Flight control systems involving a Boeing 737-377, VH-CZP, Melbourne, Victoria, on 29 May 1994

199401449

Summary

More than usual forward trim was required during and after take-off. The autopilot trim actuator ran out of forward trim and then ran continuously to full aft. The crew were unable to adequately manually trim forward. The aircraft returned for a normal descent and landing.

The autopilot Mach trim actuator was found to be inoperative. The actuator had been fitted during overnight maintenance and the observed problem occurred on the first flight after installation. Ground test procedures after installation had not shown up any problems.

Workshop rectification found anomalies with the backlash on the jackscrew and with the actuator length. The manufacturer advised that these anomalies would not have caused the problem that was experienced.

The actuator was refitted four days after the workshop check and has since operated satisfactorily. The cause of the inflight problem was not discovered.

Occurrence summary

Investigation number 199401449
Occurrence date 29/05/1994
Location Melbourne
State Victoria
Report release date 29/08/1994
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Flight control systems
Occurrence class Incident

Aircraft details

Manufacturer The Boeing Company
Model 737-377
Registration VH-CZP
Sector Jet
Operation type Air Transport High Capacity
Departure point Melbourne Vic
Damage Nil