Summary
The pilot reported EICAS messages R Gen OFF, L Util Bus and R Util Bus.
Subsequently, acrid smoke entered the flight deck and cabin. Smoke removal procedures were effective.
The APU would not start at FL390, so the pilot informed ATC of the failed right generator and requested FL350 at 1633 WST. At 1638, the pilot advised ATC of smoke in the cabin, the second occurrence, and requested FL310 as the APU still would not start.
At 1649 the pilot advised ATC that the smoke had cleared and that operations were normal.
When power was reduced for the final descent, an EICAS message R Gen Drive came on. The right generator was then disconnected.
Following selection of flap 30 for landing, an unusual airframe judder was felt until touchdown.
The generator failure was traced to a lack of oil. No reason for the airframe judder could be determined.
Occurrence summary
| Investigation number | 199501370 |
|---|---|
| Occurrence date | 06/05/1995 |
| Location | 440 km north of Perth |
| State | Western Australia |
| Report release date | 17/08/1995 |
| Report status | Final |
| Investigation type | Occurrence Investigation |
| Investigation status | Completed |
| Mode of transport | Aviation |
| Aviation occurrence category | Fumes |
| Occurrence class | Incident |
Aircraft details
| Manufacturer | The Boeing Company |
|---|---|
| Model | 767-238ER |
| Registration | VH-EAL |
| Sector | Jet |
| Operation type | Air Transport High Capacity |
| Departure point | Den Pasar Indonesia |
| Destination | Perth WA |
| Damage | Nil |