Propeller/rotor malfunction involving a Saab SF-340B, VH-TCH, Cudal, New South Wales, on 5 August 1994

199402191

Summary

During take-off the crew noticed a small surge on the right engine torque indicator, with no noticeable power change. Shortly after lift-off, as the landing gear was retracting, the right engine torque suddenly increased to 107%. The power lever, although extremely stiff to move, was eventually retarded until the torque was reduced to 85%. By this time the auto coarsen system had commanded the propeller RPM to zero and the engine was shut down. The flight continued to Orange where an uneventful single engine landing was carried out.

Subsequent investigation revealed the right engine Beta tube had failed where it entered the Propeller Control Unit (PCU). The remains of the tube were jammed in the PCU, which was stiff to operate at the power lever input shaft.

Investigation by the manufacturer attributed the failure to localised pick up and seizure of the PCU Beta Sleeve to the Beta Tube Unit Sleeve, resulting from a reduction below the minimum diametrical clearance between the two components. This was due to an incorrectly formed undercut in the Beta Rack during manufacture, which prevented satisfactory location between the two components, and subsequent distortion of the sleeve.

The manufacturer has instigated an inspection requirement for Beta Racks from the same batch number and advised that future batches will be examined prior to assembly.

Occurrence summary

Investigation number 199402191
Occurrence date 05/08/1994
Location Cudal
State New South Wales
Report release date 08/05/1995
Report status Final
Investigation type Occurrence Investigation
Investigation status Completed
Mode of transport Aviation
Aviation occurrence category Propeller/rotor malfunction
Occurrence class Incident

Aircraft details

Manufacturer Saab Aircraft Co.
Model SF-340B
Registration VH-TCH
Sector Turboprop
Operation type Air Transport Low Capacity
Departure point Cudal NSW
Destination Orange NSW
Damage Nil