Investigation number
198702410
Occurrence date
Location
Bankstown
Report release date
Report status
Final
Investigation type
Occurrence Investigation
Investigation status
Completed
Aviation occurrence type
Wheels up landing
Occurrence category
Accident
Highest injury level
None

Following a normal approach for a night landing, touchdown was made on the main landing gear. The pilot then noticed that the nose was lowering by an excessive amount, and he carried out a successful go around. Examinations from the ground and from a helicopter equipped with a searchlight revealed that the nosegear was inclined at about 30 degrees to the vertical. The position of the nosegear did not alter when the gear was cycled. After all attempts to lower the nosegear were unsuccessful, the pilot elected to carry out a landing with the maingear retracted. He was unable to use the grass flight strip alongside the lighted runway because of obstructions, and chose to land on an unlit strip. The left engine failed because of fuel exhaustion when the aircraft was on final approach. After touchdown, the aircraft slid off the end of the strip and came to rest against the boundary fence. It was determined that the nosegear retract rod plunger had failed from fatigue, resulting in the nosegear being isolated from the remainder of the landing gear system.

Aircraft Details
Departure point
Bankstown NSW
Destination
Sydney NSW
Model
55
Serial number
TE-592
Registration
VH-MKE
Operation type
Charter
Damage
Substantial
Manufacturer
Beech Aircraft Corp
Departure time
2101