Fumes

British Aerospace Plc BAe 146-300, VH-NJL

Safety Action

Issues associated with improving cabin air quality are the subject of ongoing efforts by the aircraft manufacturer, engine manufacturer, aircraft operators and some aviation regulatory authorities including the Australian Civil Aviation Safety Authority.

The Civil Aviation Safety Authority issued an airworthiness directive on 28 November 2002 (AD/BAe 146/102) requiring operators of BAe 146 type aircraft to action requirements of a manufacturer's Inspection Service Bulletin (ISB) 21-156. This related to the recurrent inspection of air conditioning ducts for traces of possible contamination and inspection of the ducts following a cabin air quality event.

The aircraft operator has also commenced replacing the noise-attenuating material that lines the air conditioning ducts across their entire BAe 146 fleet. This action exceeded the manufacturer's requirements outlined in its ISB 21-156.

The engine manufacturer is developing a redesigned bearing seal to improve the component's reliability and consequently reduce the frequency of incidents where cabin air is contaminated by engine lubricating oil.

Analysis

The investigation considered that the intermittent deterioration in cabin air quality was consistent with other similar occurrences during which the cabin air was contaminated by engine or APU lubricating oil. Due to the intermittent nature of contamination the source of the fumes was difficult to positively identify.

It was not possible to identify the substance(s) that had apparently contaminated the crew's drinking water while it had been left standing in the cups. However, the investigation could not discount the possibility that the drinking water had been contaminated by water-soluble compounds from cabin air contaminated by engine lubricating oil.

Summary

The co-pilot of the BAe146-300 reported that he noticed both cockpit side windows were open as he entered the flight deck to commence his pre-flight preparations and almost immediately detected the presence of fumes. He stated that these fumes had a distinctive odour that he recognised as being consistent with the contamination of the cabin air supply by lubricating oil from the aircraft's engines. This typically occurs when a faulty bearing seal allows lubricating oil to escape and contaminates one of the sources of cabin air for the aircraft.

The auxiliary power unit (APU) was operating and air conditioning Pack 1 and 2 were supplying air to the flight deck and passenger cabin. As Pack 1 supplies most of the air to the flight deck and because fumes were not apparent in the passenger cabin, the co-pilot immediately suspected that the contamination was associated with Pack 1. He de-selected Pack 1 and noticed an immediate improvement to the quality of the air.

The co-pilot briefed the pilot in command of these observations when he arrived on the flight deck. The crew used engine bleed air to provide cabin air conditioning as the aircraft taxied for take-off and Pack 1 remained de-selected. This was on the basis of the tailwind conditions encountered while taxiing, to reduce the possibility of ingesting fumes from the APU's exhaust into the aircraft cabin and the co-pilot's observations of air quality from Pack 1. The take-off was performed with all air conditioning packs selected off and number 4 engine supplying bleed air for pressurisation control of the aircraft cabin.

The co-pilot was the handling pilot for the sector from Perth to Karratha. After take-off, the crew selected engine bleed air sources from all engines and Pack 1 and 2 were used to provide air conditioning to the passenger cabin and flight deck. No fumes were evident in either the passenger cabin or the flight deck and the flight proceeded normally.

About 10 minutes prior to the top of descent, the co-pilot recalled starting to experience symptoms of a headache. He was able to continue his duties as handling pilot and completed the descent to the Karratha circuit area. The aircraft was on final approach to land, when strong oil-type fumes were again detected on the flight deck. As the aircraft cabin had already stabilised at sea-level atmospheric pressure and the source of fumes appeared to be either the air conditioning packs or one of the engine bleed air supplies, all air conditioning packs and all sources of engine bleed air were selected off. The intensity of the fumes quickly dissipated and the co-pilot completed the landing. Fumes were not detected in the passenger cabin by any of the flight attendants. The co-pilot reported that supplemental oxygen was not used on this occasion due to the critical phase of flight (short final approach to land) and the prompt action taken to isolate the source of fumes.

During the taxi to the passenger terminal, the co-pilot became aware that he was experiencing symptoms of an unusually strong headache, nausea and irritated eyes, nose and throat. His symptoms quickly improved as he conducted the external turnaround duties and he felt capable of performing his duties on the return sector as pilot not flying.

The pilot in command was satisfied that the source of fumes experienced on short final was associated with contamination of the cabin air supply by engine lubricating oil. The return flight was conducted without using APU air and with Pack 1 de-selected to minimise the possible recurrence of fume contamination. The flight was completed without incident.

Subsequent to the incident, the co-pilot recalled that during the outbound sector his bottled drinking water, which had been poured and left standing in his cup, had acquired a rank swampy, slightly metallic taste. The pilot in command was also reported to have made a similar comment about the taste of his drinking water. The cups were resting in the flight deck cup holders adjacent to the air outlet vents. This was noticed prior to the co-pilot reporting symptoms of a headache and fresh cups of water from the bottle tasted normal with no apparent sign of contamination. The ATSB were not able to test the water for contaminants as it had been discarded following the flight.

Following entry of the fume report in the aircraft's defect log, company engineering personnel applied the requirements of Airworthiness Directive AD BAe 146/86, issued 30 March 2001 that required inspection of various components associated with the aircraft's cabin air supply. This inspection revealed no apparent defects or source of contamination to the cabin air.

The operator received subsequent Operating Crew Reports associated with poor cabin air quality on 23 and 26 October 2002. The aircraft commenced a period of heavy maintenance on 28 October 2002. During this maintenance the APU was removed from the aircraft, cleaned, inspected (with nil defects found) and refitted. Air conditioning Pack 1 was also cleaned. The operator received subsequent reports of flight deck odours with respect to this aircraft on 5 and 8 December 2002 and the requirements of the Airworthiness Directive were again applied. On this occasion the inspections revealed slight leakage of engine lubricating oil from a bearing seal on the number 4 engine.

Occurrence summary

Investigation number 200204912
Occurrence date 20/10/2002
Location 6 km E Karratha, Aero.
State Western Australia
Report release date 20/08/2003
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer British Aerospace
Model BAe 146
Registration VH-NJL
Serial number E3213
Sector Jet
Operation type Air Transport High Capacity
Departure point Perth, WA
Destination Karratha, WA
Damage Nil

British Aerospace Plc BAe 146-200, VH-JJU

Safety Action

On 6 September 1999, the Australian Transport Safety Bureau issued recommendation R19990052 to the Civil Aviation Safety Authority. That recommendation stated that:

"The Civil Aviation Safety Authority, in conjunction with the aircraft manufacturer, British Aerospace Plc, address deficiencies that permit the entry of fumes into the cockpit and cabin areas of BAe 146 aircraft. These deficiencies should be examined by the regulatory authority as part of its responsibilities for initial certification and continued airworthiness of the BAe 146 aircraft."

The Civil Aviation Safety Authority responded on 14 March 2000 stating:

"In the lengthy period between the incident and the release of your report, CASA has investigated this issue in considerable detail, in conjunction with the aircraft manufacturer and the major Australian operators. As a result of this work, and discussions with the certifying authority (the UK Civil Aviation Authority), CASA is satisfied that the BAel46 aircraft in service in Australia are safe for public transport. CASA technical specialists are available to brief your investigators on the scope and findings of this work.

"As your recommendation does not specify the nature of any additional deficiencies that the Bureau believes need to be addressed by CASA and the aircraft manufacturers, I am seeking details of any deficiencies that you believe have not been appropriately dealt with. It would also assist us in providing a meaningful and constructive response to your recommendations if you were to provide us with details of any incidents that have occurred since the original incident in 1997.

"In the meantime, we will continue to monitor the situation and review any information that comes to hand."

The Bureau classified the response as "Open" and has initiated further correspondence with CASA. On 12 October 2000, the Senate Rural and Regional Affairs and Transport References Committee tabled its report into Safety and Cabin Air Quality in the BAe 146 Aircraft. The Government tabled its response to the References Committee's report on 28 June 2002.

Analysis

The cabin manager's observations, during the take-off roll, of a smoky burning smell, and her subsequent symptoms, suggested contamination of the cabin air supply with the by-products of engine combustion. Her blood test results, appearing consistent with CO exposure, seemed to confirm that hypothesis. Although maintenance engineers traced the source of oil contamination to the number 3 engine, the investigation was unable to positively determine the exact origin of the fumes that affected the cabin manager. At the stage of flight when fumes affected the cabin manager, the air conditioning packs were being supplied with air from the APU, not from the engines.

It was considered possible that, at some stage prior to the flight, air conditioning pack number two was contaminated with the by-products of the thermal degradation of oil from the number 3 engine. That would have resulted in the tainting of the APU air as it passed through air conditioning pack two before entering the cabin. It is also possible that the cabin air became contaminated from an external source. While taxiing, the aircraft's engine exhaust or a preceding aircraft's engine exhaust may have been ingested into the APU air intake, resulting in the cabin air contamination.

The fumes had a detrimental effect on the well being of the cabin manager. The potential effect on her ability to effectively carry out her duties in the event of an emergency could not be determined.

Summary

During the take-off roll, the cabin manager of the BAe 146 aircraft became aware of a smoky, burning smell coming from an air vent in the region of her crew seat at the forward (L1) exit door. Initially there was a mild odour. That was followed by the rapid onset of strong fumes for a short period after which the fumes dissipated quickly. The event was of 2-3 minutes duration.

The cabin manager felt overwhelmed by the fumes and was on the verge of passing out when her colleagues became aware of the situation and provided her with portable oxygen. After approximately 10 minutes of using oxygen, the cabin manager felt well enough to attempt a resumption of her duties but was unable to continue due to the effect of the fumes exposure.

The cabin manager, who had ten years of operational experience on the BAe 146, spent the duration of the flight seated at the rear of the aircraft; breathing portable oxygen for most of that time. The cabin manager reported that when she was not using oxygen she felt unwell, she had difficulty in thinking clearly and she found it difficult to coordinate her thoughts with her actions. No other members of the crew or any of the passengers reported being affected by the fumes.

Upon arrival in Kununurra, engineering inspections were performed on the aircraft and further action was deferred in accordance with the Civil Aviation Safety Authority airworthiness directive AD/BAe146/086. That airworthiness directive required certain actions to be performed whenever a cabin air quality problem was identified, which was suspected of being associated with oil contamination of the air supply from the air conditioning packs. Subsequent engineering inspections revealed that the cause of the oil contamination was a worn number one bearing seal in the number 3 engine. The engine was replaced and no further fumes were evident during following flights.

The cabin manager sought medical treatment and tests in Kununurra on the day of the incident and in Perth on the following day. Although she was eventually cleared to return to work, symptoms of anxiety, impaired judgement, and light-headedness remained with her for in excess of one week. Of note was the result of a blood test that revealed she had been exposed to a higher than normal level of carbon monoxide (CO). When inhaled, CO combines with the haemoglobin, the blood's oxygen-carrying molecule, to form carboxyhaemoglobin (COHb). Once in that state, the haemoglobin is unable to carry oxygen. Thus, the blood's ability to carry oxygen to body tissues, including vital organs such as the heart and brain, is inhibited.

CO is the product of incomplete combustion of carbonaceous material. It is found in varying amounts in the smoke and fumes from burning aircraft engine fuels and lubricants. The gas itself is colourless, odourless, and tasteless but is usually mixed with other gases and fumes that can be detected by sight or smell. Individuals that have been exposed to CO should be removed from the exposure and administered 100 percent oxygen through a tight fitting mask until all symptoms have been resolved. If blood testing for measurement of COHb level is required, the samples should be drawn as soon as possible after the exposure, as COHb has a short half-life in the body of 4-5 hours. If an individual is administered 100 percent oxygen, the half-life is reduced to 40 to 80 minutes.

The same aircraft was the subject of a pilot report three days prior to the cabin manager's experience, in which an oil-like smell was evident in the cockpit but not in the cabin. The event was of short duration and occurred just after take-off, when the source of air supply was changed from the Auxiliary Power Unit (APU) to the engines. Inspection by maintenance engineers of the engines, APU, and air-conditioning system revealed no signs of contamination and the defect was cleared.

Evidence from previous incidents of air system contamination on this type of aircraft has indicated that fumes were associated with engine or APU oil contamination of the air conditioning system. The BAe146 is similar to many aircraft in that the supply of cabin air originates in the aircraft's engines. Air is bled from the final stage of the engine's high-pressure compressor just prior to the combustion chamber. The air destined for the cabin then passes through a catalytic converter in order to clean the air of any oil contaminants. Catalytic converters operate at maximum efficiency under highly specific conditions of temperature and contaminant to air ratio. The air is then passed through a heat exchanger and then through one of two air conditioning packs before entering the cabin. During normal operation bleed air from engines one and two is fed to pack one, which in turn supplies conditioned air to the flight deck and cabin. Bleed air from engines three and four is fed to pack two, which normally only supplies air to the cabin. Additionally, bleed air from the APU is used by either pack during the take-off and landing phases or when air conditioning is required on the ground.

Occurrence summary

Investigation number 200103238
Occurrence date 18/07/2001
Location Perth, Aero.
State Western Australia
Report release date 04/07/2002
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer British Aerospace
Model BAe 146
Registration VH-JJU
Serial number E2116
Sector Jet
Operation type Air Transport High Capacity
Departure point Perth, WA
Destination Kununurra, WA
Damage Nil

British Aerospace Plc BAe 146-100, VH-NJR

Safety Action

On 6 September 1999, the then Bureau of Air Safety Investigation issued recommendation R19990052 to the Civil Aviation Safety Authority. That recommendation stated that:

The Civil Aviation Safety Authority, in conjunction with the aircraft manufacturer, British Aerospace Plc, address deficiencies that permit the entry of fumes into the cockpit and cabin areas of BAe 146 aircraft. These deficiencies should be examined by the regulatory authority as part of its responsibilities for initial certification and continued airworthiness of the BAe 146 aircraft.

The Civil Aviation Safety Authority responded on 14 March 2000 stating:

"In the lengthy period between the incident and the release of your report, CASA has investigated this issue in considerable detail, in conjunction with the aircraft manufacturer and the major Australian operators. As a result of this work, and discussions with the certifying authority (the UK Civil Aviation Authority), CASA is satisfied that the BAel46 aircraft in service in Australia are safe for public transport. CASA technical specialists are available to brief your investigators on the scope and findings of this work.

"As your recommendation does not specify the nature of any additional deficiencies that the Bureau believes need to be addressed by CASA and the aircraft manufacturers, I am seeking details of any deficiencies that you believe have not been appropriately dealt with. It would also assist us in providing a meaningful and constructive response to your recommendations if you were to provide us with details of any incidents that have occurred since the original incident in 1997.

"In the meantime, we will continue to monitor the situation and review any information that comes to hand."

The Bureau classified the response as "Open" and initiated further correspondence with CASA. On 12 October 2000, the Senate Rural and Regional Affairs and Transport References Committee tabled its report into Safety and Cabin Air Quality in the BAe 146 Aircraft. The Government tabled its response to the References Committee's report on 28 June 2002.

Analysis

The short taxi distance after landing limited the opportunity for the crew to investigate the origin of the contaminated air. However, only one air conditioning pack was in use and the APU was the sole source of air to that pack. The APU was found to be producing fumes during the day following the incident and it is considered that it was likely to have been producing fumes on the day of the incident.

By the time the aircraft was parked, the APU had almost certainly been passing oil fumes to the number 1 pack for about five minutes. Some of the crew felt increasingly unwell during the subsequent engine start even though no air supply source was selected. That may have been a result of residual fumes in the air conditioning ducting being circulated by the cabin fan.

There was no doubt that fumes contaminated the cabin and flight deck. The pilot in command became aware that the fumes had caused a detrimental effect to his performance and he took appropriate steps to terminate the flight. The implication that the fumes may have had a subtle but adverse affect on the pilot's decision-making process was not conclusively determined.

Summary

The BAe 146 aircraft had departed Brisbane, Qld on a flight to Mackay, Qld with a carried-forward defect that required the number 1 air conditioning pack to be used as the sole source of air for the cabin and flight deck. That situation was permissible under the terms of the aircraft's Minimum Equipment List (MEL), which allowed operation of the aircraft in non-standard configurations. The number 2 pack was not to be used because an intermittent oil leakage in the number 4 engine was a potential source of air contamination to air conditioning pack two.

During normal operation, bleed air from engines one and two was fed to pack one which in turn normally supplied conditioned air to the flight deck and cabin. Bleed air from engines three and four was fed to pack two, which normally supplied air to the cabin only. Additionally, bleed air from the auxiliary power unit (APU) was used by either pack during the take-off and landing phases or when air conditioning was required on the ground.

The flight to Mackay was uneventful. During the approach to land, the APU was selected as the bleed air source for pack one and the configuration remained that way until the aircraft was parked, the engines were shut down and the passengers disembarked.

From the time the aircraft turned off the runway, the crew was aware of a strong oil smell coming from the air-conditioning system. The fumes were detected in the cabin as well as the flight deck. Because it was a short taxi distance and a busy period on the flight deck, the crew did not have time to investigate the origin of the contaminated air. Although the smell was generally described as oil-like, the moderate south-east surface wind may have added to the air contamination by directing engine exhaust fumes into the APU air intake.

The pilot in command vacated the aircraft to get some fresh air and a short time later he suffered headache, itchy eyes, nausea and a bad taste. Company engineers at the Brisbane and Adelaide bases were consulted by telephone and a decision was made to proceed with the scheduled return flight to Brisbane using engine air one and two as the sole source of air to pack one. As the pilot in command was still suffering from the symptoms described above, he checked with the first officer and confirmed that he was unaffected by the fumes incident and requested the first officer to be the handling pilot on the next sector.

The passengers were embarked, the doors were closed and the engine start procedure was commenced. During the turnaround, the air conditioning had been turned off and remained off during the engine start. However, the cabin fan, which distributed air to the cabin through individual louvres above each passenger seat, was on. After starting three of the four engines the pilot in command felt increasingly unwell and the cabin staff also became aware that they were being affected by the fumes. The pilot in command then cancelled the flight and later expressed concern that he had considered attempting a flight while still feeling the effects of the air contamination. He stated that he may have been influenced by his desire to consult his Designated Aviation Medical Examiner in Brisbane as soon as possible. He also noticed that he had made simple errors during the flightdeck preparation and put those errors down to the effect of the fumes on his thought processes. Previous incidents have indicated that operating crews were not aware of their impairment and the subsequent effect on their decision making ability. The seriousness of that aspect was reflected in the decision by the Civil Aviation Safety Authority (CASA) to adopt a United Kingdom Air Accidents Investigation Branch (AAIB) recommendation requiring flight crew to use oxygen masks selected to 100 percent when there is a suspicion of flight deck or cabin air contamination.

A Licensed Aircraft Maintenance Engineer (LAME) was dispatched to Mackay to investigate the source of the fumes. The engineer carried out an inspection in accordance with a CASA airworthiness directive AD/BAe146/086, issued 30 March 2001, and British Aerospace Systems Information Service Bulletin (ISB) 21-150. The ISB required certain actions to be performed whenever a cabin air quality problem was identified, which was suspected of being associated with oil contamination of the air supply from the air conditioning packs. The engineer's inspection of the air conditioning system, engines and APU revealed no signs of oil contamination or oil leaks. The aircraft was ferried to Brisbane where further investigation, including an air test, confirmed that the number 4 engine was producing fumes during the climb and the descent and the APU was continuously producing fumes. Subsequently the number 4 engine and the APU were replaced.

The two cabin staff received medical advice and resumed their flying duties. Medical tests were carried out on the pilot in command but no abnormalities were detected and he resumed flying duties one week after the incident. The co-pilot was unaffected by the fumes.

Particular attention has been paid to this type of problem in Australia since July 1997 due to apparently similar incidents and crew reaction. A number of organisations, including the ATSB, have been conducting investigations into the subject of air quality in BAe146 aircraft. Evidence from previous incidents of air system contamination on this type of aircraft has indicated that the fumes are associated with engine or APU oil contamination of the air conditioning system. As a result, operators have incorporated various modifications to the cabin air system, APU and engines. They have also introduced improved maintenance practises to further address the issue. However, that action has not completely solved the problem. The air supplied to the air conditioning packs is protected from contamination by oil seals in the engines and APU. A technical defect arising in one of these seals can result in oil entering the cabin air conditioning system with the first signal of the defect being an awareness of fumes by the members of the crew. The difficulty of identifying the origin of the contamination is exacerbated by the often intermittent nature of the fume events.

Occurrence summary

Investigation number 200102467
Occurrence date 31/05/2001
Location Mackay, Aero.
State Queensland
Report release date 04/07/2002
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer British Aerospace
Model BAe 146
Registration VH-NJR
Serial number E1152
Sector Jet
Operation type Air Transport High Capacity
Departure point Brisbane, QLD
Destination Mackay, QLD
Damage Nil

British Aerospace Plc BAe 146-100, VH-NJY

Safety Action

Local safety action

As a result of the investigation the operator has:

  1. Scheduled detailed visual inspection of airstair actuators and fittings during routine maintenance.
  2. Issued maintenance instructions to check that:
    • airstair retract switch covers are fitted and correctly aligned with the rocker switch;
    • adequate tolerances exist when replacing panels around the retract switch so that the switch cannot be fouled by surrounding panels; and
    • the retract switch operates without obstruction and springs back to the `off' position.
  3. Amended maintenance schedules to include:
    • Operational check of the airstair hydraulic system;
    • Inspection for evidence of hydraulic leakage from the `retract' actuator banjo fittings and airstair hydraulic coupling and banjo fitting; and
    • Regular change of airstair banjo fitting `o' rings, as required, during heavy maintenance checks.
  4. Amended flight attendant emergency procedure manuals and training sessions to reflect the requirement for cockpit doors to be closed in the event of smoke or fumes.
  5. Amended flight crew and flight attendant training modules to include scenarios that reflect aspects of this occurrence, including information regarding suitable evacuation paths for passengers and crew.
  6. Formed a working group within the Australasian Aviation Ground Safety Council. The working group will develop a Recommended Industry Practice procedure for response to an aircraft that has an emergency return to the terminal from a taxi position

Significant Factors

  1. The airstair retract switch remained in the `on' position, thereby allowing sustained hydraulic pressure to be delivered to the airstair retraction system.
  2. The airstair actuator banjo fitting `o' ring failed.
  3. The non-use of the crew interphone system exposed the flight crew to the fumes.
  4. Cabin crew opened the flight deck door allowing the mist/fumes into the flight deck.
  5. Emergency response teams did not provide portable stairs in a timely manner.
  6. Cabin crew disembarked passengers through the fumes affected forward left door.



 

Analysis

Airstair operation

The electric stand-by pump would have been switched off from the flight deck shortly after airstair retraction, thereby reducing hydraulic pressure even though the retract switch was stuck in the `on' position.

However, after engine start, the engine driven hydraulic pumps would have delivered pressure to the airstair hydraulic system. Sustained hydraulic system pressure would then have been delivered to the airstair retraction system when the pump was engaged.

The failure of the retract switch allowed sustained pressure to be delivered over an undetermined, but excessive time, to the airstair retraction system. That exposure resulted in the failure of the `o' ring and consequent leakage of fluid, as a fine mist, into the cabin.

Emergency Procedures

Instead of using the crew interphone, to contact the flight crew, the flight attendants followed common practice and opened the flight deck door to tell the flight crew about the fumes. This action exposed the flight crew to the fumes.

The captain's decision not to don his oxygen mask could have resulted in flight crew incapacitation through exposure to smoke or fumes.

The information exchange between the flight crew and ground staff should have indicated a need for portable stairs at the rear door. The decision to disembark the passengers through the forward door was not appropriate. Use of the rear door would have provided passengers and flight attendants better protection from the fumes.

The absence of suitable emergency ground procedures, delay in response from ground staff, and the provision of stairs to only the front door, increased the exposure to fumes for passengers and crew.

Summary

During taxi from the terminal, when the British Aerospace BAe 146-100 was approximately 150 metres from the parking bay, and while making the pre-flight safety public address, a flight attendant began coughing due to a slight irritation in her throat and was unable to finish the presentation. When the second flight attendant went to the front of the cabin to assist, she too developed a cough. Both flight attendants saw what they described as a grey, smoky gas in the airstair region of the left door.

At approximately the same time, the first officer experienced an involuntary cough and stinging eyes and donned an oxygen mask. A short time later a flight attendant opened the flight deck door and advised the flight crew that smoke, or fumes, were filling the forward section of the passenger cabin. The flight crew turned off both air conditioning packs and the Auxillary Power Unit and immediately returned to the parking bay after advising Air Traffic Control and the ground handling company. During the return to the bay, the captain opened the left flight deck window and the flight attendants moved the forward seated passengers to the rear cabin and instructed passengers to cover their nose and mouth.

When the flight crew reported their intention to return to the terminal, the ground handling company requested that passengers remain on board the aircraft at the terminal. The first officer advised the company that this was not possible as there were fumes in the cabin. The aircraft arrived back at the parking bay approximately four minutes after the fumes were first noticed.

Upon arrival at the terminal the captain instructed the flight attendants to open the doors. A flight attendant returned to the front of the aircraft from the rear cabin and opened the forward left door. The second flight attendant opened the rear left door. The flight attendants reported that there were no portable stairs available when the doors were opened. The forward flight attendant called to ground staff in the area and portable stairs were brought to the forward left door. The flight attendants elected not to attempt airstair activation as that was believed to be the source of the smoky gas.

To avoid delay, flight attendants disembarked passengers through the forward door, in the vicinity of the fumes. They reported that, as they were coughing, they could not speak to passengers during the disembarkation.

The company later reported that the urgency of the situation might not have been conveyed to ground services during the initial advice of the aircraft's return to the terminal.

After passengers had disembarked, Aviation Rescue Fire Fighting (ARFF) personnel advised the flight attendants to sit outside the aircraft for ten minutes. The flight attendants later underwent a medical check at the recommendation of the company. Neither the captain nor first officer sought medical attention following the incident. All crewmembers have since returned to duty.

Some passengers later reported that they experienced coughing, watering of the eyes, and respiratory irritation during the event. They also reported that medical attention was not available at the terminal. The ground handling company reported that when passengers reached the terminal, staff did not call a doctor when requested by passengers. They also reported that ARFF personnel had recommended that passengers go outside into the fresh air but few passengers had followed that advice.

Subsequent investigation revealed that neither the operator nor the ground handling company had emergency response procedures in place to cover the situation of an aircraft emergency return to the terminal from a taxi position.

Integral airstair

The aircraft was fitted with an integral stairway (airstair) at the forward left door. However, portable stairs were often used in place of the narrow integral stairs for convenience and ease of boarding.

The operator reported that the forward door airstair had been in use before the flight but had been retracted and replaced by portable stairs prior to boarding passengers.

The airstair was operated from inside the aircraft. It was extended manually, but retracted by hydraulic pressure when the airstair-selector `retract' switch was pressed and held in position. This procedure allowed hydraulic fluid (Skydrol) to pass under pressure through a series of lines and valves to activate airstair retraction. When the airstair was retracted, and the airstair-selector switch was released, the rocker-type switch was designed to spring back to the `off' position. The airstair was then pushed along tracks to a rearward, stowed position out of the doorway.

While the aircraft was on the ground with engines off, an electric stand-by pump was used to top-up and maintain pressure for airstair retraction. After engine start-up, engine driven pumps delivered pressure to the airstair hydraulic system.

An examination of the integral airstair by company engineers revealed that the airstair selector switch had stuck in the `retract' position, and also revealed a failed `o' ring in the retraction jack `banjo' fitting in the airstair actuator. During the examination, other `o' rings had also shown signs of deterioration.

The operator reported that an internal failure caused the switch to be stuck in the `retract' position and also noted that the switch was flush with the surrounding panel. The operator considered it possible that the body of the switch became fouled on the panel and remained in the `retract' position.

The operator also reported that the aircraft maintenance manual stated that the airstair `retract' switch should have had a hinged flap cover. The flap was missing and an engineering order had not been raised for its removal.

Crew emergency procedures and manuals

Flight crew emergency procedures for smoke or fumes required flight deck crew to don oxygen at any time that smoke or fumes were evident. The captain reported that he did not don the oxygen mask when he was alerted to the presence of smoke or fumes as the fumes did not affect him. He also considered it more important to return the aircraft to the parking bay to disembark passengers than to stop and don his oxygen mask.

Flight crew emergency procedures for smoke or fumes also required that the flight deck door remain closed. However, this procedure was not reflected in the flight attendant emergency procedures manual. The flight attendants were unaware of the requirement to keep the flight deck door closed.

Occurrence summary

Investigation number 200102292
Occurrence date 24/05/2001
Location Perth, Aero.
State Western Australia
Report release date 18/09/2002
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer British Aerospace
Model BAe 146
Registration VH-NJY
Serial number E1005
Sector Jet
Operation type Air Transport High Capacity
Departure point Perth, WA
Destination Barrow Island, WA
Damage Nil

Beech Aircraft Corp 200C, VH-KFN

Safety Action

As a result of this occurrence, the Australian Transport Safety Bureau issues the following recommendations:

R20010085

The Australian Transport Safety Bureau recommends that the Civil Aviation Safety Authority review the potential side effects on humans of a mix or cocktail of HFC-134a refrigerant, in its gaseous form, and the associated air conditioning system lubricant. If that review finds the use of such materials is significantly adverse to human health, the use of HFC-134a refrigerant and its associated lubricant as an air conditioning refrigerant in aircraft should also be reviewed.

R20010124

The Australian Transport Safety Bureau recommends that the Civil Aviation Safety Authority advise the aviation industry of the potential side effects on humans of the mix or cocktail of HFC-134a refrigerant, in its gaseous form, and the associated lubricant.

R20010086

The Australian Transport Safety Bureau recommends that the Federal Aviation Administration of the United States review the potential side effects on humans of a mix or cocktail of HFC-134a refrigerant, in its gaseous form, and the associated air conditioning system lubricant. If that review finds the use of such materials is significantly adverse to human health, the use of HFC-134a refrigerant and its associated lubricant as an air conditioning refrigerant in aircraft should also be reviewed.

R20010087

The Australian Transport Safety Bureau recommends that Raytheon Aircraft Company review the potential side effects on humans of a mix or cocktail of HFC-134a refrigerant, in its gaseous form, and the associated air conditioning system lubricant. If that review finds the use of such materials is significantly adverse to human health, the use of HFC-134a refrigerant and its associated lubricant as an air conditioning refrigerant in aircraft should also be reviewed.

Analysis

It was probable that, from the description of the odour detected by the crew, the refrigerant and oil that was found leaking from the forward air conditioning evaporator were the source of fumes inhaled by the crew. The smell of the melting plastic tie and heated insulation material was not directly relevant to the safety problem. Leakage of refrigerant may allow the ingress of moisture into the air conditioning system leading to formation of other hazardous contaminants. Consequently, the fumes inhaled by the crew may have been a mix of refrigerant HFC-134a, oil lubricant and any other contaminants present in the air conditioning system. The symptoms exhibited by the crew were consistent with those described in the MSDS for both the refrigerant and the oil.

The aircraft was cruising at FL250. Under normal conditions, the Beech 200 pressurisation system is designed to provide a cabin pressure altitude of approximately 3,900 ft at an aeroplane operating altitude of 20,000 ft; 9,900 ft at 31,000 ft and 11,700 ft at 35,000 ft. The occurrence flight was operating at an altitude of 25,000 ft, and the aircraft's pressurisation system would have been expected to maintain the cabin altitude at approximately 6,800 ft.

The aircraft's cabin altitude was maintained by restricting the outflow of air from the cabin which would lower the rate at which total cabin air is changed and consequently may have allowed an accumulation of fumes. Additionally, because the cabin pressure was less than sea level, any air conditioning system gas released into the cabin would expose the crew to higher concentrations of contaminant cocktail, particularly in the relatively small cabin volume of a little over 11 cubic metres. Despite the studies conducted by several agencies including the USEPA and the US Navy, it appeared that no research has been performed into the use of HFC-134a or the cocktail of refrigerant and additives in the aviation industry. Extrapolation of the results of the US Navy study appeared to confirm that the release of HFC-134a into an even more confined area such as in an aircraft cabin is likely to be more hazardous.

PAFT noted that the release of the entire refrigerant charge from a domestic refrigerator (6 ounces) into a space the size of the typical kitchen would not pose a risk. This is a space considerably larger than the 11 cubic metres of the aircraft cabin involved in this occurrence. The initial refrigerant loss during the occurrence was an estimated at 1.1 pounds or approximately .5 kg. This represented about 17% of the total refrigerant capacity of the system. If the oil content, in solution with the refrigerant, lost a similar percentage of its total, then the system could have lost about 22 ounces (.625 kg) of its total system content of refrigerant and oil into the cabin. The location of the pipe fracture on the high-pressure side of the system probably resulted in a sudden and total loss of the system contents into the cabin in a very short time. However, the precise rate at which the air conditioning system discharged into the confines of the relatively small aircraft cabin could not be determined. The PAFT recommendation to keep vents open when operating air conditioning systems in automotive vehicles was not an option available to the pilot until the aircraft was depressurised.

The stresses that resulted in the pipe fracture may have been introduced some time prior to the incident during maintenance on the fittings. Access to the fittings is difficult and proper support with tools of both halves of the fitting during the torque fastening procedure was reported as not always possible. This may have been a factor in the fracture of the pipe.

Factual Information

The Beech Super King Air aircraft was maintaining flight level (FL)250 on an aerial ambulance flight, when members of the medical crew advised the pilot that they noticed an unusual burning odour in the cabin, similar to that of a bakery. When the smell became stronger, the pilot elected to return the aircraft to the maintenance facility at Jandakot.

A short time later, in addition to the cooking odour, an odour similar to hot plastic and rubber was smelt by the crew. The medical crew elected to don therapeutic oxygen masks and advised the pilot that the smell had become more intense and that they had now gone onto oxygen. The flight nurse observed that the doctor's complexion had changed to ashen gray and he was leaning against the cabin bulkhead with his eyes closed. The nurse then assisted the doctor to don his oxygen mask. The nurse said that the doctor was in a confused mental state. The nurse only recognised the seriousness of the situation "when the doctor's speech became slurred and was running his words together in their sentences". The nurse stated that his own symptoms manifested very quickly and he "felt quite euphoric and light headed". The nurse also estimated that by the time he donned his own oxygen mask, he was rapidly approaching unconsciousness. The pilot donned his oxygen mask and, when he feared he may be sick in his mask, initiated an emergency descent to 10,000 ft. During the descent he depressurised the cabin in an attempt to clear the fumes.

The crew reported that the fumes in the cabin had caused them to experience nausea and confusion soon after they detected the smell. They remained on oxygen for the rest of the flight.

The pilot reported that while inbound he had asked Air Traffic Services (ATS) to repeat instructions on several occasions and this prompted ATS to ask him to confirm that operations were normal. He did not recognise any of the landmarks that he usually used to identify his correct track while on approach to Jandakot. He stated that on that occasion his vision was affected to the extent that he had great difficulty focussing outside the cockpit. The pilot said that following the emergency descent to 10,000 ft, he engaged the autopilot and changed the GPS to the coordinates for Jandakot. The aircraft autopilot then flew the GPS guided track to abeam Jandakot from where the pilot took control and conducted the landing. He could not recall anything about the approach and landing, and later had to ask the flight nurse if he had used any flap, because the flaps were in the retracted position after landing and he did not remember retracting them. After landing, the crew's symptoms did not significantly improve and they were taken to hospital for medical assessment.

Several months after the occurrence, some members of the crew reported to the ATSB that they were still suffering various residual effects including headaches, elevated blood pressure, reduced concentration levels and anxiety. They attributed the symptoms to their exposure to the fumes encountered on the occurrence flight.

A maintenance investigation following the occurrence discovered several air conditioning system defects. A bleed air pressure-reducing valve in the under-floor cabin area was found to be leaking hot bleed air onto an adjacent air conditioning duct. There was also evidence that the insulation was heat affected and had discoloured from the bleed air leak. A "spirap" type loom bundling plastic tie was also found in the vicinity, which had been melted. Samples of those heat-affected items were taken by the ATSB and forwarded to a laboratory for testing, to identify if heat application produced any emissions. The results of that testing and subsequent instrumented flight test showed that the bleed air leak did not reach a sufficiently high enough temperature to be considered a source of hazardous fumes in this incident.

In addition to the faulty reducing valve, two air conditioning refrigerant leaks were detected in the forward air conditioning evaporator refrigerant pipes. Airconditioning compressor lubricating oil was also observed on the evaporator and dripping from a fractured flared fitting onto the surrounding structure. The fitting was located on a pipe that delivered high pressure liquid refrigerant to the expansion valve and evaporator. When the system refrigerant was replenished during the maintenance investigation, it was noted that a considerable quantity of refrigerant was required to refill the system. The initial refrigerant loss was estimated as at least 1.1 pounds or approximately 0.5 kg. As the lubricating oil level could not be determined with any accuracy, maintenance personnel then decided to totally evacuate the system and replenish refrigerant and oil levels from empty. The nature of the leak, troubleshooting and repairs precluded an accurate measurement of the total oil and refrigerant quantities that had escaped and the initial estimate would have been the minimum system loss incurred from the leak. The pipes and fittings to the evaporator were located in a confined space to which proper access for some maintenance activities was very difficult.

The vapour cycle type air conditioning system in the aircraft used a new environment-friendly refrigerant HFC-134a instead of the ozone depleting refrigerant type R12 that had been in service for many years. The design of the vapour cycle systems was such that a significant amount of the oil lubricant for the air conditioning compressor was in solution with the refrigerant. The polyol ester-based lubricating oil had a particular odour when heated, which was similar to the smell detected by the crew.

The Material Safety Data Sheet (MSDS) for HFC-134a stated, "overexposure can cause central nervous system depression with dizziness, confusion, incoordination, drowsiness or unconsciousness. Irregular heartbeat with a strange sensation in the chest, `heart thumping', apprehension, light-headedness, feeling of fainting, dizziness, weakness, sometimes progressing to loss of consciousness and death. Suffocation if air is displaced by the refrigerant vapours".

The MSDS for the polyol ester-based lubricating oil that was used in conjunction with the refrigerant charge stated that inhalation may cause nasal respiratory irritation and dizziness. The operator's engineering manager also stated that the lubricating oil was known to produce valeric acid when heated which was known to cause dizziness and nausea. He stated that prolonged exposure could lead to unconsciousness. The MSDS sheet supported that. In addition to the refrigerant charge of 104 ounces or almost three kg of HFC-134a, the air conditioning system was also charged with 34 ounces or almost one kg of polyol ester oil, of which approximately 26 ounces or almost 75% was held in solution with the refrigerant gas/liquid.

In addition to the refrigerant and oil chemicals, the airframe manufacturer had a maintenance warning that when moisture entered the air conditioning system, it could cause the formation of hydrofluoric acid or hydrochloric acids. The MSDS data for those compounds gave warnings of eye irritations and burns when exposed to the mist or vapours.

The Programme for Alternative Flurocarbon Toxicity (PAFT) found in 1987 that the HFC-134a refrigerant exhibited a very low risk and was considered to be "practically non-toxic". The PAFT tests stated that at very high concentration levels (over 50%), exposure could sensitise the heart to adrenaline and that it could cause irregular heartbeat, even death.

A 1998 University of New South Wales (UNSW) study on the use of HFC-134a in the confined space of motor vehicles concluded that the refrigerant posed a considerable risk to vehicle occupants. It cited two scientific reports in the United States and four scientific papers in peer reviewed journals describing adverse effects expected from human inhalation as all being "scientifically consistent". The study recommended that fresh air vents be kept open at all times when using the air conditioning system and to introduce a pungent odour producing element into the systems to aid in the early detection of refrigerant leaks.

The United Sates Environmental Protection Agency (USEPA) and the US Navy Bureau of Medicine commissioned research to determine safe levels of exposure to HFC-134a. The studies concluded with statements of significantly different safe exposure values. The US Navy-determined levels of acceptable exposure were significantly lower than the values assessed by the USEPA. The US Navy research into the exposure of humans to HFC-134a was conducted in a confined area to simulate the confines of a submarine.

Although there was research data available on HFC-134a and polyol ester-based lubricants, at the time of preparing this report, the ATSB could not find any data on the effects of exposure to HFC-134a at air pressures less than sea level. Similarly, the ATSB could not find data on exposure to a mix or "cocktail" of the two agents HFC-134a and polyol ester lubricants at air pressures at sea level or less than sea level.

Occurrence summary

Investigation number 200005948
Occurrence date 02/12/2000
Location 102 km W Southern Cross
Report release date 21/12/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Serious Incident
Highest injury level Minor

Aircraft details

Manufacturer Beech Aircraft Corp
Model 200
Registration VH-KFN
Serial number BL-31
Sector Turboprop
Operation type Aerial Work
Departure point Jandakot, WA
Destination Kalgoorlie, WA
Damage Nil

Boeing 767-338ER, VH-OGQ

Factual Information

The ATSB did not conduct a technical investigation of this incident. The report has been compiled with the aid of information provided by the airline operator.

While en route from Sydney to Melbourne at flight level (FL) 410, fumes were detected in the flight deck and an aft toilet smoke detector was activated by smoke haze in the rear of the aircraft. The crew carried out the appropriate non-normal procedures and diverted the aircraft to Canberra as a precautionary measure. During the descent the engines were at idle thrust and the fumes decreased in intensity.

Engineering staff carried out a series of checks on the aft galley and the air conditioning, electrical and powerplant systems. No defects were found and the aircraft was then ferried to Sydney for further checks. No fumes were evident during the flight at FL230 nor during the subsequent engine ground runs. The aircraft was returned to service and operated for eight sectors without incident.

Two days later, the fumes were again detected as the aircraft climbed through FL410 en route from Sydney to Melbourne. The flight crew carried out the non-normal checklist for "Smoke or Fumes Air Conditioning" and the aircraft was turned back to Sydney. Following that incident, engineering staff carried out inspections of the pneumatic ducting and the air conditioning system. No evidence of oil contamination was found in the pneumatic system. Hydraulic reservoir pressurisation modules and recirculation filters were replaced and an assessment flight was then conducted. The take-off and climb phases of flight were uneventful but as the aircraft was levelled out at FL416, an acrid odour became apparent in the cabin and flight deck. An isolation procedure was initiated which traced the source of the odour to the right pneumatic distribution system and the right air conditioning system. Following that flight, the right engine was changed.

During a second assessment flight, the odour re-occurred in the cabin as the aircraft was flown above FL410. By using a sequence of bleed air conditions, in which each pack was operated independently and from each engine bleed system in turn, the source of the odour was isolated to the right air conditioning pack system. A subsequent ultraviolet light inspection of the pneumatic ducting indicated that the pneumatic ducting was free of engine and hydraulic oil contamination.

Various components of the right air conditioning system were removed and replaced including the air cycle machine (ACM), water separator, condenser, reheater and primary and secondary heat exchangers. An inspection of those components revealed a black deposit on the ACM compressor wheel and 500 mL of brown fluid in the right secondary heat exchanger. The secondary heat exchanger and downstream components were also found to emit the same odour as that noted during the assessment flights. The secondary heat exchanger had undergone a complete overhaul in July 2000, at a contracted repair facility in the United States, before being returned to the operator. The contractor's internal process review revealed that there were differing processing requirements in regard to the coating applied to the exchanger for corrosion protection. During a strip and repaint of the exchanger, the protective coating was baked at a significantly lower temperature than if the exchanger had been completely re-cored.

The right air conditioning components were replaced and a further assessment flight was conducted. No odours were evident at any altitude or operating condition during the flight. The aircraft was then returned to service and subsequently operated without incident.

A sample of the brown fluid recovered from the secondary heat exchanger was independently analysed using infra-red spectroscopy. The results of the analysis indicated that the primary contaminant was sodium polyacrylate, a water treatment chemical. Material Safety Data Sheets for products containing that chemical indicated that inhalation of the compound in vapour/mist form may cause irritation to mucus membranes. Further analysis using gas chromatography/mass spectrometry did not show the presence of sodium polyacrylate but indicated a range of numerous phenol-based compounds that would produce offensive odours. The discrepancy between the results of the two sets of tests could not be explained. A consultant occupational hygienist, experienced in cabin air quality testing, was unable to determine the potential for the contaminants exiting the air conditioning system to cause harm to either the passengers or the crew on the aircraft.

Maintenance records indicated that the secondary heat exchanger had been installed in the aircraft on 18 September 2000. Following installation, the aircraft flew 30 sectors before the fumes incident on 30 September 2000. Data was not available on the levels flown on those sectors but the operator indicated that it was probable that they were flown below FL410. Following the engineering work after the first incident, the aircraft was released back to line and operated eight domestic and international sectors without any cabin air quality problems becoming evident. The levels flown ranged from FL290 to FL390. The second fumes incident on 02 October 2000, occurred when the aircraft climbed to FL410. Between FL410 and FL431 (the maximum certified altitude for the aircraft) the air conditioning system was operating under the highest design load condition with several components running at high temperature.

Safety Action

Local safety action

Following the incidents, the contractor amended the heat exchanger overhaul process so that all exchangers were baked at a higher temperature in order to break down any possible contaminants. Additionally, forced ventillation was introduced during the baking process to ensure that any fumes were flushed from the exchangers and not allowed to recondense on the exchanger surfaces. As of 1 April 2002, no further incidents of this type had been reported to the ATSB.

Analysis

The source of the fumes was probably the result of heating of chemical compounds contained in the secondary heat exchanger that was fitted to the aircraft on 18 September 2000. The compounds contained in the secondary heat exchanger apparently decomposed under high temperatures in the heat exchangers, resulting in the contamination of the cabin and flight deck air supply. The investigation was unable to positively determine the origin of those compounds but it appears that they were introduced at some stage during the overhaul of the secondary heat exchanger.

Summary

While en route from Sydney to Melbourne at flight level (FL) 410, fumes were detected in the flight deck and an aft toilet smoke detector was activated by smoke haze in the rear of the aircraft. The crew carried out the appropriate non-normal procedures and diverted the aircraft to Canberra as a precautionary measure. During the descent the engines were at idle thrust and the fumes decreased in intensity.

Occurrence summary

Investigation number 200004432
Occurrence date 30/09/2000
Location Canberra, Aero.
State Australian Capital Territory
Report release date 23/05/2002
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer The Boeing Company
Model 767
Registration VH-OGQ
Serial number 28154
Sector Jet
Operation type Air Transport High Capacity
Departure point Sydney, NSW
Destination Melbourne, VIC
Damage Nil

Boeing 767-338ER, VH-OGC

Safety Action

As a result of the investigation into this occurrence, the Australian Transport Safety Bureau has simultaneously issued Safety Advisory Notices 20000278 and 20000279 to the Civil Aviation Safety Authority and the Federal Aviation Administration respectively. These advisories suggested the Civil Aviation Safety Authority and the Federal Aviation Administration take appropriate action to mandate compliance with Service Bulletins DME 700-34-10, 17, 23, 34, and 35.

Any responses received to these Safety Advisory Notices will be published on the ATSB website at the conclusion of the investigation.

Summary

The Boeing 767 had just reached cruise altitude at flight level 330 approximately 40 minutes out of Singapore enroute to Perth, when the flight crew noted smoke and electrical fumes on the flight deck. The source of the smoke and fumes could not be readily identified. The pilot in command elected to have the flight crew don oxygen masks, and diverted to Jakarta.

The operator's engineering personnel examined the aircraft and found the right DME (Distance Measuring Equipment) circuit breaker open. Technicians isolated the problem to the right DME interrogator unit. The malfunctioning DME unit was disabled in accordance with the MEL (Minimum Equipment List) guidelines to allow the aircraft to continue to Perth. Following arrival in Perth, the unit was replaced.

Examination of the unit by the manufacturer revealed that the DME unit's A5 modulator had overheated. This failure mode was similar to two other units, which had overheated on a different aircraft in January 2000 (see Occurrence 200000055). The failure mode of those units was such that the A5 modulator had overloaded the positive 86 volt DC power supply and overheated the power transformer. Compliance with service bulletins recommending product improvements to this unit were not mandatory, and the recommended modifications had not been incorporated into this unit, or the previous two units that had sustained failures.

Occurrence summary

Investigation number 200003857
Occurrence date 06/09/2000
Location 489 km ESE Singapore Jatcc, Aero.
State International
Report release date 03/04/2001
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer The Boeing Company
Model 767
Registration VH-OGC
Serial number 24317
Sector Jet
Operation type Air Transport High Capacity
Departure point SINGAPORE
Destination Perth, WA
Damage Nil

Saab SF-340B, VH-KDQ

Summary

Due to intermittent reports of smells in the cockpit associated with bleed air from the right engine, first reported on 4 July 2000, a compressor wash had been carried out on the engine and the crew had been requested to report further.

The crew subsequently reported a strong smell in the cockpit at times during climb, cruise and descent. The smell was accompanied by an oily taste in the mouth with general ill feeling and headaches. The symptoms abated after the right engine bleed air was turned off.

The operator reported that there have been no further reports. However, the engine has been scheduled for removal and return to the manufacturer for further investigation as a defective internal engine oil seal is suspected.

Occurrence summary

Investigation number 200003428
Occurrence date 24/07/2000
Location 37 km N Sydney, Aero.
State New South Wales
Report release date 21/09/2000
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Incident
Highest injury level None

Aircraft details

Manufacturer Saab Aircraft Co.
Model 340
Registration VH-KDQ
Serial number 340B-325
Sector Turboprop
Operation type Air Transport Low Capacity
Departure point Sydney, NSW
Destination Coffs Harbour, NSW
Damage Nil

Piper PA32/260 Cherokee Six, VH-BIC, Simpson Desert, NT, 24 August 1970

Summary

Approximately thirty minutes after departure a peculiar odour was noticed in the cabin which the pilot attributed to a boiling battery. He turned off the master switch and, since the odour then partially dissipated, continued the flight and advised that he would only use the aircraft's electrics to report at scheduled times. However, as the flight progressed, the fumes in the cabin became so obnoxious that a forced landing became imperative. The pilot advised his intentions and landed on a lone small claypan but over-ran into the surrounding uneven sand. During the landing the forward baggage compartment door flew open and portions of a burning foam plastic mattress fell out, igniting small spinifex bushes. After disembarkation, the fire, now obviously in the baggage compartment, was quickly extinguished and the spinifex fires were trampled out. The investigation established that a rolled foam mattress, which was the last item loaded at Birdsville, partially unravelled itself in flight and contacted the illuminated hot naked bulb in the baggage compartment light causing the foam to smoulder and emit acrid smoke and fumes which were carried back to the cabin. The composition of the foam was such that the smouldering would continue even when the heat source was removed but it is probable that the mattress did not burst into flames until the door flew open during the landing roll.

Occurrence summary

Investigation number 197003828
Occurrence date 24/08/1970
Location Simpson Desert
Report release date 10/04/1972
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Fumes
Occurrence class Accident
Highest injury level None

Aircraft details

Manufacturer Piper Aircraft Corp
Model PA-32
Registration VH-BIC
Operation type Business
Departure point Birdsville
Destination Alice Springs
Damage Substantial

Fumes event involving a Gippsland Aeronautics GA-8, Elcho Island, Northern Territory, on 5 May 2020

Brief

Occurrence Briefs are concise reports that detail the facts surrounding a transport safety occurrence, as received in the initial notification and any follow-up enquiries. They provide an opportunity to share safety messages in the absence of an investigation.

What happened

On 5 May 2020, a Gippsland Aeronautics GA-8 was scheduled to operate a charter flight from Elcho Island to Ramingining, Northern Territory.

During the boarding process, the pilot asked the single passenger whether there were any dangerous goods in their luggage. The passenger proceeded to check the luggage and willingly handed over two spray cans with flammable contents. Following this, the pilot loaded the luggage into the aircraft.

As the aircraft climbed through approximately 4,000 ft, fumes were detected in the cabin described as smelling of solvent. At this time, the pilot became light-headed and adjusted the air vent to ensure fresh air was coming into the cabin. The pilot directed the passenger to check through the luggage for the source of the fumes. The passenger returned with a plastic container of glue, which had subsequently leaked. The pilot completed the fumes checklist and jettisoned the container safely out of the aircraft while operating over water.

Safety message

This incident highlights the importance of ensuring that all items taken on board an aircraft do not pose a safety risk to the flight. More information regarding dangerous goods can be found on the CASA website, including the Can I pack that? dangerous goods app for passengers.

About this report

Decisions regarding whether to conduct an investigation, and the scope of an investigation, are based on many factors, including the level of safety benefit likely to be obtained from an investigation. For this occurrence, no investigation has been conducted and the ATSB did not verify the accuracy of the information. A brief description has been written using information supplied in the notification and any follow-up information in order to produce a short summary report, and allow for greater industry awareness of potential safety issues and possible safety actions.

Occurrence summary

Mode of transport Aviation
Occurrence ID AB-2020-021
Occurrence date 05/05/2020
Location Elcho Island
State Northern Territory
Occurrence class Incident
Aviation occurrence category Fumes
Highest injury level None
Brief release date 25/06/2020

Aircraft details

Manufacturer Gippsland Aeronautics Pty Ltd
Model GA-8
Sector Piston
Operation type Charter
Departure point Elcho Island, Northern Territory
Destination Ramingining, Northern Territory
Damage Nil