On 12 October 2016, a Vee H Aviation Fairchild Industries Inc. SA227-DC, registered VH-VEU, conducted a regular public transport flight from Armidale, New South Wales, to Brisbane, Queensland. On board the flight were two flight crew and 13 passengers.
At 0755 Eastern Daylight-saving Time, the aircraft was about 170 km south of Brisbane, when the aircraft suddenly yawed to the right. The flight crew confirmed the right engine was not delivering power and then shut down the right engine and feathered the right propeller. During the diagnosis, the flight crew noted that all right engine indications were normal except for a low torque reading and low fuel flow.
Air traffic control contacted the crew to confirm they were maintaining their altitude and the captain responded with a PAN broadcast that they were descending due to a right engine failure. The crew then requested, and were given, a direct track to Brisbane Airport from air traffic control. They completed their normal and single engine landing checklist procedures and landed at Brisbane Airport runway 19 without further incident.
Following the aircraft yaw, the flight crew actively employed their crew resource management procedures to identify and confirm the engine fault and then shut down the right engine. The use of these procedures reduced the risk of an incorrect diagnosis of the fault or activation of the incorrect engine controls during shut down.
Aviation Short Investigations Bulletin - Issue 57
What happened
On 12 October 2016, a Vee H Aviation Fairchild Industries Inc. SA227-DC, registered VH-VEU, conducted a regular public transport flight from Armidale, New South Wales, to Brisbane, Queensland. On board the flight were two flight crew and 13 passengers. The captain was the pilot flying (PF) and the first officer was the pilot monitoring (PM).[1]
At 0755 Eastern Daylight-saving Time (EDT), the aircraft was about 170 km south of Brisbane, cruising at FL 170,[2] when the aircraft suddenly yawed to the right.[3] The PF re-stated they had command of the aircraft and directed the PM to identify the failure. The flight crew then employed their ‘identify and confirm’ crew resource management (CRM) procedures to confirm the right engine was not delivering power and then shut down the right engine and feathered the right propeller.[4] During the diagnosis, the PM noted that all right engine indications were normal except for a low torque reading (10%) and low fuel flow (140 pounds per hour).
Air traffic control contacted the crew to confirm they were maintaining FL 170 and the PM responded with a PAN broadcast[5] that they were descending due to a right engine failure. The crew reviewed their options and decided to continue to Brisbane Airport. They completed the remaining checklist actions and briefed the passengers. The crew then requested, and were given, a direct track to Brisbane Airport from air traffic control. They completed their normal and single engine landing checklist procedures and landed at Brisbane Airport runway 19 without further incident.
Maintenance findings
The engine installed in the aircraft was the Honeywell (previously Garrett) TPE331-12UHR-701G. The operator’s engine maintenance organisation found a retainer ring within the engine accessory gear assembly had failed, which allowed the main shaft (which drives the propeller) to de-couple from the engine driven reduction gearbox (Figure 1).
The retainer ring was shipped to the maintenance organisation from Honeywell in December 2008 as part of a batch of 10 with a certificate of conformance from the part manufacturer and Honeywell. It was fitted new to the incident engine in December 2009 at the last engine overhaul, about 2,429 hours prior to the failure. The maintenance organisation introduced this practice of replacing the retainer ring at each overhaul based upon their previous service experience of this part failing. December 2009 was the last overhaul of the accessory gear assembly prior to the failure.
In October 2015, Honeywell added temporary revision 72-241 to the maintenance manual procedure: removal and installation of accessory gear assembly, to direct the replacement of the retainer ring at each exposure. Figure 2 depicts the failed retainer ring.
Figure 1: Engine accessory gear assembly

Source: Maintenance organisation, annotated by ATSB
Figure 2: Retainer ring

Source: Operator
Continuing airworthiness maintenance interval
The operator set their maintenance interval for the incident engine in accordance with the engine manufacturer’s service bulletin for periodic inspections, (Honeywell TPE 331-72-0476). From the service bulletin, the operator set the inspection of the engine at the 7,000 hour continuing airworthiness maintenance (CAM) interval with gearbox inspection, for commercial operations. This included the requirement for the accessory gear assembly inspection in accordance with the maintenance manual procedures at the 7,000 hour interval.
The operator’s spectrometric oil-analysis programme (SOAP analysis) was set at 150 hour intervals at the time of the incident.[6] The previous SOAP analysis was conducted at about 26 hours prior to the failure and did not detect any anomalies. Further information on SOAP is available from Civil Aviation Safety Authority airworthiness bulletin (AWB 79-1): Spectrographic oil analysis program (SOAP).
The gearbox is fitted with a single magnetic drain plug (chip detector).[7] If a metallic particle is detected by the chip detector inflight, it will activate a caution light to advise the flight crew. The inspection interval for the chip detector is set at 300 hours. The last inspection was about 144 hours prior to the incident and no anomalies were found. There were no activations of the chip detector between the last scheduled inspection and the incident flight, and the chip detector did not activate during the incident flight.
The operator also conducts propeller dynamic balance checks at 600 hour intervals. There have been no out-of-limit vibration indications since engine installation. The last check was performed 17 September 2016.
Safety analysis
The operator had several preventive maintenance inspections in place, which included an overhaul of the gearbox, SOAP analysis, magnetic drain plug inspection and propeller dynamic balance. The previous overhaul was about 2,429 hours prior to the failure at which time the retainer ring was fitted new to the gearbox. During the time interval to failure of the retainer ring, the SOAP analysis, magnetic drain plug inspections and propeller dynamic balance checks did not detect any anomalies. Therefore, the failure of the retainer ring was within the required gearbox inspection intervals and without prior warning of an impending failure.
Findings
These findings should not be read as apportioning blame or liability to any particular organisation or individual.
- The retainer ring failed within the prescribed maintenance interval.
- There was no prior warning of an impending failure of the retainer ring.
Safety action
Whether or not the ATSB identifies safety issues in the course of an investigation, relevant organisations may proactively initiate safety action in order to reduce their safety risk. The ATSB has been advised of the following proactive safety action in response to this occurrence.
Operator
As a result of this occurrence and subsequent to an update by the engine manufacturer to the engine manufacturer’s service bulletin, the aircraft operator has advised the ATSB that they are taking the following safety actions:
SOAP analysis
The operator reduced their SOAP analysis interval from 150 hours to 100 hours.
Damaged parts
The damaged parts from the gearbox were sent to the engine manufacturer for analysis.
Safety message
Following the aircraft yaw, the flight crew actively employed their crew resource management procedures to identify and confirm the engine fault and then shut down the right engine. The use of these procedures reduced the risk of an incorrect diagnosis of the fault or activation of the incorrect engine controls during shut down.
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