On 22 October 2004, at approximately 1910 Universal Co-ordinated Time, a Boeing Company 747-338 aircraft, registered VH-EBU, was being operated on a scheduled passenger service from Honolulu, in the United States of America, to Sydney, Australia. The flight crew had been cleared by air traffic control to climb from flight level (FL) 340 to FL360. When the crew set climb thrust on the engines, they reported that they felt a vibration in the aircraft and the number-3 engine airborne vibration monitor lights illuminated, indicating that the number-3 engine had an abnormal vibration level. The crew shut down the number-3 engine and continued to Sydney.
A subsequent engineering examination of the number-3 engine indicated that a low pressure turbine (LPT) second stage blade had failed. The ATSB examination revealed that the LPT blade had failed as a result of high cycle fatigue originating at a site of an anomalous inclusion in the blade material.
On 22 October 2004, at approximately 0510 Australian Eastern Standard Time, an Australian registered (VH-EBU), Boeing Company 747-338 aircraft, was being operated on a scheduled passenger service from Honolulu, in the United States of America, to Sydney, Australia. Near the instrument flight rules reporting point ISTEM, located approximately 700 nautical miles north-east of Sydney, the flight crew had been cleared by air traffic control to climb from flight level (FL) 340 to FL360. When the crew set climb thrust on the engines, they reported that they felt a vibration in the aircraft and the number-3 engine airborne vibration monitor lights illuminated, indicating that the number-3 engine had an abnormal vibration level. The crew shut down the number-3 engine and continued to Sydney.
A subsequent engineering examination of the number-3 engine indicated that a low pressure turbine (LPT) second stage blade had failed. The engine, a Rolls-Royce RB211-524D4 turbofan, serial number 12682, was removed from the aircraft and the recovered LPT blade fragments were sent to the Australian Transport Safety Bureau (ATSB) for detailed examination. At the time of the failure, the engine had a recorded time in service of 71,200 hours and 11,221 cycles since new and 14,787 hours and 2,513 cycles since repair. The ATSB examination revealed that the LPT blade had failed as a result of high cycle fatigue cracking (HCF), originating at an anomalous inclusion in the blade material. Details of the failed LPT blade examination are contained in the Technical Analysis report (Appendix A).
Previous LPT blade failures
The engine manufacturer reported that there had been three previous LPT blade failures in this engine type. Two of the events were attributed to engine fuel mal-distribution and subsequent blade excitation, leading to HCF and failure. There was no detail provided on the third event. The failure of this blade type was a rare event, given that the engine type has accumulated in excess of 25 million flight hours in service.
LPT blade life monitoring
The LPT blades in the Rolls-Royce RB-211 series engines do not have a defined blade retirement life and are maintained on condition; being monitored throughout their service life by inspection and engine trend analysis. Once the engine LPT performance parameters change to pre-determined levels, the engine is removed for overhaul or repair. During engine overhaul, the LPT blades are subject to inspections to determine if they meet the dimensional requirements for continued service. LPT blades may be exchanged between various engines during this process.
The engine manufacturer's Time Limits Manual for RB211-524 series engines specified that LPT blades are 'Group B' parts and states that it is 'considered necessary to life mark or maintain life records of Group B parts'. While it was evident that engine serial number 12682 had been overhauled in accordance with the manufacturer's requirements, the individual LPT blades' service lives were not recorded and so the age and life history of the failed blade could not be determined.
The number-3 engine failed in flight as a result of a low pressure turbine (LPT) second stage blade failure. The blade failure was a result of a fatigue crack that propagated from a casting inclusion formed during blade manufacture.
Despite the engine manufacturer's recommendations regarding the maintenance of life records for Group B components, the LPT blades are not subject to any mandatory life recording program, and so the actual time and hours in service cannot be determined for any individual blade. In addition, unless the life of each blade is recorded from new, the introduction of any life recording program to components already in-service would not be of any benefit.
1. FACTUAL INFORMATION
1.1. Examination brief
During a climb to a new cruise level with maximum climb thrust set, the flight crew of a scheduled passenger service Boeing 747-338 aircraft noted an increase in vibration from the number-3 engine, accompanied by warning indications from the engine monitoring instrumentation. The engine was shut down and the flight continued to its destination.
Subsequent engineering examination of the RB211-524D2 engine (serial number 12682) revealed the failure of a single blade from the low-pressure turbine second stage (LPT-2, figure 1). Sections of the failed blade, including the root block, and portions of the separated airfoil section were recovered from the engine and forwarded to the Australian Transport Safety Bureau (ATSB) for examination (figure 2).
Figure 1: RB211-524 engine profile showing location of LPT-2 blades (coloured)
Figure 2: Blade fragments recovered from the failed engine
1.2. Visual characterisation
The part number LK83851 stage-2 low-pressure turbine blade (serial number TA6939B) had fractured through the base of the airfoil section; the fracture path extending diagonally from just above the dovetail transition at the rear face, to a position approximately 33 mm above the blade base, measured along the forward face (figure 3).
Figure 3: LPT-2 blade root section showing the fracture profile and its point of origin (arrowed)
The entire fracture was confined to the region beneath the blade platform and airfoil section transition. The fracture surface morphology confirmed a progressive fatigue cracking mechanism (figure 4), with optical and electron microscopy identifying a single origin approximately 790 µm from the rear face of the root block (figures 5 - 7).
Figure 4: Plan view of the blade fracture showing the fatigue cracking morphology and point of initiation
Figures 5 - 7: Blade fracture at increasing magnifications with origin identified
Other than mechanical damage attributable to the loss of the outer blade section, the blade root block showed no evidence of external tool marks, handling damage or other physical features that could be held as contributory to fatigue initiation.\
The blade root block carried the embossed and engraved identification:
Trailing edge face: C2179 1H1153 < 22>
Leading edge face: LK83851 TA6939B < 9> < 13> < 29> < 201>
The engine manufacturer confirmed that the numbers represented as <xx> above indicated the application of various repair schemes during prior blade overhaul/s. On review, none of those schemes contained actions involving activity at or in the vicinity of the fatigue origin. The manufacturer also indicated that the engraved (vibro-etched) markings '< 201>' had been placed closer to the shank edge than allowed by the particular repair scheme, and that markings too close to section corners have the potential to adversely affect the blade integrity. In this instance however, the cracking showed no association with the < 201> marking, or any other similar feature.
1.3. Metallography & micro-analysis
A serial grind-polish-examine process was used to investigate and characterise the features at and surrounding the fatigue origin. The plane of grinding was parallel to the trailing edge root block face and a total of four metallographic planes were examined through the origin area. A fractured and intrusive dark oxide-like material inclusion was observed during the second stage of examination (figure 8).
Figure 8 and 9: Metallographic cross-section through origin and EDS spectra of inclusion present at arrow
Energy dispersive x-ray analysis (EDS, figure 9) of the inclusion identified a range of elements from the typical base metal chemistry (Ni, Nb, Ti), as well as zirconium (Zr) which was foreign to the base metal alloy, but later identified as a component of the refractory moulding material used during the investment casting of the turbine blades. Dimensionally, the visible sections of the inclusion measured approximately 40 µm in the major dimension, with the engine manufacturer indicating that the maximum root defect dimension allowable by the relevant quality acceptance standards (QAS) was in the order of 508 µm (0.2").
The general blade microstructure was typical of a cast nickel-based high temperature alloy, with massive semi-script form carbides within a solid-solution (?, gamma) matrix.
1.4. Chemical analysis
Spectrographic analysis techniques identified the base LPT blade alloy as an IN713LC nickel-chromium-aluminium-molybdenum material. The engine manufacturer confirmed this as the intended LPT blade alloy.
1.5. Fatigue loading and operating conditions
The initiation of fatigue cracking within any component is an
indication that the magnitude and number of local stress cycles
sustained have exceeded the limits of the material at the crack
origin. Components such as the LPT-2 blades that do not have a
prescribed fatigue life limit are engineered such that the nominal
and expected transient design stresses and stress cycles are kept
below the threshold for fatigue initiation. Where fatigue cracking
does initiate in these items, it is, by implication, an indication
that either the component has been subject to general stresses
above the design limits, or that some anomaly has acted to locally
concentrate the stresses in the affected area. The presence of
notches, tool marks, physical defects, inclusions or
microstructural abnormalities can all lead to local stress
concentration effects, thus providing conditions suitable for
fatigue crack initiation.
In the analysis of previous LPT-2 blade failures, the engine manufacturer had implicated uneven fuel distribution issues in the excitation of blade vibration sufficient to produce high-cycle fatigue cracking. In this instance however, there was no reported evidence from the engine examination to suggest that fuel distribution or combustion conditions had been problematic, or that those conditions had contributed to the blade failure.
The LPT-2 blade fracture morphology indicated that failure had
resulted from a progressive high-cycle fatigue (HCF) mechanism,
initiated from a surface or near-surface inclusion at the rear
trailing corner of the blade root section. The inclusion chemistry
and morphology suggested its origin from the refractory mould used
to cast the blade during initial manufacture.
Given that inclusions and other entrained discontinuities are inherently difficult to avoid in components produced by casting processes, limits are conventionally placed on the size and location of such features to maintain the structural integrity of the items under static and dynamical loading conditions. In this instance, although the dimensions of the visible portion of the inclusion were below the manufacturer's allowance for discontinuities of that nature, it was possible that the defect in total may have been considerably larger, being broken up and partly lost during the blade fracture and separation.
The following conclusions were drawn from the examination of the failed LPT-2 blade from RB211-524D2 engine serial number 12682.
1. Blade failure resulted from the initiation and growth of a fatigue crack from the rear trailing corner of the blade root section.
2. Physical evidence suggested the initiation of cracking from a casting inclusion formed during blade manufacture.
|Date:||22 October 2004||Investigation status:||Completed|
|State:||International||Occurrence type:||Engine failure or malfunction|
|Release date:||26 April 2006||Occurrence category:||Incident|
|Report status:||Final||Highest injury level:||None|
|Aircraft manufacturer||The Boeing Company|
|Type of operation||Air Transport High Capacity|
|Damage to aircraft||Nil|
|Departure point||Honolulu, USA|
|Departure time||1100 UTC|