Summary
The pilot reported hearing a snapping sound during landing gear retraction and subsequently confirmed that the nose gear had not fully retracted. Flight Service were advised of the problem and the aircraft diverted to Bankstown. An uncertainty phase was declared and emergency procedures implemented. The aircraft subsequently made an emergency landing, during which the nose gear collapsed.
Subsequent investigation determined that the nose gear actuating rod end had failed from fatigue cracking. The fatigue had initiated from a pre-existing crack. It is likely that the original crack had originated from a previous nose gear collapse in October 1993 when the aircraft had collided with a kangaroo.
Occurrence summary
| Investigation number | 199401906 |
|---|---|
| Occurrence date | 15/07/1994 |
| Location | Bankstown |
| State | New South Wales |
| Report release date | 26/08/1994 |
| Report status | Final |
| Investigation type | Occurrence Investigation |
| Investigation status | Completed |
| Mode of transport | Aviation |
| Aviation occurrence category | Wheels up landing |
| Occurrence class | Accident |
Aircraft details
| Manufacturer | Beech Aircraft Corp |
|---|---|
| Model | E55 |
| Registration | VH-USP |
| Sector | Piston |
| Operation type | Charter |
| Departure point | West Wyalong NSW |
| Destination | Bankstown NSW |
| Damage | Substantial |