No sediments, or evidence that water had been present for an extended period, were found. The examination of the carburettor found no defect that may have adversely affected its operation.

The aircraft was manufactured in 1993 and operated in the USA before its purchase by the Australian owner in 1996. The aircraft Certificate of Registration holder made a valid election to use the Civil Aviation Safety Authority (CASA) maintenance schedule, CAR42B Schedule 5, as the aircraft maintenance schedule and the aircraft had undergone a periodic maintenance inspection prior to the issue of an Australian maintenance release. A subsequent periodic maintenance inspection would then be required at the completion of 100 flying hours or 12 calendar months.

An option available to the aircraft Certificate of Registration holder was to elect to use the aircraft manufacturer's maintenance schedule, which would require that the fuel filter be inspected every 50 (+/- 5) flight hours.

On 5 February 1999, CASA informed the Bureau that the aircraft maintenance schedule, CAR 42B Schedule 5 Part 1, required that a fuel sample drain of aircraft fuel filters be conducted each day the aircraft was flown, except when not applicable to the aircraft. In the case of the PZLM18A aircraft, CASA stated that the engine firewall fuel filter would not be required to have a fuel sample drain carried out during the daily inspection.

The Civil Aviation Safety Authority confirmed that the firewall fuel filter should have been inspected during the initial periodic inspection for the issue of the aircraft maintenance release.

At the tiine of the accident, the aircraft had accumulated approximately 53 flying hours since the completion of the periodic inspection. The investigation could find no evidence that the firewall fuel filter had been inspected at any time prior to or during flying operations in Australia.

Occurrence summary

Investigation number 199700297
Occurrence date 03/02/1997
Location Maddington
State Western Australia
Report release date 19/03/1999
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Occurrence class Accident
Highest injury level Minor

Aircraft details

Manufacturer PZL Warszawa-Okecie
Model M-18
Registration VH-JTD
Serial number VH-JTD
Sector Piston
Operation type Aerial Work
Departure point Perth, WA
Destination Perth, WA
Damage Destroyed

Bell 47G-2, VH-JKR, 1 km south-east of Gawler, Tasmania

Summary

While spraying fungicide onto an 8-acre potato crop, the helicopter struck a powerline. The helicopter impacted the ground, and the pilot received fatal injuries.

Occurrence summary

Investigation number 199700357
Occurrence date 07/02/1997
Location 1 km south-east of Gawler
State Tasmania
Report release date 06/08/1997
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Wirestrike
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Bell Helicopter Co
Model 47
Registration VH-JKR
Serial number 2409
Sector Helicopter
Operation type Aerial Work
Departure point 4 km NW Gawler, Tas
Destination 4 km NW Gawler, Tas
Damage Destroyed

Alexander Schleicher Gmbh & Co, VH-UKG and Schempp-Hirth GmbH & Co. KG, VH-GWX, Roseberry, Victoria

Summary

During a competition, several high-performance single-seat gliders were flying on a triangular cross-country exercise in loose formation at between 2,500 and 3,000 ft AGL. VH-UKG was flying near the front of the group and began a left turn in search of rising air. At that time, VH-GWX, which had recently joined the group, came alongside the left side of UKG and began to pass.

The pilot of UKG became aware of GWX at the last moment and attempted to dive clear but the right wing of his glider, at about mid-span, struck the right side of the cockpit of GWX.

UKG became uncontrollable as the wing disintegrated, the pilot jettisoned the canopy and bailed out at low level, receiving serious injuries.

The other glider was seen to perform a looping-type manoeuvre and impact the ground in a near-vertical attitude at high speed. Although the pilot was wearing a parachute, he did not abandon the aircraft. The pilot received fatal injuries.

Occurrence summary

Investigation number 199700214
Occurrence date 24/01/1997
Location Roseberry
State Victoria
Report release date 01/07/1997
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Airborne collision
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Alexander Schleicher Segelflugzeugbau
Model ASW 22
Registration VH-UKG
Serial number 5
Operation type Gliding
Departure point Horsham, Vic
Destination Horsham, Vic
Damage Destroyed

Aircraft details

Manufacturer Schempp-Hirth Flugzeugbau GmbH
Model Nimbus
Registration VH-GWX
Serial number Nimbus 2C, 178
Operation type Gliding
Departure point Horsham, Vic
Destination Horsham, Vic
Damage Destroyed

Cessna 182F, VH-CNG, 22 km south-south-east of Proserpine Aerodrome, Queensland

Summary

The aircraft struck powerlines while manoeuvering near the Bloomsbury airfield. It then fell to the ground on the edge of a small dam. Most of the aircraft was destroyed by fire but the empenage came to rest on a small boat moored at the edge of the dam.

Occurrence summary

Investigation number 199700051
Occurrence date 08/01/1997
Location 22 km south-south-east of Proserpine Aerodrome
State Queensland
Report release date 26/09/1997
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Ditching
Occurrence class Accident
Highest injury level Fatal

Aircraft details

Manufacturer Cessna Aircraft Company
Model 182
Registration VH-CNG
Serial number 182-54642
Sector Piston
Operation type Private
Departure point Mackay, Qld
Destination Shute Harbour, Qld
Damage Destroyed