The Sikorsky S76C helicopter was in cruise flight with the
automatic flight control system engaged, when the flight crew noted
a loud noise and the helicopter yawed to the left, rolled left, and
the nose pitched down. The flight crew disengaged the automatic
flight control system and resumed flying the helicopter manually,
stabilising it in level flight. The right engine-out and
fire-warning annunciators were illuminated, with the engine-out
aural warning sounding. The right engine instruments displayed zero
rotational speed of the gas generator (GG) and extremely high
turbine outlet temperature (measured at point T4 within the
engine). The crew activated the right engine fire bottles and
simultaneously closed the fuel firewall shut-off valve. The fire
indication extinguished. They then configured the helicopter for
single engine flight with the remaining engine operating
approximately ten seconds into the two and one-half minute One
Engine Inoperative (OEI) limitation. The flight crew adjusted power
requirements for the OEI condition and then completed an uneventful
single engine landing at their Longford base.
Examination of the helicopter revealed minor shrapnel damage to
the right engine exhaust extension, and fracture separation of the
engine oil pressure switches and rear bearing external oil vent and
return pipes.
The Turbomeca Arriel model 1S1 engine comprised five modules.
Module three (or the high-pressure section) contained the gas
generator first and second stage wheels. The left side of the right
engine, forward of the external rear bearing oil return line near
the outer surface of module three, displayed evidence of fire and
oil residue.
The right engine was removed and shipped to the engine
manufacturer's Australian facility for disassembly and examination
with Australian Transport Safety Bureau (ATSB), operator, and
engine manufacturer representatives in attendance.
Engine examination
Disassembly and preliminary examination of Arriel 1S1 engine,
serial number 15038, revealed a separation of one GG second stage
turbine blade. Blade number sixteen was separated above the blade
'fir tree' attachment point, below the blade platform, and had
punctured the second stage nozzle guide vane turbine ring. The rear
bearing of the GG had collapsed and was significantly damaged.
Separated pieces of the centrifugal diffuser of module three were
found inside the module. There were indications that several
fracture surfaces of the separated sections were pre-existing
before the incident. In addition, the engine exhibited signs of
severe overheating and significant damage in the air path
downstream of the turbine blade separation.
The fracture surface of the separated blade was typical of
ductile tensile overload, with the exception of the small corner
area of fatigue cracking. The dendritic patterns within the
fracture were indicative of the normal underlying microstructure of
the blade casting. Failure of the blade in that mostly ductile
overload manner indicated exposure to a transient or sustained
stress level above the ultimate strength of the blade material at
its operating temperature. Refer to ATSB Technical Analysis Report
200103038 (BE/200100017) for further details.
Engine history
The engine was installed on 4 March 2000 and had accumulated
7,935.0 hours and 6,784.1 cycles since new. It had been overhauled
on 12 February 1999, and had accumulated 1,992.0 hours time since
overhaul (TSO) and 1,878.1 cycles since overhaul. The GG assembly
second stage turbine disc, serial number DC3666YC, had been
installed during the overhaul with zero hours and cycles
accumulated. The turbine disc and blades were well within the life
limit of 10,000 cycles established by the manufacturer. Arriel
engine modification TU204 (GG turbine blade plasma coating) had
been incorporated.
Previous Australian occurrences
Occurrence report 200100584
On 7 February 2001, a Sikorsky S76C helicopter belonging to the
same operator, with two crew and ten passengers on-board, was in a
hover with the flight crew completing before take-off checklist
items. The pilot reported that while trimming the engines, a "pop"
was heard. He then noted that the left engine turbine gas
temperature (measured at point T4 within the engine) was in excess
of 1000 degrees C. The helicopter was then landed uneventfully. The
flight crew reported that the only cockpit indication of imminent
failure was the almost simultaneous illumination of the left engine
chip (magnetic particle) detector advisory.
Examination of the helicopter revealed minor shrapnel damage to
the left engine exhaust extension and engine cowling. There was no
reported engine fire. The left engine was removed and sent to the
engine manufacturer for disassembly and examination. The
manufacturer's final report noted a separation of turbine blade
number six of the GG second stage disc. The blade was separated
above the 'fir tree' attachment point but below the blade platform,
and had punctured the second stage nozzle guide vane turbine ring.
One adjacent blade (number seven) in the direction of turbine wheel
rotation was also noted as cracked.
Metallurgical examination by the manufacturer attributed the
blade failure to a low-cycle fatigue cracking mechanism. The
manufacturer concluded that abnormal loading was the major
contributing factor in the failure, given the reported absence of
anomalous material features or evidence of high-temperature
operation. Dimensional inspections failed to reveal any sign of
non-conformity that could have led to the development of the
abnormal loads. However, the manufacturer stated that turbine blade
platform/GG disc interferences were also a potential factor that
could have aggravated the fatigue failure of the blade.
At the time of the occurrence, Arriel 1S1 engine, serial number
15522, had accumulated 4,737.4 hours and 4,471 cycles since new. It
had accumulated 1,740.0 hours TSO and 1,615 cycles since overhaul.
Following overhaul, the engine was installed on March 11, 1999.
Module three did not have turbine blade plasma coating modification
TU204 incorporated.
Occurrence report 199602839
On 9 September 1996, a Sikorsky S76C helicopter belonging to the
same operator, experienced an in-flight engine failure of the right
engine while taking off from an oil platform. A loud noise was
heard before the engine failure. The right engine was shut down and
the crew completed an uneventful single engine return to the
Longford base. There was no reportedassociated engine fire. The
right engine was removed and sent to the manufacturer
fordisassembly examination.
At the time of the occurrence, Arriel 1S1 engine serial number
15513, had accumulated 2,282.0 hours and 1,949 cycles since new.
The manufacturer provided the operator with a final report noting
the rupture (separation) of one GG turbine blade with subsequent
rear bearing damage and GG seizure. Their report stated that the
separation was suspected to be the result of blade rubbing with the
second stage nozzle guide vanes with no signs of fatigue or
abnormal over temperature operation. Module three had turbine blade
plasma coating modification TU204 incorporated.
Other overseas occurrences
The French airworthiness authority, Direction Generale de
l'Aviation Civile (DGAC), reported knowledge of three other
overseas occurrences involving GG second stage turbine blade
separation failures. Of those three incident engines, all had the
TU204 modification. Cycles since overhaul on those incident engine
turbine discs and blades varied from 1,978 to 5,933 cycles.
Engine service bulletin history
Turbomeca Service Bulletin (SB) 292 72 0151 was originally
issued on 5 June 1992 specifying the incorporation of modification
TU204, the protection of the GG second stage turbine blades from
corrosion or erosion with a Heurchrome low pressure plasma coating.
That modification also permitted a performance improvement by
allowing the more accurate machining of the turbine tip diameter to
control the tip clearance. The service bulletin addressed all
Arriel variants, with Arriel 1S1 engines having incorporated TU204
from the first production engine. For all other variants, TU204
implementation was optional and installed at the customers'
request.
In July 1998, the engine manufacturer implemented internal
documentation and procedures to remove all GG turbine blades with
TU204 installed during overhaul of module three. Consequently, SB
292 72 0151 was amended on 18 August 2000, to recommend removal of
all TU204 modified blades, citing possible weight mass increases
and suspected increased stress on the turbine blade root. The
manufacturer stated that if the plasma coating was not applied as
per drawing requirements, the resulting stresses could be more than
anticipated, resulting in abnormal loading of the blade root. Both
incorporation and removal of modification TU204 required removal of
the engine and/or module and shipment to the manufacturer.
External oil pipe description
Three external oil related pipes provided lubrication of the GG
rear bearing. Those pipes passed through hollow support struts and
were then physically secured to module three. The supply oil pipe
provided oil from the engine driven gear type oil pump to the
bearing after passing through a restrictor and a tube screwed into
the bearing housing. Oil was then sprayed onto the bearing. After
lubricating the bearing, the oil fell by gravity to the bottom of
the housing, through a tube and was returned to the tank through an
oil pipe to the scavenge pump. The air/oil mist that resulted from
the lubrication of the bearing was vented overboard through a vent
pipe attached to the top of the housing.
Engine oil flashpoint/autoignition
The engine oil temperature of a normally operating Arriel 1S1
engine in a S76C helicopter was approximately 100 degrees Celsius
(C). The flash point of the turbine engine oil was approximately
223 degrees C. The flash point of a liquid was defined as the
lowest temperature at which a material would produce a flammable
vapour, and was a measure of the volatility of the material.
The auto-ignition temperature of engine oil was approximately
388 degrees C. Auto-ignition temperature was defined as the
temperature at which auto-igniting materials spontaneously combust.
According to the engine manufacturer, during normal operation, the
external surface temperatures of number three modules ranged
between 280 to 450 degrees C, dependent upon location on the
module, with a maximum surface temperature of 450 degrees nearest
the rear bearing. The surface temperature maximum values of module
three were well within the auto-ignition temperature of the engine
oil.